ML20054L988
| ML20054L988 | |
| Person / Time | |
|---|---|
| Site: | Beaver Valley |
| Issue date: | 01/21/1982 |
| From: | Timko D DUQUESNE LIGHT CO. |
| To: | |
| Shared Package | |
| ML20054L973 | List: |
| References | |
| NUDOCS 8207090128 | |
| Download: ML20054L988 (7) | |
Text
t DUQUESNE LIGHT COMPANY Beaver Valley Power Station Narrative Summary of Monthly Operating Experience - December, 1981.
December 1 Station in operational mode 1 at nominal 90% power.
Operating through at reduced load for fuel conservation.
December 14 December 15 Station in operational mode 1 at nominal 90% power. At 1829 hours0.0212 days <br />0.508 hours <br />0.00302 weeks <br />6.959345e-4 months <br /> reactor power was reduced 5% to aid the main feed water regulating valve (MFRV) FCV-FW-488 by reducing feed water flow to the B steam generator.
December 16 Station in operational mode 1 at nominal 85% power.
Between 0100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br /> and 2300 hours0.0266 days <br />0.639 hours <br />0.0038 weeks <br />8.7515e-4 months <br /> reactor power was reduced to 22% to by-pass the B MFRV for repairs.
December 17 Station in operational mode I at nominal 221 power for repairs to the B MFRV. At 0550 hours0.00637 days <br />0.153 hours <br />9.093915e-4 weeks <br />2.09275e-4 months <br />, after repairs were completed, B MFRV was placed back in service and began increasing power to approximately 48% power.
December 18 Station in operational mode 1 at nominal 49% power.
Operating through at reduced load for fuel conservation.
December 21 December 22 Station in operational mode 1 at nominal 49% power.
Between 0945 hours0.0109 days <br />0.263 hours <br />0.00156 weeks <br />3.595725e-4 months <br /> and 1036 hours0.012 days <br />0.288 hours <br />0.00171 weeks <br />3.94198e-4 months <br /> power was reduced to 34% in order to by-pass the B MFRV for replacement of a controller air regulator.
At 1050 hours0.0122 days <br />0.292 hours <br />0.00174 weeks <br />3.99525e-4 months <br />, after repairs were completed, B MFRV was placed back in service and began increasing load back to 49% power.
December 23 Station in operational mode 1 at nominal 49% power.
Operating through at reduced load for fuel conservation.
December 24 December 25 Station in operational mode 1 at nominal 49% power.
At 1845 hours0.0214 days <br />0.513 hours <br />0.00305 weeks <br />7.020225e-4 months <br /> the reactor was manually tripped due to loss of station instrument air.
December 26 Station in hot stand-by mode 3.
AT 1145 hours0.0133 days <br />0.318 hours <br />0.00189 weeks <br />4.356725e-4 months <br /> on the 26th it was decided to begin the major modifications and 2nd refueling outage.
December 27 Station in hot stand-by mode 3 due to main steam safety valve set through point check testing in progress.
December 28 8207090128 820108 PDR ADOCK 05000334 R
DUQUESNE LIGHT COMPANY Beaver Valley Power Station Narrative Summary of Monthly Operating Experience - December, 1981 (Continued)
December 29 Station in hot stand-by mode 3.
At 1308 hours0.0151 days <br />0.363 hours <br />0.00216 weeks <br />4.97694e-4 months <br /> began to cool down to cold shutdown mode 5.
At 1400 hours0.0162 days <br />0.389 hours <br />0.00231 weeks <br />5.327e-4 months <br /> entered hot shut-down mode 4.
December 30 Station in hot shutdown mode 4.
At 0238 hours0.00275 days <br />0.0661 hours <br />3.935185e-4 weeks <br />9.0559e-5 months <br /> station entered cold shutdown mode 5.
December 31 Station in cold shutdown mode 5 for major modifications and 2nd refueling outage.
I
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DUQUESNE LIGHT COMPANY Beaver Valley Power Station Major Safety-Related Maintenance - December - 1981 1.
- 2 rod drive motor generator set inboard motor bearings replaced.
2.
Air regulator replaced on main feed regulator valve [FCV-FW-488].
3.
Component cooling pump CCR-P-1B inboard and outboard motor bearings replaced.
4.
Component cooling pump CCR-P-lC shutdc m to rebuild motor.
5.
Auxiliary river water pump WR-P-9A declared inoperable due to loss of coolant to the packing.
l l
l' OPERATING DATA REPORT DOCKET NO. 50-334 DATE 1/21/82 COMPLETED BY D. R. Tinko TELEPHONE. 417-A41-1947 OPERATING STATUS
- 1. Unit Name: Beaver Valley Power Station, Unit #1 Notes
- 2. Reporting Period:
December, 1981
- 3. Licensed Thermal Power (MWt):
2660
- 4. Nameplate Rating (Gross MWe):
923
- 5. Design Electrical Rating (Net MWe):
852
- 6. Maximum Dependable Capacity (Gross MWe):
860 810
- 7. Maximum Dependable Capacity (Net MWe):
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since IJst Report, Give Reasons:
- 9. Power Level To Which Restricted,If Any (Net MWe):
None I
- 10. Reasons For Restrictions.If Any:
N/A This Month Yr.-to-Date Cumulative
!!. Hours In Reporting Period 744 8760 49,704
- 12. Number Of Hours Reactor Was Critical 594.75 6,532.62 21,059.29
- 13. Reactor Reserve Shutdown Hours 0
0 4,482.8
- 14. Hours Generator On-Line 594.75 6,447.81 20,154.06
- 15. Unit Reserve Shutdown Hours 0
0 0
- 16. Gross Thermal Energy Generated (MWH) 1,148,932.86 15.521.047.33 43.628,940.48
- 17. Gross Electrical Energy Generated (MWH) 381,000 5,023,100 13,650,440
- 18. Net Electrical Energy Generated (MWH) 349,205 4,662,450 12,523,954
- 19. Unit Service Factor 79.9 73.6 42.7
- 20. Unit Asailability Factor 79.9 73.6 42.7 i
l
- 21. Unit Capacity Factor (Using MDC Net) 57.9 65.7 34.8 L
- 22. Unit Capacity Factor (Using DER Net) 55.1 62.5 33.1
- 23. Unit Forced Outage Rate 20.1 26.4 40.2
- 24. Shutdowns Scheduled Over Next 6 Months (Type. Date.and Duration of Eacht:
Refueling Outage 12/28/81 20 weeks l
- 25. If Shut Down At End Of Report Period. Estimated Date of Startup:
May 21, 1982
- 26. Us.its in Test Status (Prior to Commercial Operationi:
Forecast Achieved i
INITIAL CRITICA LITY N/A N/A l
INITIAL ELECTRICITY N/A N/A COMMERCIA L OPERATION N/A N/A (9/77)
OPERATING DATA REPORT DOCKET NO. 50-334 DATE 1/4/82 COMPLETED BY D.
R.
Tinko TELEPHONE. 417-443-1947 OPERATING STATUS
- 1. Unit Name: Beaver Valley Power Station, Unit #1 Notes December, 1981
- 2. Reporting Period:
- 3. Licensed Thermal Power (MWt):
2660
- 4. Nameplate Rating (Gross MWe):
923 852
- 5. Design Electrical Rating (Net MWe):
- 6. Maximum Dependable Capacity (Gross MWe):
860 810
- 7. Maximum Dependable Capacity (Net MWe):
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
- 9. Power Level To which Restricted. If Any (Net MWe):
None
- 10. Reasons For Restrictions. lf Any:
N/A This Month Yr..to.Date Cumulative
- 11. Hours in Reporting Period 744 8760
'49.704
- 12. Number Of Hours Reactor Was Critical 594.75 6,532.62 21.059.29
- 13. Reactor Reserve Shutdown Hours 0
0 4,482.8
- 14. Hours Generator On.Line 594.75 6,447.81 20,154.06
- 15. Unit Reserve Shutdown Hours 0
0 0
- 16. Gross Thermal Energy Generated (MWH) 1,148,932.86 15,521,047.33 43.628,940.48
- 17. Gross Electrical Energy Generated (MWH) 181,000 _,
5,023,100 13,650,440
- 18. Net Electrical Energy Generated (MWH) 349,205 4,662,4AD 12,523,954
- 19. Unit Service Factor 79.9 73.6 42.7
- 20. Unit Availability Factor 79.9 73.6 42.7
- 21. Unit Capacity Factor (Using MDC Net) 57.9 65.7 34.8
(
- 22. Unit Capacity Factor (Using DER Net) 55.I 62.5 33.1 I
- 23. Unit Forced Outace Rate 20.1 26.4 40.2
- 24. Shutdowns Scheduled Over Next 6 Months IType. Date,and Duration of Eacht:
I Refueline Outage 12/28/81 20 weeks
- 25. If Shut Down At End Of Report Period. Estimated Date of Startup:
May 21, 1982
- 26. Units in Test Status (Prior to Commercial Operation):
Forecast Achieved INITIA L CRITICA LITY N/A N/A INITIAL ELECTRICITY N/A N/A l
COMMERCIA L OPERATION N/A N/A l
l (9/77) t
0 AVERAGE DAIL UNIT POWER LEVEL 50-334 DOCKET NO.
UNIT BVPS Unit #1 DATE 1/4/82 D. R. Timko COMPLETED BY TELEPHONE 412-643--1947 MONTH December, 1981 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)
(MWe-Net) 726 37 277 2
722 gg 385 3
734 39 389 4
726 20 377 5
735 376 21 734 369 6
22 731 385 7
3 g
734 377 24 9
734 291 25 10 730 26 0
II 734 27 0
12 734 0
28 13 734 0
29 14 734 30 0
15 730 0
3g 16 499 INSTRUCTIONS On this format. list the average daily unit power lesel in MWe Net for each day in the reportmg month. Compute io the nearest whole megawatt.
i
((1.1771
UNITSifUTDOWNS AND POWER REDUCTIONS DOCKET NO.
50-334 UNIT N AME BVPS Unit #1 DATE 1/4/82 REPORT MONTil December, 1981 COMPLETED BY
_D.
R.
Timko TELEPIIONE 412-643-1947,
i Q
.N 3 Licelhee
[-t, CJuse & Correstt%c No.
DJ'e g
3g g
_g g 5 Event s7 s.'E Action to
$3 E
j5g RcPort "
IiG j'
Prevent Recurrente c5 16 811216 F
0 B
4 Replaced "B" main feed regulating i
valve.
l l
l L
l 17 811222 F
0 B
4 Replaced air regulator on "B" main feed regulating valve.
18 811225 F
- 149.25 A
2 PA VALVEX Transfer valve on instrument air dryer inlet stuck in mid position, resulting in a loss of instrument air pressure. Reactor was manually tripped. Repaired transfer valve.
f Major modificati,ons and refueling outage, scheduled tg start on 1/2/82, was startyd early I week because of trip.
F: Forced Reason:
Method:
Exhibie G - Instructions S: Schedu!cd A.Equiprnent Failure (Explain) 1-Manual for Pseparation of Data B-Maintenance of Test 2-Manual Seraan.
Entr> Sheets for Licensee C. Refueling 3 Autonatic Scram.
Event Repori ILI:R) Fde (NUREG D Regulator) Restriction 4-Other I Explain) 01611 110peratot Training & License Examination F Admmistrative 5
G Operational Esfor liixplaint Eslubit 1 Same'Somee (9/77) 11 Other (E splaini