ML20052F853

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RO 82-22/1T:confirms That from 801218 Until 820418,all Unit Operations in Excess of 200 F Have Been Performed W/Combined Leakage Rate Greater than Specs for Penetrations & Valves Subj to Type B & C Testing
ML20052F853
Person / Time
Site: Calvert Cliffs Constellation icon.png
Issue date: 05/04/1982
From: Russell L
BALTIMORE GAS & ELECTRIC CO.
To: Haynes R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
References
RO-82-22-1T, NUDOCS 8205140043
Download: ML20052F853 (1)


Text

DE3IG:iATED 021GIIIAL Certified By 7 1 6. A i 4

B ALTIMORE G AS AND ELECTRIC COMPagYs O

P.O. BOX 1/.75 B ALTIM OR E M A R YL A N D 212o3 g%

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,,M713198gg -Q NUCLEAR power DEPARTMENT catvaar currs auctema ao.ca aca~r 9"

8g tusen uanytano ro m May 4,1982 c,

4 v3 ta Mr. Ronald C. Haynes, Director Docket No. 50-317 Oftice of Inspection and Enforcement License No. DPR-53 U. S. Nuclear Regulatory Commisssion Region 1 631 Park Avenue King of Prussia, PA.19406

SUBJECT:

LER 82-22/IT, Unit 1 Dear Mr. Haynes This letter is to confirm our verbal notification of your Mr.E. B. McCabe of our discovery that from 12-18-80 until 4-18-82 all Unit 1 operations in excess of 200 have been performed with a combined leakage rate of greater than 0.60 L f r all penetrations and valves subject to Type B and C tests a

(T.S. 3.6.1.2.b).

At 1400 on 5-3-82 it was confirmed that an error in Surveillance Test Procedure M-571-1, Local Leak Rate Tests, caused the total measured Type B and C leak rate to be compared to L versus 0.60 L as required by a

a T.S. 3.6.1.2.b.

A complete description of this event, including causes and corrective action will be addressed in a follow-up report.

Veryctruly yours,

$C5(diah L. B. Russell Plant Superintendent LBR:fid cc:

3. A. Tiernan R. M. Douglass Director, Office of Management R. E. Architzel Information & Program Control L. B. Russell R. B. Sydnor 8205140043 820504 PDR ADOCK 05000317 p 13 S

PDR g I,0

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