ML20050F866

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Monthly Operating Rept for Jul 1981
ML20050F866
Person / Time
Site: La Crosse File:Dairyland Power Cooperative icon.png
Issue date: 08/06/1981
From: Goodman L
DAIRYLAND POWER COOPERATIVE
To:
Shared Package
ML20050F856 List:
References
NUDOCS 8204130401
Download: ML20050F866 (8)


Text

.

s OPERATING DATA REPORT DOCKET NO.

50-409 CO3tPLETEb

  • N TELEPilONE _608-6W-2331 OPERATING STATUS N'"
1. Unit Name: LA CROSSE B0llING WATER REACTOR
2. Reporting Period: 0001. 07-01-81 TO 2400, 07-31-81
3. Licensed Ther:nst Power (5!WI):

165

4. Namerlate Rating (Grow 5tWe):

65.3

5. Ded;n Electries! Rating (Net 31We):

50

6. 5fnimum Dependab!e C p city (Gross AlWe):

50 48

7. 3!nimum DependJbIc C373eity (Net 5!We):
5. If Chan;cs Oceur in Capacity R: tings (Irems Number 3 Through 71Since Last Report.Gise Reamn.

1

9. Power Lese! To Which Restricted,1f Any (Net MWe):

10, Remsens For Restrictions.lf Any:

This Month Yr.-t o-Da t e Cumulatise

11. !!oun In Reporting Period 744 5,087 102J86
12. Number Of Hours Reactor Was Critical

_740_5 3 775.6 6LR22.6

13. Reactor Resene ShutdowTillours 0

0 478 I4. Ilours Gener: tor On-Line 732.6 3.446.9 62.478.2

15. Unit Rewne Shutdown floun 0

0 79

16. Gross Thermal Encryy Generated (5tWil) 4R;740_?

467.592.7

&,5 L 930.1

17. Groo Electrical Energy Generated (h!Wil) 27.905 133 69R

?,564,333 lb. Net Electrical Energy Ger.mted (MWil) 26.016 123.760 Pa371.040

19. Urdt Senice Factor 98.5 67.8 60.7
20. Unit Asailabi?ity Factor 98.5 67.8 60.7
4. 0 8
21. Unit Capa:ity Factor (Using MDC Net) 77 0 50.7 69.9 48.7 46.1
22. L' nit Capacity Factor (Udng DER Net) 1.6 8.6 7.2
23. Urdt Forced Outs;e Rate
24. Shutdowns S:heduled Oser Nest 6 Months (T3pe.Date.and Duration of Eacht:

None NA

25. If Shut Down At End Of Report Period. Estimated Date of Startup:
26. Units in Test Status (Psint to Commercial Operation):

Forecast Achiesed INITI A L CRITICALITY INITIAL FLEClRICITY CO\\lMERCI AL OPER ATION 8204130401 820810

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PDR ADOCK 05000409 R

PDR

UNIT SilU1 DOWNS AND POWER RLDUCTIOss DOCKET NO. 50-409 UNIT NAME _I.ACl3WR DATE 09-06-R1 COMPl.ETED fly L S. GOODMAN REPORT STON111

.Tili.V 1481 TEl.ErilONE 60R-694-m 1 1

f%

Cauw & Correi;iise

{g 3

Ek Litenset Ew Date k

3?

d,i 2 522 Ihent 3,'f Q

Atenin to f

j5g Repors r vi O jL Paevent Recurrence d

81-11 07-06-81 F

11.4 A

3 NA IA INSTRU SPURIOUS SPIKE ON NUCLEAR-INSTRUMENTATION (NI) CAUSED CORRESPONDING MOMENTARILY IIIGli READING ON POWER / FLOW CIIANNEL WIIICII RESULTED IN AUTOMATIC SIlUTDOWN.

NI CllANNEL 8 IIIGII SPEED MULTIPLIER WAS REPLACED.

4 1

2 3

4 I l'oned Reamn:

Steiln=3 l' sinh:1 G. lnstructions s 5.heduled A l:quipment l'ailure (l'splaml I 41Junal for Pseparation of D na 114taintenance of Test

.'414nual Sia m.

1.ni 3 shecis sur 1.itensee C Refueling

3. Antion.use N o.un.

13ent Report 11.110 l' ele int!RI.G.

D Regulator) Restriction 4.Oiher ll spianti oleti I Operator Traming & l.iseme I ununation F Adnunntraine 4

G.OperJ tionJI l's t ol ( l's plattil

[ slph:1 l Sarne heinr6e i* 77) 11 Other il splain) j

AVER AGE DAILY UNIT POhER LEVEL DOCKET NO. _50-409 LACBWR exir DATE 08-06-81 L.S. GOODMAN CO3fPLETED BY TELEPl!ONE 608-689-2331 MONTH JULY 1981 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL t MWe. Net) ignye.ge,y 1

29 17 38

=<

2 31 is 38 3

34 i,

37 4

37 20 37 5

~

37 21 37 6

18 22 37 7

21 23 37 s

34 24 37 9

37 25 37 10 27 26 37 II 74 27 37 I2 38 37 28 13 17 29 32 14 17 30 33 15 38 31 31 16 1R INS 1 RUCTIONS On this format hst the aserage daily unit power levelin Mwe. Net for each day in the reporting month. Compute to the nearest whole megawatt.

(9f77)

, ~.

JULY 1981 MEClfANICAL MAINTENANCE LER OR f1ATURE Of OUTAGE SAlfuMCTI0il EQUIPMEtiT Malt 1TErlAfiCE tiUf4BER CAUSE RESULT CORRECTIVE ACTI0f4 i

IB WASTE WATER PUMP CORRECTIVE NA MECHANICAL LEAKED EXCESSIVE REPLACED MECHANICAL MR-0530 SEAL LEAK AMOUNT OF WATER SEAL IB CONTAINMENT AIR CORRECTIVE NA LOW ON REFRIG-WOULD NOT COOL EXPANSION VALVE CONDITIONER UNIT MR-0708 ERANT DOWN PROPERLY GASKET REPLACEMENT REACTOR BATTERY RACK FACILITY CHANGE NA NA NA INSTALLATION OF NEW RESTRAINTS 74-81-7, MR-0636 RESTRAINTS FOR EARTH-QUAKE 1B SHIELD COOLING CORRECTIVE NA MECHANICAL LEAKED EXCESSIVE REPLACED MECHANICAL PUMP MR-0710 SEAL LEAK AMOUNT OF WATER SEAL ilADIOLOGICAL SAMPLE NEW INSTALLATION LER-NA NA INSTALLED NEW WELL WELL FACILITY CHANGE 80-12 FOR CHECKING GROUND 54-81-3, MR-0522 WATER CONTAMINATION HEATING BOILER PREVENTIVE

~ NA NA NA ANNUAL INSPECTION MR-0750 CRD HYDRAULIC CHARG-CORRECTIVE NA O-RING FAILURE LEAKED EXCESSIVE REPLACED TWO O-RINGS ING PUMP DISCHARGE MR-0746 AMOUNT OF OIL IN EACH VALVE VALVES 1A & 1B 1B REACTOR FEED PUMP PREVENTIVE NA NA NA PERFORMED PREVENTIVE MR-0754 MAINTENANCE TO KEEP SCOOP TUBES WORKING FREELY.

AIR MONITORS IN NEW INSTALLATION NA NA NA-ANCHORED IN CASE OF CONTAINMENT MR-0778 EARTHQUAKE

.s

JULY 1981 1

f3 TriSTRUMEf4T Af!D ELECTRfCAL l'AlfiTEtiAfiCE LER OR outage Item f4ATURE OF OUTAGE MALFUflCTIOft i

EQUIPMENT MAlf4TENAf1CE fiUMBER CAUSE RESULT CORRECTIVE ACT10ft 3ECURITY SYSTEM CORRECTIVE NA UNKNOWN FALSE ALARM BALANCED ALARM UNIT

.\\LARM 25-6 MR-0761 3ECURITY SYSTEM CORRECTIVE NA UNKNOWN FALSE ALARM BALANCED ALARM UNIT.

4ICROWAVE 20-4 MR-0758 SECURITY SYSTEM CORRECTIVE NA WATER IN ALARM INOPER-REPLACED ALARM SWITCII '

ALARM 25-6 MR-0757 SWITCli ATIVE SECURITY SYSTEM CORRECTIVE NA

-LOW SENSITIV-POOR PICTURE ADJUST LENSE SENSITIV-CCTV CAMERA 1 MR-0730

'ITY

'ITY SECURITY SYSTEM FACILITY CilANGE NA IIEATER INSTALLED INSTALLED ENGINE DIESEL. GENERATOR 78-17, MR-0704 REQUIRED ENGINE IIEATER llEATER SECURITY SYSTEM CORRECTIVE NA LOW POOR PICTURE REPLACED AUTO LENSE

/CTV CAMERA 1 MR-0743 SENSITIVITY SECURITY SYSTEM CORRECTIVE NA UNKNOWN ALARM INOPER-SWITCIIED ALARM ALARM 25-7 MR-0745 ABLE CIIANNELS i

SECURITY SYSTEM READ-CORRECTIVE NA ABUSE BROKEN WIRE REPLACED WIRE ON p

JUT TERMINAL OT3 MR-0747 CONNECTOR FOR OT3 SECURITY SYSTEM CORRECTIVE NA UNKNOWN INOPERATIVE REPLACED SYNC POWER INVERTER MR-0774 BOARD IN. INVERTER I

NET TEST METER CORRECTIVE NA ACCIDENT BROKEN "U" TUBE REPLACED "U" TUBE AUXILIARY EQUIPMENT MR-0760 AND TilERMOMETER AND ' TIIERMOMETER t

TELEPilONE PAGE CORRECTIVE NA ADDITION INSTALLED PAGE INSTALLED PAGE 1

I SPEAKER MR-0141 SPEAKER SPEAKER i

STAND PIPE IIEATER CORRECTIVE NA NORMAL ALARM INSTALLED PilOTO ALARM UNIT MR 0771 USAGE INOPERABLE LAMP

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JULY 1981 ff1STRUMEf4T AftD ELECTRICAL MAffiTEfiAfiCE 2 of 3 Outage Item LER OR flATURE OF OUTAGE MALFutiCTI0fl EQUIPMEffT MAlf1TEf1AfiCE fiU'iBER CAUSE RESULT CORRECTIVE ACTIO!1 LECTRICAL EQUIPMENT CORRECTIVE NA WATER IN UNIT BURNOUT OF RETURN $D FOR REPAIR OOM FIRE ALARM PANEL MR-0749 COMPONENTS OMTROL ROD DRIVE CORRECTIVE NA VIBRATION LOWER SETTING READJUSTED MERCURY CRD) HYDRAULIC MR-0744 SWITCH ESERVOIR ALARM B REACTOR FEED PUMP CORRECTIVE NA LOST COOLING OVERIIEAT OF REPLACED MOTOR AND ONTROL MOTOR MR-0754 AIR MOTOR COOLING TUBE RD SECONDARY POSITION CORRECTIVE NA NORMAL USAGE NO LIGilT REPLACED LAMP 4

MR-0756 PR SYSTEM PNEUMATIC PREVENTIVE OUTAGE OIL IN AIR CLEANED SYSTEM CLEANED SYSTEM ONTROL MR-0739 81-11 SYSTEM 1D SECONDARY CORRECTIVE OUTAGE NORMAL USAGE NO LIGHT REPLACED LAMP JSITION #20 MR-0734 81-11 a INLET DAMPER FOR CORRECTIVE OUTAGE NORMAL USAGE BROKEN CONNEC-REPLACED LINK FACK BLOWER MR-0738 81-11 TIVE LINK RD SECONDARY CORRECTIVE NA NORMAL USAGE NO LIGilT REPLACED LAMP OSITION #14 MR-0742 ILTER FEED MOTOR FOR CORRECTIVE NA NORMAL USAGE NO DRIVE REPLACED DRIVE MOTOR TACK MONITOR MR-0723

.UTOMATIC GAIN CORRECTIVE NA UNKNOWN LOW READING ADJUSTED GAIN CONTROL llANNEL N-8 MR-0724 UCLEAR CilANNEL N-5 PREVENTIVE NA TEST DUE COMPLETED TESTS COMPLETED TESTS

'llROUGil N-9 N-5 TIIROUGli N-9 AFETY SYSTEM CllANNEL PREVENTIVE NA TEST DUE COMPLETED TESTS COMPLETED SAFETY 2 NAD 11 0 #3 2

SYSTEM TESTS 1, 2,

AND II 0 #3 2

-s J

m JULY 1981' INSTRUMEfiT AND ELECTRICAL MAINTEllANCE 3 of 3 Onage Item LER OP' NATURE OF OUTAGE MALFUNCT10fl EQUIPMENT MAINTENANCE NUMBER CAUSE RESULT CORRECTIVE ACTION CESTED CHANNEL N-7 CORRECTIVE NA UNKNOWN SPIKES ON REPLACED POWER SUPPLY

\\ND N-8 AGS MR-0733 CHANNELS CHANNEL 7 AND MULTI-MR-0737

~ PLIER'FOR CHANNEL 8 iECURITY SYSTEM CARD PREVENTIVE NA TESTS DUE COMPLETED TESTS COMPLETED TESTING 1EADERS AND ALARM INIT TESTS NVIRONMENTAL FACILITY NA NRC REQUEST COMPLETED COMPLETED FACILITY 10NITORING CHANGE 48-81-1 INSTALLATION-CHANGE.

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5 NARRATIVE

SUMMARY

OF OPERATING EXPERIENCE JULY 1981 At the onset of the July 1981 reporting period, slow power escalation was continuing after the outage which concluded June 27.

The reactor achieved 85% Reactor Rated Thermal Power (37 MWe-Net) on July 4, 1981.

This power level has been scheduled to extend the time period between refueling outages.

At 1137 on July 6, a spurious spike on Nuclear Instrumentation Channel No. 8 caused a corresponding momentarily high reading on Power / Flow Channel No.

2, which resulted in an automatic shut-down.

The reactor was returned to critical at 1508 and the turbine-generator was synchronized to the DPC grid at 2302 on i

July 6.

Power escalation continued until July 9, when 85% Rated Thermal Power (37 MWe-Net) was achieved.

At 2315 on July 29, a power reduction to-75% Reactor Rated Thermal Power (32 MWe-Net) was commenced, due to pressure swings in the. turbine governor control system.

At 0805 on July 31, a power reduction commenced in preparation for replacement of the turbine Initial Pressure Regulator controller.

The power reduction was halted at 72% Reactor Rated Thermal Power due to system demand.

Power generation continued at this level for the remainder of the day, which marked the end of the July reporting period.

Significant maintenance items performed during July 1981 are indicated on the attached Mechanical Maintenance and Instrument and Electrical Maintenance listings.t a

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