ML20054M112
| ML20054M112 | |
| Person / Time | |
|---|---|
| Site: | Hope Creek, Turkey Point, 05000000 |
| Issue date: | 06/15/1982 |
| From: | Pace P FLORIDA POWER & LIGHT CO. |
| To: | |
| Shared Package | |
| ML20054M092 | List: |
| References | |
| NUDOCS 8207090260 | |
| Download: ML20054M112 (3) | |
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SUMMARY
OF OPERATING EXPERIENCE DOCKET NO.
50-250 UNIT Turkey Point Unit No. 3 DATE June 15, 1982 COMPLETED BY Paul L. Pace TELEPHONE (305) 552-3654 REPORT MONTH May 1982 Unit 3 operated at essentially full power except for outages on 5/15, 5/19 and 5/20. See the " Unit Shutdown Report" and Power Reduction for details.
Major Safety-related maintenance activities performed during the month included:
Steam Generator Blowdown line snubber, and pipe hangers were rebaired.
Diesel Generator auto start compressor was repaired.
Inspections and requirements of IE Bulletins and NUREG-0737 are continuing.
Florida Power & Light Company commitments for NUREG-0737 Implementation are continuing. Refer to correspondence between FPL and NRC for additional information.
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SUMMARY
OF OPERATING EXPERIENCE DOCKET NO.
50-251 UNIT Turkey Point Unit No. 4 DATE June 15, 1982 COMPLETED BY P.L. Pace TELEPHONE (305) 552-3654 REPORT MONTH May 1982 Unit 4 operated at essentially full power for the entire month, except for an outage on May 5.
See the " Unit Shutdowns and Power Reductions" Report for details.
Major maintenance activities performed during the month included:
Diesel Generator auto start compressor was repaired.
Inspections and requirements of IE Bulletins and NUREG-0737 implementation are continuing.
Refer to correspondence between FPL and NRC for additional information.
See the " Unit Shutdowns and Power Reductions" Report for additional maintenance activities.
SUMMARY
OF OPERATING EXPERIENCE DOCKET NO.
50-335 UNIT St. Lucie Unit No. 1 DATE June 15, 1982 COMPLETED BY P.L. Pace TELEPHONE (305) 552-3654 IEPORT MONTII May 1982 Unit 1 operated at essentially full power except for the scheduled outage for steam generator tube inspector.
Major Safety-related maintenance activities performed during the month included:
Steam genergtor tube eddy current testing.
Reactor coolant pump seal repair.
Code pressurizer safety valve replacement Inspections and requirements of IE Bullentins and NUREG 0737 in progress.
Florida Power & Light Company commitments for NUREG-0737 implementation are continuing.
Refer to correspondence between FPL and NRC for additional information.
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