ML20050B745

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Monthly Operating Rept for Feb 1980
ML20050B745
Person / Time
Site: Cook 
Issue date: 03/05/1980
From: Gillett W
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
Shared Package
ML20050B743 List:
References
NUDOCS 8204070314
Download: ML20050B745 (6)


Text

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OPERATING DATA REPORT 50-315 DOC:GT NO.

3-5-80 DATE COMPLETED gy W. T. Gillett.

TELE?-iONE 616-a6%5901 O?IRATING STATUS Donald C. Cook 1

Notes 3, en3 3,m..

2. Repor:ing Period:

February 1980_

3250

]

3. LicensedTher==! Power (MWr):

1089 i

4. Nameplate Rating (Gross MW ):

1054 y

S. Design Ele:: im! R:da;(Net MWe):

1080

6. Maximum Depend:ble Cap:dty (Gross MWe):

l 1044

7. Maxirnum Dependable C:p: city (Net Mwe):

S. If Changes Oc=:rin Capz:I:y Ratings (Items Number 3 Through 7) Since Last Report. Give Reasons:

9. Power Level To Whi:h R=s:ri::ed.If Any (Net Mwe):
10. Reasons For Restd:tio.s.If Any:

This Month Yr. to.Dat-Cu=u!:nve 696 1440 45,264

11. Hou:s in Reporting Pedad 696 1042.8 34,004.b
12. Number of Hours Re2::or was Criti s!

0 0

463

13. Re:c:or Reserve Shu:down Hou:s 696 1036.6 33,119.8
14. Houn Genestar On.Line 0

0 321

15. Unit Reserve Shutdown Ho=r 2,209.403 3.190,053 97.256.358
16. Gross Therms! Enegy Gener:ted (MWH)
17. Cross Elec.:i=! Enegy Gene = red (MWH) 734,460 __,

1,057,970 30,215,310 708,795 1,020,062 29,017,376

18. Net Ele:: deal Energy Genen:ed g, wn) 100

/Z.0 -

75.0

19. Unit Servi:: F:c:or 100 72.0 75.0
20. Unic Av:il:bi!!:y F:c:or 97.5 67.8 67.0
21. Unit C:pacity F:::or(Using MDC Net) 96.6 67.2 62.2
22. Unit Capscity F=::or (Using DER Net) 0 28.0
8. _6
23. Unic Forced Ou::Se R:te
24. Shutdowns Scheduled Over Nex: 6 Months (Type. Date.:nd Du : tion of Each):
25. If Shut Down At End Of Report Period.Estimered Date of Startup:
25. Units in Test St:tus (Prior to Ce= mere!al Oper: tion):

Force:st Achieved INITIAL CRITICALITY

~~

INITIAL ELECTR:C:TY COMMERC:AL OPER ATiCN tof 7 3 8204070314 800306 PDR ADOCK 05000315 PDR R

AVERAGE DAILY UNIT POWER LEVEL DOCKET ~NO.

50-315-UNIT 1

DATE 3-4-80 COMPLETED BY W. T. Gillett TELEPHONE 616-465-5901 MONTH February 1980 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWE-Net)

(MWe-Net) 1 1041 17 655 2

1032 18 960 3

1044 19 1038 4

1044 20 1045 S

1043 21 1046 6

1037 22 1046

-7 1039 23 1035 8

1045 24 1034 9

1035 25 1046 10 1045 26 1045 11 1046 27 1047 12 1044 28 1043 13 1044 29 1043 14 1041 W

15 1046 W

16 827 l.

[

INSTRUCTIONS On this format list the average daily unit power level in MWe-Net for each

- day in the reporting month. Compute to the nearest whole megawatt.

- i UNITSilUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50-315 UNIT NAhlE 0.C. Cook-Unit 1 DATE 3-6-80 REPORT Af0N TH February, 1980 00hlPLETED BY B.A. Svensson TELEPil0NE (616) 465-5901 "E

.3== ='A Licensee g r,,

e.,

Cause & Co icciive 5

c ri 3 _e E

n 5

7,cgy Event ay 83 Ac. tion to No.

Date g

gg g

H

$5 5

j;5g Report #

(NC fU Prevent Recurrence a

158 800216 F

0 B

b N.A.

CH ZZZZZZ Reactor power reduced to 62% to permit removal of the west main feed pump curbine from service to investigate cause for oscillation in pump and turbine 5 ration.

Re-actor power returneu o 100% 800218.

I 2

3 4

F: Forced Reason:

hiethod:

Exhibit G -Instructions S: Schetinted A-Equipment Failme (Explain) 1.hlanual for Preparation of Data ll hlaintenance of Test 2 klanual Scram.

Ent y Sheets for 1.icensee C Refueling

3. Autmnatic Scram.

livent Repmi (1.ER) File INilREG-D-Regulatory Restriction 4 Other (Explain) 0161)

E-Opesator reaining & License lixamination F Administrative 5

G Operational Eeror (Explain)

Exinbit 1 - Same Somce 19/77) ll-Other (Explain)

Docket No.:

50-315 Unit Name:

D. C. Cook Unit #1 Completed By:

R. S. Lease Telephone:

(616)465-5901 Date:

March 11, 1980 Page:

1 of 2 l MONTHLY OPERATING EXPERIENCES -- FEBRUARY,1980 l l Highlights l:

The Unit operated at 100% power the entire reporting period except as detailed in the summary.

Total electrical generation for the month was 734,460 Mwh.

l Summary 1:

2/1/80 -- Power was reduced to 90% for testing of turbine control valves. Total time below 100% was 5.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />.

2/6/80 -- Loop 2 Tavg and 6T signals were defeated and the bistables tripped for a 5.75 hour8.680556e-4 days <br />0.0208 hours <br />1.240079e-4 weeks <br />2.85375e-5 months <br /> period for replacement of a calibration potentiometer.

2/9/80 -- Power was reduced to 90% for testing the turbine control valves. Total time below 100% was 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />.

2/11/80 -- East Component Cooling Water puro was inoperable for a 2 hour2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> period for bearing inspec ion.

2/15/80 -- Safeguards Fan HV-AES-1 was inoperable for a 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> period for replacement of HEPA filters.

2/16/80 -- Power was reduced to 90% for testing of turbine control valves.

Total time below 100% power was 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />.

Power was reduced to 65% of a 2 hour2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> ramp starting at 1040 hours0.012 days <br />0.289 hours <br />0.00172 weeks <br />3.9572e-4 months <br /> to remove the West Main Feed Pump from service.

This pump had been showing minor vibration problems. The vibration pattern showed an oscillation between 1 and 2 rails over an 8-minute time span. A balance weight was placed on the pump and it was returned to service at 0145 2-18-80.

The Unit was~ returned to 100% power by 1045 the same day.

The balance weight did not help the oscillating. This vibration pattern went away 2-29-80.

At this time there is no explanation as to what caused it.

2/17/80 -- The filter paper drive on stack particulite Radiation Monitor R-25 failed at 1630 hours0.0189 days <br />0.453 hours <br />0.0027 weeks <br />6.20215e-4 months <br />.

Repairs were made and this was again retu ned to service at 1350 hours0.0156 days <br />0.375 hours <br />0.00223 weeks <br />5.13675e-4 months <br /> 2-24-80.

i 1

~

Docket No.:

50-315 Unit Name:

D. C, Cook Unit #1 Completed By:

R. S. Lease Tela.nhone:

(616) 465-5901 Date:

March 11, 1980 Page:

2 of 2 2/19/80 -- Power was reduced to 96% over a 3.25 hour2.893519e-4 days <br />0.00694 hours <br />4.133598e-5 weeks <br />9.5125e-6 months <br /> period due to the West Main Feed Pump indicating excessive vi-bration.

It was determined that the vibration instrument wan in error.

Power was returned to 100%.

Containment area Radiation Monitor R-2 was inoperable for a 30 hour3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br /> period starting at 1725 hours0.02 days <br />0.479 hours <br />0.00285 weeks <br />6.563625e-4 months <br /> for necessary repairs.

l Safeguards Fan HV-AES-1 was removed from service at 0815 hours0.00943 days <br />0.226 hours <br />0.00135 weeks <br />3.101075e-4 months <br />. Tt.is was for replacement of the charcoal filter.

This unit was returned to operable status at 1710 hours0.0198 days <br />0.475 hours <br />0.00283 weeks <br />6.50655e-4 months <br /> 2-23-80.

2/22/80 -- Control Room air conditioning unit 1-HV-ACRA-2 was inoperable for 3 days, starting at 0327 hours0.00378 days <br />0.0908 hours <br />5.406746e-4 weeks <br />1.244235e-4 months <br />.

This was for repairs of a safety valve on the expansion tank.

2/23/80 -- Power was reduced to 90% for testing the turbine valves.

Total time below 100% was 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />.

2/24/80 -- Power was reduced to 97% at 0810 hours0.00938 days <br />0.225 hours <br />0.00134 weeks <br />3.08205e-4 months <br /> for a moderator temperature coefficient test.

Power was returned to 100% by 1740 hours0.0201 days <br />0.483 hours <br />0.00288 weeks <br />6.6207e-4 months <br /> the same day.

2/26/80 -- The AB Emergency Diesel Generator was inoperable for a 6 hour6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> period for cleaning of switch gear.

This unit experienced its normal condenser tube leak problems, and condenser halfs were out of service periodically throughout the reporting period.

i'

DOCKET NO.

50 - 315 UNIT NAME D. C. Cook - Unit No. 1 DATE 3-6-80 COMPLETED BY B. A. Svensson TELEPHONE (616) 465-5901 PAGE 1 of 1 MAJOR SAFETY-RELATED MAINTENANCE FEBRUARY,1980 M-1 No. 4 steam generator blowdown regulating valve, DRV-341, had a body to bonnet leak.

Replaced all valve gaskets and had valve retested.

M-2 The HEPA filter for ESF ventilation system fan HV-AES-1, has a high DP.

Replaced HEPA filter and had unit tested.

C&I-l ZRV-014, the fire protection water supply to ventilation Unit 1-AES-1,.

would not open manually when the actuation button was depressed.

  • Time delay relay 62-ESS-1 was found energized, preventing the sole-noid valve from energizing and opening ZRV-D14.

A 50 microfarad capacitor utilized as a filter in the power supply circuit failed.

The capacitor was replaced with a spare and an operational test of the control circuit was performed.

C&I-2 ZRV-023, the fire protection water supply to the control room pressurizer / cleanup filter system (1-HV-ACRF), would nct open manu-ally when the actuation button was depressed.

Time delay relay 62 CRPF was energized which prevented the solenoid valve from ener-gizing.

The circuit board was replaced and an operability test was performed to verify correct operation.

C&I-3 C-4, overpower delta T block rod withdrawal and turbine runoack, was received at 99% reactor power operation.

...a resistance to voltage converter output voltages was measurt J for comparisons on all four protection sets.

Loop No. 4 indicated the highest AT% power value, and was producing the annunciator actuation.

The hot leg RTD terminations in the rack were found loose.

The ter-minations were tightened and the AT% power signal decreased 7% of power Loop 4 was returned to normal operation.

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