ML20057B927

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Insp Rept 50-440/93-18 on 930822-27.Violations Noted But Not Cited.Major Areas Inspected:Review of Two Issues Re Eop,Including Ability of Plant Procedures to Meet Intent of BWROG Guidelines for Secondary Containment Control
ML20057B927
Person / Time
Site: Perry  
Issue date: 09/18/1993
From: Langstaff R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20057B922 List:
References
50-440-93-18, NUDOCS 9309240156
Download: ML20057B927 (11)


See also: IR 05000440/1993018

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U. S. NUCLEAR REGULATORY COMMISSION

REGION III

Report No. 50-440/93018(DRS)

Docket No. 50-440

License No. NPF-58

Licensee:

Cleveland Electric Illuminating Company

Post Office Box 5000

Cleveland, OH

44101

Facility Name:

Perry Nuclear Power Plant

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Inspection At:

Perry Site, Perry OH

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Inspection Conducted:

August 22 - 27, 1993

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Inspectors:

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Lead InspYctor

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Approved Byg ~ruce L. Burgess (Chief

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Operational Programs Section

Inspection Summary

Inspection on Auaust 22 - 27, 1993 (Report No. 50-440/93018(DRS))

Areas Insoected:

Reactive, announced safety inspection to review two issues

pertaining to emergency operating procedures (EOPs). The specific issues

reviewed were the ability of plant procedures to meet the intent of the

Boiling Water Reactor Owner's Group (BWR0G) guidelines for secondary

containment control and the effects of containment venting upon surrounding

buildings.

Results:

The licensee's recent actions taken to address issues pertaining to

E0Ps were, in general, comprehensive and conservative.

Issues pertaining to secondary containment control as a result of previous

inadequate reviews have been addressed. The licensee's recent review and

subsequent actions were comprehensive in nature.

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Inspection Summary

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Appropriate interim corrective actions were taken in response to concerns

associated with the effects of containment venting upon surrounding buildings.

The most significant concern was the potential to overpressurize the fuel

handling building.

A. violation was identified because potential

overpressurization of the fuel handling building should have been identified

previously. However, no notice of violation will be issued because the

violation is within the scope of an existing violation for which corrective

actions were still ongoing.

Additional engineering analyses were planned in

order to fully address the concerns.

In general, communication and interdepartmental teamwork associated with

resolution of the above issues was considered good.

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REPORT DETAILS

1.

Persons Contacted

Cleveland Electric Illuminatina Company (CEI)

M. Bezilla, Manager, Operations

K. Donovan, Manager, Regulatory Affairs

C. Angstadt, Senior Project Engineer, Perry Nuclear Engineering Dept.

G. Chasko, Operations Engineer, Operations

V. Colacicco, Reactor Operator, PEI Improvement Team

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W. Colvin, Member, Independent Safety Engineering Group

J. Lausberg, Supervisor, Quality Assurance

J. Messina, Operations Staff Supervisor, Operations

E. Ortalan, Senior Engineer, Perry Nuclear Engineering Dept.

J. Pelcic, Engineer, PEI Improvement Team

T. Rausch, PEI Coordinator, PEI Improvement Team

L. Routzahn, Compliance Engineer, Regulatory Affairs

P. Schuerger, Engineer, PEI Improvement Team

A. Silakoski, Member, Independent Safety Engineering Group

B. Stetson, Unit Supervisor, PEI Improvement Team

A. Widmer, Engineer, Perry Nuclear Engineering Dept.

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U.S. Nuclear Reaulatory Commission (NRCl

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A. Vegel, Resident Inspector

All of the individuals listed above attended the management exit meeting

held on August. 27, 1993. Other people were contacted during the

inspection including members of the licensee's operations and

engineering staffs.

2.

Action on Previously Identified Items

a.

(0 pen) Open Item (440/91013-04): During an August 1991 inspection

(Inspection Report 50-440/91013), there was no evidence that the-

licensee had modified applicable plant procedures to meet the

intent of the Boiling Water Reactor Owner's Group (BWROG)

Emergency Procedure Guidelines (EPGs) for secondary containment

control.

An inadequate review of existing procedures formed the

licensee's basis for not revising the procedures. As a result of

the inadequate review, the licensee considered existing procedures

to meet the intent of the secondary containment control guidelines'

and the licensee presented this view to the NRC in a October 31,

1991 response to a licensing commitment.

In response to a ,

May 1993 inspection (Inspection Report 50-440/93007), the licensee

performed an additional review and identified that existing

procedures did not meet the intent of the secondary. containment

control guidelines. Applicable procedures were modified to meet

secondary containment guidelines. The 'resulting procedure changes

are discussed in Section 3 of this report.

Specific details

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concerning the review of the secondary containment control

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guidelines evaluated during this inspection are as follows:

(1)

Adeauacy of 1993 Review:

The inspectors evaluated the

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review performed in-1993 and considered the review to be

adequate in both depth and scope.

No concerns were

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identified with respect to the conclusions drawn or

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recommendations made. As a result of the 1993 review, the

licensee determined that existing plant procedures did not

meet, for many steps, EPG guidance for secondary containment

control guidelines and informed NRC Region III on August 13,

1993.

In general, existing procedures lacked specific

operator guidance for when ta enter an E0P flowchart for

reactor pressure vessel (RPV) control, shutting down the

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reactor, and emergency depressurization of the reactor for

conditions outside of the containment structure.

The review

evaluated by the inspectors was documented in the licensee's

draft report " Multi-Discipline Review of How Existing Perry

Instructions Meet the Intent of the BWROG EPG Secondary

Containment Control Guideline," dated August 26, 1993.

(2)

Information Reauested: During discussions held August 30,

1993 and September 3, 1993 between L. Routzahn of Centerior

Energy and R. Langstaff of the NRC, it was agreed to delay

submittal of licensee's evaluation concerning secondary

containment control until issuance of this inspection

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report.

The inspectors requested that the following

information be provided as part of the submittal:

(1) a

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summary of the report developed to determine how existing

instructions met the intent of the secondary. containment

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control guideline; and (2) any corrections to the

conclusions presented in previous submittals concerning

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secondary containment control.

The licensee agreed to

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provide a copy of the final report to the NRC residents

office onsite.

This item will remain open pending receipt

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and review of the requested submittal.

b.

(0 pen) Violation (440/93007-01): The writer's guide for E0Ps was

not appropriate to the circumstances because it permitted

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inconsistent usage of a flowchart symbol. - As a result, operators

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did not use the flow path intended by the E0Ps for steps -

associated with " Emergency Depressurization is Required."

In

correspondence dated August 6, 1993, the licensee committed to

performing an interim change by August 30, 1993 to the E0P

flowcharts to correct the specific example cited by the violation.

During this inspection, the inspectors reviewed the interim change

planned which consisted of identifying the appropriate flowchart

or action leg in addition to the phrase " Emergency

Depressurization is Required" for the affected steps.

No concerns

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associated with the planned change were identified. The licensee

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also committed to performing an E0P improvement program with

completion projected for June, 1994. This violation will remain

open pending review of the licensee's E0P improvement program

effectiveness.

c.

(0 pen) Violation (440/93007-02): Corrective actions for a

previous violation concerning ineffective validation and

verification (V&V) of E0Ps were inadequate. As a result, the

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" unsafe region" of a heat capacity limit curve was not marked

which was contrary to the E0P writer's guide. Consequently, two

operators were not able to correctly identify the " unsafe" region

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of a heat capacity limit curve.

In correspondence dated August 6,

1993, the licensee committed to performing an interim change by

August 30, 1993, to the E0P flowcharts to correct the specific

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example cited by the violation. During this inspection, the

inspectors reviewed an interim change which consisted of marking

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the " unsafe" region of the heat capacity limit curve.

No concerns

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associated with the planned change were identified.

The licensee

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also committed to performing an E0P improvement program with

completion projected for June 1994.

During this inspection,

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another example of ineffective V&V was identified and is discussed

in Section 4.

However, the additional example is considered

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within the scope of a violation for which corrective actions were

still ongoing.

Consequently, no new Notice of Violation (NOV)

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will be issued for this example. This violation will remain open

pending review of the licensee's E0P improvement program

effectiveness.

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3.

Secondary Containment Control

During a review performed at the request of the NRC, the licensee

identified that existing plant procedures did not meet the intent of the

EPG guidance for secondary containment control for many steps of the EPG

guidance.

The review is discussed above in Section 2.a of this report.

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Procedures were revised to meet the intent of secondary containment

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control guidelines and put in place August 16, 1993. No concerns were

identified with respect to the procedure revisions.

Details are as

follows:

a.

Procedure Revisions: The inspectors concluded that the procedure

revisions were sufficient to meet the intent of the secondary

containment control guidelines. The inspectors reviewed procedure

ON1-Nil, " Pipe Break Outside Containment (Unit 1)," which was

revised on August 16, 1993. The revision was made to identify

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maximum safe operating limits and provide appropriate operator

actions in order to meet the intent of secondary containment

control guidelines.

Procedure ON1-017, "High Radiation Level

Within Plant (Unit 1)," and several alarm response instructions

were also revised to reference ON1-Nil for conditions pertaining

to the secondary containment control guidelines.

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b.

Sunnortina Documentation: No concerns were identified with

respect to the methodology used to develop maximum safe operating

limits.

The maximum safe operating limits for areas outside of

containment were developed in order to meet the intent of the

secondary containment control guidelines. The bases for these

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limits were documented by design input record, " Maximum Safe

Operating Limits (Temperature, Water Level, Radiation)," for

procedure ONI-Nil, dated August 13, 1993. Temperature and

radiation level limits were based on existing equipment

qualification information listed in the updated safety analysis

report (USAR). Water level limits were developed based on

walkthroughs of affected rooms to identify the lowest equipment

important to safety not environmentally qualified for. submergence.

c.

Procedure Change Implementation: The inspectors concluded that

implementation of the procedure changes associated with meeting

the intent of the secondary containment control guidelines was

acceptable. Two observations concerning implementation were made

by the inspectors as follows:

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(1)

Although not required by existing administrative procedures,

two independent reviewers performed a verification of the

revised procedure ONI-N11.

In addition, comments obtained

from operators during training were documented.

However,

both the reviewer and operator comments were generated

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subsequent to the revision of ONI-N11.

Consequently, these

comments were not considered for the August 16, 1993

revision. The licensee planned to consider the comments for

future procedure revisions.

(2)

The licensee painted level markings on the walls of affected

rocas to reflect maximum safe water levels. The inspectors

were able to visually locate the level markings.

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No violations or deviations were identified in this area.

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4.

Containment Ventina

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During the licensee review of how existing plant procedures met the

intent of the EPG secondary containment control guidelines, the licensee

identified concerns associated with containment venting and its effects

upon surrounding buildings. The most significant concern identified was

potential overpressurization of the fuel handling building.

An interim

procedural change was made to provide an unobstructed vent path until

additional engineering analyses could be performed to assess the

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concern. The inspectors concluded that the licensee's interim

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corrective actions were conservative and appropriate. The concerns were

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documented by Condition Report (CR)93-178, dated August 17, 1993 and

NRC Region III was informed August 18, 1993. A preliminary

investigation of the concerns was documented in a Management Preliminary

Report (MPA) dated August 19, 1993. A violation was identified because

the potential overpressurization of the fuel handling building should

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have been identified during technical verification of E0P procedures

performed in 1991.

However, no Notice of Violation will be issued

because corrective actions for an existing violation were still ongoing

at the time of this inspection.

Details are as follows:

a.

Potential Overoressurization of the Fuel Handlina Building:

Each

of the containment vent paths specified by the E0Ps vented to the

spent fuel pool in the fuel handling building.

Preliminary

calculations showed that during certain accident scenarios, steam

flow rates during containment venting would be substantially in

excess of the fuel handling building's exhaust ventilation system

capability.

In addition, vesilation system dampers held open

with fusible links could cloo and isolate the exhaust ventilation

system due to high temperatures. Consequently, the potential for

overpressurization of the fuel handling was identified.

The MPA

for CR 93-178 recommended providing instructions to open a roll up

door in the fuel handling building prior to containment venting

thereby providing an unobstructed vent path as interim corrective

action.

Although the concern was self-identified by the licensee, the

potential for overpressurization of the fuel handling building

should have been identified previously.

For example, the vent

paths from the spent fuel pool area were not sufficiently

addressed in correspondence to the NRC dated July 29, 1986, which

submitted the Perry unique analyses for emergency containment

venting.

This submittal did not identify problems associated with

venting using the fuel handling building exhaust ventilation

system.

In addition, the licensee did not identify these concerns

during technical verification of containment vent paths performed

in response to a Severity-Level Ill violation identified in

Inspection Report 50-440/91013. As such, the inspectors

considered the lack of adequate technical verification identified

by tbis concern to be an example of inadequate E0P verification

and validation (V&V).

However, this example is within the scope

of an existing violation concerning ineffective corrective action

with respect to V&V (Violation 440/93007-02).

Consequently, no

NOV will be issued for this example because corrective actions for

the existing violation were still ongoing at the time of this

inspection,

b.

Other Concerns Identified:

In addition to potential

overpressurization of the fuel handling building, several other

concerns were identified by CR 93-178.

However, no additional

interim corrective actions were deemed necessary for the reasons

detailed below. The inspectors considered the licensee's actions

acceptable on an interim basis and did not identify any other

concerns. The additional concerns were:

(1)

Increased radiation levels and environmental conditions

adverse to personnel safety were identified during review of

conditions caused by containment venting into the

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intermediate building. CR 93-178 specifically identified

venting from a surge tank vent as being a concern. However,

the MPA for CR 93-178 noted that there was no need to enter

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he surge tank area during containment venting.

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Consequently, no interim corrective action was deemed

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necessary to address this concern. During review of the

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building's ventilation system, the inspectors identified the

potential for conditions adverse to personnel safety in the

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control rod drive (CRD) pump room from containment venting

due to the interconnection of ventilation ductwork.

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However, E0P related actions in the CRD pump room would

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likely have already been performed prior to containment

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venting, negating the need for additional access by plant

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personnel.

The licensee planned to review this issue

further to assess the potential adverse impact on personnel

safety and equipment.

(2)

The spent fuel pool water level may swell above the building

floor during containment venting and potentially flood lower

elevations. The licensee deemed additional engineering and

operations review necessary to assess this concern.

Consequently, no interim corrective action was deemed

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necessary to address this concern.

(3)

Previous calculations for determining the primary

containment pressure limit did not consider the back-

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pressure against containment venting caused by the head of

water in the spent fuel pool above the point of venting.

No

interim corrective action was deemed necessary because other

calculations demonstrated sufficient containment vessel

capacity exists to accommodate such back-pressure.

The

licensee planned to revise the calculations for determining

the primary containment pressure limit to consider back-

pressure effects.

c.

Planned Enaineerina Analyses: To fully address the above concerns

associated with containment venting, the licensee planned to

perform additional engineering analyses. The licensee anticipated

completing the necessary analyses by the end of December,1993.

The inspectors requested the licensee to submit the following

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information upon completion of the analyses:

(1) a summary of the

engineering analyses results and planned corrective actions; and

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(2) any necessary corrections to the Perry unique analysis for

emergency containment venting previously submitted to the NRC.

The licensee's response will be tracked by an inspection followup

item (440/93018-01).

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d.

Procedure Chance implementation:

The licensee revised an E0P

support procedure on August 22, 1993, to provide instructions for

opening a roll up door in the fuel handling building to provide an

unobstructed vent path from the spent fuel pool area.

The

procedure revised was section 7.1, " Preparation for Containment

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Venting," of procedure PEI-SPI, "Special Plant Instructions." The

inspectors concluded that implementation of this procedure change

was acceptable.

Specific comments are as follows:

(1)

The inspectors considered the procedure revision acceptable

in providing an unobstructed vent path from the fuel

handling building. However, the licensee took credit for

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filtering by the exhaust ventilation system in their

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licensing submittal concerning emergency containment

venting, dated July 29, 1986. This filtering is bypassed

when the door i.s used as a vent path. The licensee agreed

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to address this issue, if necessary, depending upon.the

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final resolution for containment venting and the concern

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associated with overpressurization of the fuel handling

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building.

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(2)

No concerns were identified during a walkthrough of the

revised procedure with a non-licensed operator.

No

procedural nomenclature discrepancies were identified.

The

inspectors noted additional lighting had been provided in

the area near the roll up door.

(3)

V&V of the revised procedure was good. Comments generated

during V&V were indicative of a thorough review and were

properly dispositioned.

For example, minor problems

associated with manual operation of.the roll up door were

identified during V&V and appropriate maintenance work was

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initiated.

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(4)

Two minor discrepancies associated with the revised

procedure were identified. The licensee planned to address

these discrepancies as part of their E0P improvement

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program.

The discrepancies were

(a)

Line spacing in the revised procedure was not in

accordance with that specified by the support

procedure writer's guide, attachment 2, " SPI Writers

Guide," to procedure PAP-0524, " Development of Plant

Emergency Instructions," Revision 0.

However, the

inspectors considered the line spacing used to provide

greater readability and to be a considerable

improvement over that specified by the writer's guide.

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(b)

Two abbreviations, "CAS" and "SAS," were used in the

revised procedure which were not listed as approved

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abbreviations by PAP-0524.

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5.

Communications and Interdepartmental Teamwork

The E0P related revisions provided an opportunity for the licensee to

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demonstrate effective communications and interdepartmental teamwork

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under time restraints.

In general, the inspectors considered

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communications and interdepartmental teamwork to be good.

Cooperation

between operations and engineering was evident.

However, such

cooperation was expected because the E0P improvement program was planned

as a multi-disciplinary effort with operations as lead.

Specific

observations were as follows:

a.

Monitorina of Radioactive Release Points:

No followup action was

initiated with appropriate personnel to address the feasibility of

monitoring a potential release through the fuel handling building

roll up door.

For interim corrective action, not having

provisions for monitoring such a release was acceptable because

the site emergency plan addressed unmonitored releases.

However,

because monitoring such a release is desirable, the inspectors

considered additional discussions with appropriate personnel to

address the feasibility of monitoring warranted.

The licensee

agreed to review the issue further.

The inspectors recognized

corrective actions were still in progress at the time of the

inspection and that additional review and evaluation of this issue

was planned,

b.

System Engineer Knowledge:

The system engineer for the fuel

handling building ventilation system was not fully aware of the

issues discussed by CR 93-178.

The inspectors recognized that the

individual did not require an immediate knowledge of the condition

report because operability of the ventilation system was not an

issue nor was he directly involved in the engineering analyses

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beir,g performed. However, considering the significance of the

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issue and that the ventilation system was affected by it, the

inspectors were surprised that the individual was not more aware

of the issues discussed by the condition report.

c.

Role of Security:

In addition to operations personnel, security

personnel had a role in performance of PEl-SPI, Section 7.1.

Based on an interview with a security shift supervisor, the

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inspectors concluded that security's knowledge and understanding

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of their role to support E0P implementation was good.

d.

Trainino: Training provided to operators for the procedure

changes associated with both meeting the intent of the secondary

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containment control guidelines and providing and unobstructed vent

path for containment venting was good.

For each change, operators

were briefed for approximately a half hour prior to coming on

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shift.

Supplemental information such as reasons why the changes

were being made was provided.

Two of the training sessions were

observed by other inspectors and were considered to be good.

No violations or deviations were identified in this area.

6.

Inspection Followup Items

Inspection followup items are matters which have been discussed with the

licensee, which will reviewed further by the inspectors, and which

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involve some action on the part of.Jbe NRC or licensee or both.

An

inspection followup item was disclosed during this inspection and is

discussed in Section 4 of this report.

7.

Exit Meetina

The inspectors met with licensee representatives (denoted in

Paragraph 1) on August 27, 1993.

The inspectors summarized the purpose,

scope, and findings of the inspection and the likely informational

content of the inspection report.

The licensee acknowledged this

information and did not identify any information as proprietary.

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