ML20050A883

From kanterella
Jump to navigation Jump to search
Final Part 21 Rept 81-01 Re Motor Terminal Block Voltage Rating in Limitorque Valve Control,Initially Reported 810121.Valve Will Be Inspected for Correct Size Control Terminal Block & Cable Terminations & Will Be Reworked
ML20050A883
Person / Time
Site: LaSalle  Constellation icon.png
Issue date: 03/25/1982
From: Schroeder C
COMMONWEALTH EDISON CO.
To: James Keppler
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
References
REF-PT21-82-603-000 10CFR-50.55E, 3722N, PT21-82-603, PT21-82-603-000, NUDOCS 8204020360
Download: ML20050A883 (2)


Text

.

g Comm:nw:cith Edison O / one First National Plaza. Chicago, lihnois i

C/

Address Reply to: Post Office Box 767 Chicago, Illinois 60690 March 25, 1982 Mr. James G. Keppler, Regional Administrator Directorate of Inspection and Enforcement - Region III U.S. Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, IL 60137

Subject:

LaSalle County Station Units 1 and 2 Motor Terminal Block Voltage Rating in Limitorque Valve Controls ps, j ' h' 10 CFR 50.55(e) #81-01 Final Report NRC Docket Nos. 50-373 and 50-374 p

MEC:

9 References (a):

L.

DelGeorge to J.

G. Keppler 2D s

dated February 20, 1981.

Same k-APRJ Subject, 30 Day Report.

3 Ugrgt.

2 'I (b):

L. DelGeorge to J.

G.

Keppler

  1. N '

//

dated July 15, 1981.

Same qp c(\\

Subject, Interim Report.

I.T ' M (c):

C.

Sargent letter to J.

G. Keppler dated Septembe r 15, 1981.

Same Subject, Interim Report.

(d):

C.

Sargent letter to J.

G.

Keppler dated October 29, 1981.

Same Subject, Interim Report.

(e):

C.

Sargent letter to J.

G. Keppler dated-Decembe r 15, 1981.

Same Subject, In terim Report.

Dear Mr. Keppler:

The purpose o f this letter is to submit the Final Report

  1. 81-01 regarding the subject Motor Terminal Block Modification.

This incident was initially reported to your o f fice on January 21, 1981, a 30-day report was made (Reference (a)), and several interim reports have been submitted (References (b),(c),(d), and (e)).

d}h s204o20260 e20223 PDR ADDCK 05000373 S

% 20 PDR

=

i J. G. Keppler March 25, 1982 J

The Unit 1 status is as follows:

1.

All Unit 1 limitorques have been inspected.

2.

All Unit 1 limitorques that are fed by Safety-Related cables have had the motor terminal blocks removed and a lug to-lug connection installed.

+

2 3.

Unit 1 limitorques that are fed by Non-Safety-Related cables will have the motor terminal blocks removed and j

a lug to lug connection installed prior to Unit 1 criticality.

(Note:

Limitorque operators type SMC-04 s

and type PB do not contain a motor terminal block l

because the motor leads are terminated on the control terminal block.

These limitorques were inspected and i

found to have the correct size control terminal block and the correct cable terminations.

In addition, these types of limitorque operators are only fed by non-safety-related cables at LaSalle County Station).

The Unit 2 status is as follows:

Unit 2 limitorques will be inspected and reworked prior to Unit 2 fuel load.

Limitorque operators type SMC-04 and type PB will be inspected for correct size control terminal I

block and for the correct cable terminations, q

If there are any further questions in this matter, please contact this o f fice.

I Very truly yours, i

@W 3hs/82.

C.

W. Schroeder Nuclear Licensing Administrator 1m i

i j

cc:

NRC Resident Inspector - LSCS Director of Inspection and j

Enforcement - Washington, D.C.

20555 i

1 1

'3722N i

l 4

i

,_-., _ _..