ML20055A921
| ML20055A921 | |
| Person / Time | |
|---|---|
| Site: | Farley |
| Issue date: | 07/06/1982 |
| From: | Hairston W ALABAMA POWER CO. |
| To: | |
| Shared Package | |
| ML20055A920 | List: |
| References | |
| NUDOCS 8207200131 | |
| Download: ML20055A921 (7) | |
Text
E i
OPERATING DATA REPORT I
DOCKET NO.
50-364 8
DATE 7/06/82 LOMPLETED i1Y G Hairston III TELEP110NE
$TT99-5155 OPERATING STAT US Notes
- 1. Unit Name:
Te nh M.
1:'nriev Unit II
- 2. Reporting Period: June. 1982 1)
Cumulativedata since
- 3. Licensed Thermal Power (MWI):
2652 7/30/81, date of cone-
- 4. Nameplate Rating (Gross MWe):
R60 mercial operation S. Design Electrical Rating (Net MWe): R?o
- 6. Maximum Dependable Capacity (Gross MWe):
854.7
- 7. Masimum Dependable Capacity (Net MWe):
811.7
- 8. If Changes Occur in Capacity Ratings (items Number 3 Through 7)Since Last Report.Gise Reasons:
N/A
!^
- 9. Power Lesel To Which Restricted.If Any (Net MWe):
- 10. Reasons For Restrictions,1f Any:
.N/A i
4 This Month Yr..to Date Cumulatise 0
- 11. Ilours in Reporting Period 4343 8064
- 12. Number Of flours Reactor Was Critical 720 3A1A R 7117.0
- 13. Reactor Resene Shutdown flours 0
71_n
-111.8
- 14. Ilours Generator On-Line 720 1551.5 7??n O
- 15. Unit Resene Shutdown Hours n
0 0
- 16. Gross Thermal Energy Generated (MWil) 1.836.202 8.864.930 1R.331.087 17 Gross Electrical Energy Generated (MWill
___.585.148 2.843,240 s_414_618
- 18. Net Electrical Energy Generated (MWil) 555.884 2.687.130 5 607.850 81.8 89.5
- 19. Unit Senice Factor ice,9 l
- 20. Unit Asailability Factor 100.0 R1.R R9.5
' 21. Unit Capacity I' actor (Using MDC Net) 94.9 7A_n 85.5
- 22. Unit Capacity Factor (Using DER Net) 93.1 74.6 83.9 21 Unit Forced Outage Rate 0.0 18.2 10.5
- 24. Shutdowns Scheduled Oser Nest 6 Months (Type.Date,and Duration of Eacht:
Refueling Outage; October 22, 1982; Approximately 6 weeks.
- 25. If Shut Down At End Of Heport Period. Estimated Date of Startup:
N/A 2tn. Units in lest Status (Prior to Commercial Operation):
Forecast Achiesed INill A L CRITICA LII Y 5/6/81 5/8/81 INITI AL ELLCIRICITY 5/24/81 5/25/81
\\
COMMERCI A L Ol'ER A flON 8/1/81 7/30/81 4
(9/77 )
8207200131 820712 PDR ADOCK OSOOOg R
DOCKET NO.
sn_v A trNIT J. M. Ftrisy-Unit II DAlT. 7/06/82 COSIPLETED BY W.
C. Hnfrston, III s'
IILEPl!ONE (?nsi 809-5156 510f(111 DAY AVEllAGE DAILY POhEit LEVEL.
DAY AVER AGE DAILY POWER LEVEL (Mbe Net)
(MWe Net) g, 37 530 799
[3 528 2
808 3
803 39 551 4
7R1 20 778 3
Rn7 21 800 6
R1A 22 nni 7
R1A 23 803
]
g 811 24 806 9
__80R 25 804 10 ani 26 769 11 781 27 801 12 802 23 801 801 l3 802
- 9 798 14 Ana 30 15 803 33 16
- 749 I
INSTRUCl!ONS On this formst. list the average daily umt power levelin MWe Net for each d;y in the reporting inunth. Compute to
, the neare t whole nr:;2w.att.
I s
a (9p7)
. i tQ e.,
e e
~
4 l
neo go e
- Q.-
s
\\
-)
J UNIT SilUTDOWNS AND POWER REDUCTIONS DOCKET NO.
50- W.
UNIT NAME T-M rn vi m t',it II DATE 7/06/97 REPORT MONTH June, 1982 COMPLETED BY t'
c u,4veenn, III TELEPHONE nn53 noo_575g w.
$ wE c
c r.
No.
Date 1
h _I 3 5b g4 Cause & Corrective
'n y
gj 0
g3x Event y,?
g Action to jey Report a g
Prcvent Recurrence v) O 0-5 010 820617 S
0 B
NA NA HC HTEXCH Powr reduced to 71% for investi-gation and repair of condenser tube leaks, i
l l
l l
I 2
3 4
F: Forced Reason:
Method:
Exhibit G Instructions l
S: Scheduled A Equipsnent Failure (Explain) l-Manual for Pseparation of Data B Maintenance or Test 2 Manual Scram.
Entry Sheets for Licensee C. Refueling 3 Automatic Scram.
Event ReporI(LER) File (NUREG-D Regulatory Restriction 4-Other (Explain) 0161)
E-Operator Training & License Examination F-Administrative 5
i G-Operational Esrur (Explain)
Exhibit I Same Source (9/77)
Il-Other (E xplain) i t_______
e 4
JOSEPH M. FARLEY NUCLEAR PLANT UNIT 2 NARRATIVE
SUMMARY
OF OPERATIONS JUNE, 1982 There was one (1) power reduction in the month of June.
The following safety-related maintenance was performed in the month of June:
1.
Performed miscellaneous maintenance on diesel generators 2.
Repaired reactor makeup water discharge pipe to prevent leakage 3.
Repaired 2B BIT Recirculation Pump to prevent leakage 4.
Replaced grounded cable on #7 River Water Pump 1
l l
l l
I
I 1
OP8 RATING DATA RLPORT I
DOCKET NO.
50-364 8;
DATE.ll_Q6/82 COMPLETED liY LG. Hairston III TELEPilONE (205FBV9-5155 l I' OPERATING STA1US Notes I. Unit Name:.Jncoph M.
T'nriey Unit II
'P"'""8
'I" 1)
Cumulativedata since
- 3. Licenwd Thennal Power (MWt):
2652 7/30/81, date of com-
- 4. Nameplate Rating (Gross MWe):
R60 mercial operation
- 5. Design Electrical Rating (Net MWe): A70
- 6. Masimum Dependable Capacity (Gross MWe):
854.7 l
- 7. Masimum Dependable Capacity (Net MWe):
813.7
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7)Since Last Report,Gise Reamns:
N/A
^
- 9. Power Lesel To Which Restricted. If Any (Net.ilWe):
- 10. Reawns For Restrictions.If Any:
.N/A 1
This Month Yr..t o-Da t e Cumulatise 7
I1. Ilours in Reporting Period 4343 8064 720
- 12. Number Of Ilours Reactor Was Critical 363A R 7317.0
- 13. Reactor Resene Shutdown flours 0
71.n 111.8
- 14. Ilours Generator On-Line 720 1ss3d 7??n 0
- 15. Unit Resene Shutdown flours n
0 0
- 16. Gross Thermal Energy Generated (MWil) 1.83f. 202
_B H64,930 1R,331,087
- 17. Gross Electrical Energy Generated (MWil) 535J48 _,.
2,843,240
- 3414 618
- 18. Net Electrical Energy Generated (MWil) 555.884 2,687.130 5.607.850 81.8 89.5
- 19. Unit Senice Factor ice,9 e
- 20. Unit Asailability Factor 100.J)
R1 R 89.5 j
- 21. Unit Capacity Factor (Using MDC Net) 94 9 7A.n 85.5 93.1 74.6 83.9 l
- 22. Unit Capacity Factor (Using DER Net)
- 23. Unit Forced Outage Rate 0.0 18.2 10.5
- 24. Shutdowns Scheduled Oser Nest 6 Months (Type. Date.and Duration of Eacht:
Refueling Outage; October 22, 1982; Approximately 6 weeks.
- 25. If Shut Down At End Of Report Period.lXtimated Date of Startup:
N/A
- 26. Units in Test Status (Prior to Commercial Operation):
Forecast Achiesed r
1 INITI A L CRITICALITY 5/6/81 5/F/81 l
INiilAL ELECIRICITY 5/24/S1 5/25/81 COMMERCI AL OPER ATION 8/1/81 7/30/81 No (9/77)
DOCKET T40.
sn_3A A (JNIT J. M. Fzriny-Unit II D Aly, 7/06/82 COSIPLETED DY E. C. Itairston, III i
1ELEPil0NE, (2ns) Aqq-sis 6 MONTil DAY AVEllAGE D/.lLY POWEit LEVEL DAY AVER AGE D AILY POWER LEVEL (5114e Net)
($1We Net) 799 37 530 g,
IG 528 2
808 3
__ 801 19 551 4
7R1 20 778 5
_ Rn7 21 800 6
Al^
22 Ani 803 7
Ala 23 g
811 24 806
]
9
_ RnR 25 804
~
10 An1 G
769 27 801
' II 7R1 12 802 28 801 801 13 802
- 9 798 14 Roa jn 15 803 33 16
- _ 749 INSTRUCllONS On this formar. list the aversge daily unit power levet in MWe Net for each d
- y in the reporting snunth.Cornpute to
, the nease:t whole nepwait.
(907) d
. _,. ~ ~ - -
... _,n.
n
\\
,y rI m
n s
UNITSilUTDOWNS AND POWER REDUC 110NS DOCKEYNO.
50-164 UNiTNAME T v
r=riou itnit II DATE 7 /06 / R?
REPORT MONTH June, 1982 COMPLETED BY t.'
c n u vann, 111 TELEPHONE onu naa _Si u e.
's u 5 E
e c.
E
'3.gg Lie se E%
g*.
Cause & Currective N"'
D"
E.g
'y.a 3
.c s e Even' y,T Q
Action to m0 j ifi y Report #
g Picvent Recurrence oO E
5 010 820617 S
0 B
NA NA HC HTEXCH Power reduced to 71% for investi-gation and repair of condenser tube leaks.
l i
l I
I 2
3 4
F: Forced Reason:
Method:
. Exhibit C -Instsuctions S: Scheduled A-Equipment Failure (Explair.)
I-Manual for Preparation of Data B. Maintenance of Test
- 2. Manual Scram.
Entry Sheets for Licensee C-Refueling 3 Automatic Scram.
Event Repors (LER) File INUREG-D. Regulatory Restriction 4-Other (Explain) 0161)
E-Operator Training & License Examination F-Administrative 5
G-Operational En ror (Explain)
Exhibit I - Same Source (9/77) 110 her(Explain)
.