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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217N8911999-10-15015 October 1999 Forwards Rept of Changes,Tests & Experiments at Pilgrim Nuclear Power Station for Period of 970422-990621,IAW 10CFR50.59(b).List of Changes Effecting Fsar,Encl ML20217D3951999-10-13013 October 1999 Forwards Request for Addl Info Re Util 990806 Submittal on USI A-46, Implementation Methodology Used at Pilgrim Nuclear Power Station, Per GL 87-02 ML20217E1581999-10-0808 October 1999 Forwards Insp Rept 50-293/99-05 on 990726-0905.Three Violations Noted & Being Treated as Ncvs.Violations Include Failure to Assure That Design Bases Correctly Translated Into Specifications ML20217C3151999-10-0606 October 1999 Forwards Scenario Package for Pilgrim Nuclear Power Station Nrc/Fema Evaluated Exercise Scheduled for 991207.Without Encl ML20217D5591999-10-0505 October 1999 Documents Pilgrim Nuclear Power Station Five Yr Survey of Main Breakwater.Survey Has Determined That Pilgrim Main Breakwater Is Intact & Remains Adequately Constructed to Perform Designed Safety Function ML20217C8051999-10-0505 October 1999 Forwards Proprietary Results of Audiologic Evaluations for Jp Giar,License SOP-10061-3.Attachment Clearly Shows Requirements for Operator Hearing Ability Are Met. Proprietary Info Withheld,Per 10CFR2.790(a)(6) ML20212J8301999-09-30030 September 1999 Informs of Completion of mid-cycle PPR of Pilgrim Nuclear Power Station.Staff Conducts Reviews for All Operating NPPs to Integrate Performance Info & to Plan Insp Activities at Facility Over Next Six Months ML20216J9961999-09-29029 September 1999 Forwards Resume of Person Identified as Acting RPM in Licensee to NRC Re Notification That Person Named in License Condition 11 of 20-07626-02,is No Longer Employed at Pilgrim Station.Resume Withheld,Per 10CFR2.790 ML20212F7871999-09-24024 September 1999 Advises That Util 990121 Application for Amend Being Treated as Withdrawn.Proposed Changes Would Have Modified Facility UFSAR Pertaining to Values for post-accident Containment Pressure Credited in Pilgrim Net Positive Head Analyses ML20212H1381999-09-23023 September 1999 Submits Info in Support of Request Filed on 990730 to Grant one-time Exemption from 10CFR50,App E,Authorizing Biennial Full Participation Emergency Preparedness Exercise to Be Conducted in 2002 Instead of 2001 ML20212H1441999-09-23023 September 1999 Withdraws 990121 Request for License Change Re Emergency Core Cooling Sys Net Positive Suction Head,Due to Incorrect Datum Preparation ML20216F3451999-09-16016 September 1999 Forwards Summary Rept Providing Results of ISI Conducted at PNPS on-line & Refueling Outage (RFO 12) ML20212C2861999-09-16016 September 1999 Forwards SER Accepting Licensee 981123 Request for Relief RR-E1,RR-E5,RR-E6 Pursuant to 10CFR50.55a(a)(3)(i) & Request for Relief RR-E2,RR-E3 & RR-E4 Pursuant to 10CFR50.55a(a)(3)(ii) ML20216E7111999-09-0909 September 1999 Forwards License Renewal Application Including Form NRC-398 & Form NRC-396 for Jp Giar,License SOP-10061-3.Without Encls ML20216E5891999-09-0707 September 1999 Forwards Copy of Pilgrim Station Organization Structure. Encl Refelcts Changes in Upper Mgt Level Structure.Changes Were Effective 990901 ML20211M4501999-09-0303 September 1999 Informs That Pilgrim Nuclear Power Station Plans to Conduct Full Participation Emergency Preparedness Exercise with Commonwealth of Ma on 991207,IAW 10CFR50,App E,Section IV.F.2 ML20211M9161999-08-31031 August 1999 Submits Review & Correction of Info in Reactor Vessel Integrity Database (Rvid),Version 2,re Pilgrim Station ML20211J8391999-08-30030 August 1999 Forwards Rev 1 to Provisional Decommissioning Trust Agreement for Plant,Changing Portions of Agreement to Permit Up to Two Distributions & Clarify Formula for Distribution ML20211H5701999-08-27027 August 1999 Forwards Insp Rept 50-293/99-04 on 990610-0725.Two Violations Identified Being Treated as non-cited Violations ML20211C3381999-08-19019 August 1999 Provides semi-annual LTP Update,Including Schedule, Commitment Descriptions,Progress Since Last Update & Summary of Changes.Rev Bars Indicate Changes in Status Since Last Submittal ML20210U5761999-08-18018 August 1999 Responds to Opposing Merger of Bec Energy & Commonwealth Energy Sys in Commonwealth of Massachusetts. Informs That for Sale,Nrc Responsible for Only Ensuring That Entergy Technically & Financially Qualified to Operate NPP ML20210U6691999-08-18018 August 1999 Forwards from Massachusetts State Senator T Murray Opposing Merger Between Bec Energy & Commonwealth Energy Systems ML20210U7521999-08-18018 August 1999 Forwards from Massachusetts State Senator T Murray Opossing Merger Between Bec Energy & Commonwealth Energy Systems ML20210U5151999-08-17017 August 1999 Forwards Notice of Withdrawal of Application for Approval of Indirect Transfer of FOL for Pilgrim in Response to .Approval No Longer Needed Since Beco Sold Interest in Pilgrim to EOI on 990713 ML20211B3841999-08-16016 August 1999 Forwards Response to NRC Second RAI Re Pressure Locking & Thermal Binding of SR power-operated Gate Valves ML20210U4831999-08-13013 August 1999 Forwards fitness-for-duty Program Performance Data Sheets for Period of 990101-0630,per 10CFR26.71(d) ML20210S0891999-08-0909 August 1999 Forwards Amend 11 to Indemnity Agreement B-48 Signed by Boston Edison Co & Entergy Nuclear Generation Co ML20210R6251999-08-0606 August 1999 Provides Supplementary Info on USI A-46 Implementation Methodology at Pilgrim Station,To Enable NRC to Perform Evaluation & Issuance of Plant Specific SER for Plant ML20210M9411999-08-0202 August 1999 Requests That NRC Treat Pending Actions Requested by Beco Prior to 990713,as Requests Made by Entergy.Ltr Requests That Minor Administrative Changes to License Amend 182 & Associated Ser, ,reflect 990713 Transfer ML20210H8761999-07-30030 July 1999 Requests That NRC Grant Exemption from Requirements of 10CFR50,App E,Section IV F,Which Would Authorize Rescheduling of 2001 Biennial Full Participation Emergency Preparedness Exercise for Pilgrim Station to 2002 ML20210H8661999-07-29029 July 1999 Provides Revised Response to GL 96-06 & Addresses NRC Insp Concern for Containment Penetration X-12.Info Submitted to Facilitate NRC Review & Closeout of Subject GL for Plant ML20216E2321999-07-26026 July 1999 Discusses GL 92-01,rev 1,suppl 1, Rv Structural Integrity. NRC Revised Info in Rvid & Releasing as Rvid Version 2 ML20216D4131999-07-22022 July 1999 Informs That J Conlon,License OP-11040-1,terminated Employment with Beco on 990703,per 10CFR50.74.Individual Will Not Participate in Util Licensed Operator Requalification Training Program ML20210E2231999-07-20020 July 1999 Discusses Arrangements Made by Dennis & M Santiago During 990615 Telephone Conversation for NRC to Inspect Licensed Operator Requalification Program at Pilgrim During Wk of 991004 ML20210C4151999-07-19019 July 1999 Informs That Util Intends to Submit Approx Eight Licensing Actions in FY00 & Eight in FY01,in Response to Administrative Ltr 99-02.Actions Are Not Expected to Generate Complex Reviews ML20210F3711999-07-14014 July 1999 Informs NRC That Effective 990713,listed Pilgrim Station Security Plans Have Been Transferred from Boston Edison to Entergy & Are Still in Effect ML20210A9441999-07-14014 July 1999 Responds to Re Changes to Pilgrim Nuclear Power Station Physical Security Plan Identified as Issue 2,rev 14, Addendum 1,respectively.No NRC Approval Is Required IAW 10CFR54(p) ML20209G2251999-07-0909 July 1999 Forwards Insp Rept 50-293/99-03 on 990419-0609.Five Severity Level IV Violations of NRC Requirements Identified & Being Treated as non-cited Violations,Consistent with App C. Several Individual Tagging Errors Occurred ML20209C4661999-07-0707 July 1999 Forwards SE Accepting Addendum on Proposed Change in Corporate Ownership Structure Involving Entergy Nuclear Generation Co ML20209C7761999-07-0606 July 1999 Submits Annual Summary Rept of Changes Made to QAP Description as Described in QA Manual,Vol Ii.Rept Covers Period of Jul 1998 Through June 1999.No Changes Made During Period ML20209C3851999-07-0606 July 1999 Forwards Redacted Draft of Decommissioning Trust Agreement Re Transfer of PNPS & NRC Operating License & Matls License from Boston Edison Co to Entergy Nuclear Generating Co ML20196J7251999-07-0101 July 1999 Informs of Completion of Licensing Action for GL 96-01, Testing of Safety-Related Logic Circuits, for Pilgrim Nuclear Power Station ML20209B9411999-06-30030 June 1999 Discusses Deferral of IGSCC Welds to RFO 13.Deferral of Welds to Refueling Outage 13 Does Not Impact Acceptable Level of Quality & Safety Per 10CFR50.55(a)(3)(i) Since Plant in Compliance W/Exam Percentage Requirements ML20209B9431999-06-30030 June 1999 Provides Formal Notification That Closing Date for Sale & Transfer of Pilgrim Station Scheduled to Occur on 990713. a Wang Will Be Verbally Notified of Time of Sale Closing ML20209B9791999-06-29029 June 1999 Forwards Rev 13A to Pilgrims COLR for Cycle 13,IAW TS 5.6.5 Requirements.Rev 13A Provides cycle-specific Limits for Operating Pilgrim During Remainder of Cycle 13 ML20196H2381999-06-29029 June 1999 Forwards SER Denying Licensee 980820 Request for Alternative Under PRR-13,rev 2 for Use of Code Case N-522 During Pressure Testing of Containment Penetration Piping ML20209A8761999-06-28028 June 1999 Forwards SER Authorizing Licensee 990317 Relief Request to Use ASME Code Case N-573 as Alternative to ASME Code Section XI Article IWA-4000 for Remainder of 10-year Interval Pursuant to 10CFR50.55a(a)(3)(i) ML20209A8701999-06-25025 June 1999 Responds to NRC Request for Info Re Y2K Readiness of Computer Sys at Nuclear Power Plants. Y2K Readiness Disclosure for Plant,Reporting Status of Facility Y2K Readiness Encl ML20210U5901999-06-25025 June 1999 Opposes Merger of Bec Energy & Commonwealth Energy Sys in Commonwealth of Massachusetts.Expresses Skepticism Re Claim by Companies That Consumers Will Benefit from Proposed Consolidation & four-year Freeze in Base Rates ML20209C3431999-06-22022 June 1999 Forwards Addendum 1,Rev 14 to Pilgrim Station Security Plan,Iaw 10CFR50.54(p)(2).Changes Proposed Have Been Implemented & Constitute Increase in Plant Defense Plan Commitments.Encl Withheld,Per 10CFR73.21 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217N8911999-10-15015 October 1999 Forwards Rept of Changes,Tests & Experiments at Pilgrim Nuclear Power Station for Period of 970422-990621,IAW 10CFR50.59(b).List of Changes Effecting Fsar,Encl ML20217C3151999-10-0606 October 1999 Forwards Scenario Package for Pilgrim Nuclear Power Station Nrc/Fema Evaluated Exercise Scheduled for 991207.Without Encl ML20217C8051999-10-0505 October 1999 Forwards Proprietary Results of Audiologic Evaluations for Jp Giar,License SOP-10061-3.Attachment Clearly Shows Requirements for Operator Hearing Ability Are Met. Proprietary Info Withheld,Per 10CFR2.790(a)(6) ML20217D5591999-10-0505 October 1999 Documents Pilgrim Nuclear Power Station Five Yr Survey of Main Breakwater.Survey Has Determined That Pilgrim Main Breakwater Is Intact & Remains Adequately Constructed to Perform Designed Safety Function ML20216J9961999-09-29029 September 1999 Forwards Resume of Person Identified as Acting RPM in Licensee to NRC Re Notification That Person Named in License Condition 11 of 20-07626-02,is No Longer Employed at Pilgrim Station.Resume Withheld,Per 10CFR2.790 ML20212H1441999-09-23023 September 1999 Withdraws 990121 Request for License Change Re Emergency Core Cooling Sys Net Positive Suction Head,Due to Incorrect Datum Preparation ML20212H1381999-09-23023 September 1999 Submits Info in Support of Request Filed on 990730 to Grant one-time Exemption from 10CFR50,App E,Authorizing Biennial Full Participation Emergency Preparedness Exercise to Be Conducted in 2002 Instead of 2001 ML20216F3451999-09-16016 September 1999 Forwards Summary Rept Providing Results of ISI Conducted at PNPS on-line & Refueling Outage (RFO 12) ML20216E7111999-09-0909 September 1999 Forwards License Renewal Application Including Form NRC-398 & Form NRC-396 for Jp Giar,License SOP-10061-3.Without Encls ML20216E5891999-09-0707 September 1999 Forwards Copy of Pilgrim Station Organization Structure. Encl Refelcts Changes in Upper Mgt Level Structure.Changes Were Effective 990901 ML20211M4501999-09-0303 September 1999 Informs That Pilgrim Nuclear Power Station Plans to Conduct Full Participation Emergency Preparedness Exercise with Commonwealth of Ma on 991207,IAW 10CFR50,App E,Section IV.F.2 ML20211M9161999-08-31031 August 1999 Submits Review & Correction of Info in Reactor Vessel Integrity Database (Rvid),Version 2,re Pilgrim Station ML20211J8391999-08-30030 August 1999 Forwards Rev 1 to Provisional Decommissioning Trust Agreement for Plant,Changing Portions of Agreement to Permit Up to Two Distributions & Clarify Formula for Distribution ML20211C3381999-08-19019 August 1999 Provides semi-annual LTP Update,Including Schedule, Commitment Descriptions,Progress Since Last Update & Summary of Changes.Rev Bars Indicate Changes in Status Since Last Submittal ML20211B3841999-08-16016 August 1999 Forwards Response to NRC Second RAI Re Pressure Locking & Thermal Binding of SR power-operated Gate Valves ML20210U4831999-08-13013 August 1999 Forwards fitness-for-duty Program Performance Data Sheets for Period of 990101-0630,per 10CFR26.71(d) ML20210S0891999-08-0909 August 1999 Forwards Amend 11 to Indemnity Agreement B-48 Signed by Boston Edison Co & Entergy Nuclear Generation Co ML20210R6251999-08-0606 August 1999 Provides Supplementary Info on USI A-46 Implementation Methodology at Pilgrim Station,To Enable NRC to Perform Evaluation & Issuance of Plant Specific SER for Plant ML20210M9411999-08-0202 August 1999 Requests That NRC Treat Pending Actions Requested by Beco Prior to 990713,as Requests Made by Entergy.Ltr Requests That Minor Administrative Changes to License Amend 182 & Associated Ser, ,reflect 990713 Transfer ML20210H8761999-07-30030 July 1999 Requests That NRC Grant Exemption from Requirements of 10CFR50,App E,Section IV F,Which Would Authorize Rescheduling of 2001 Biennial Full Participation Emergency Preparedness Exercise for Pilgrim Station to 2002 ML20210H8661999-07-29029 July 1999 Provides Revised Response to GL 96-06 & Addresses NRC Insp Concern for Containment Penetration X-12.Info Submitted to Facilitate NRC Review & Closeout of Subject GL for Plant ML20216D4131999-07-22022 July 1999 Informs That J Conlon,License OP-11040-1,terminated Employment with Beco on 990703,per 10CFR50.74.Individual Will Not Participate in Util Licensed Operator Requalification Training Program ML20210C4151999-07-19019 July 1999 Informs That Util Intends to Submit Approx Eight Licensing Actions in FY00 & Eight in FY01,in Response to Administrative Ltr 99-02.Actions Are Not Expected to Generate Complex Reviews ML20210F3711999-07-14014 July 1999 Informs NRC That Effective 990713,listed Pilgrim Station Security Plans Have Been Transferred from Boston Edison to Entergy & Are Still in Effect ML20209C3851999-07-0606 July 1999 Forwards Redacted Draft of Decommissioning Trust Agreement Re Transfer of PNPS & NRC Operating License & Matls License from Boston Edison Co to Entergy Nuclear Generating Co ML20209C7761999-07-0606 July 1999 Submits Annual Summary Rept of Changes Made to QAP Description as Described in QA Manual,Vol Ii.Rept Covers Period of Jul 1998 Through June 1999.No Changes Made During Period ML20209B9411999-06-30030 June 1999 Discusses Deferral of IGSCC Welds to RFO 13.Deferral of Welds to Refueling Outage 13 Does Not Impact Acceptable Level of Quality & Safety Per 10CFR50.55(a)(3)(i) Since Plant in Compliance W/Exam Percentage Requirements ML20209B9431999-06-30030 June 1999 Provides Formal Notification That Closing Date for Sale & Transfer of Pilgrim Station Scheduled to Occur on 990713. a Wang Will Be Verbally Notified of Time of Sale Closing ML20209B9791999-06-29029 June 1999 Forwards Rev 13A to Pilgrims COLR for Cycle 13,IAW TS 5.6.5 Requirements.Rev 13A Provides cycle-specific Limits for Operating Pilgrim During Remainder of Cycle 13 ML20209A8701999-06-25025 June 1999 Responds to NRC Request for Info Re Y2K Readiness of Computer Sys at Nuclear Power Plants. Y2K Readiness Disclosure for Plant,Reporting Status of Facility Y2K Readiness Encl ML20210U5901999-06-25025 June 1999 Opposes Merger of Bec Energy & Commonwealth Energy Sys in Commonwealth of Massachusetts.Expresses Skepticism Re Claim by Companies That Consumers Will Benefit from Proposed Consolidation & four-year Freeze in Base Rates ML20209C3431999-06-22022 June 1999 Forwards Addendum 1,Rev 14 to Pilgrim Station Security Plan,Iaw 10CFR50.54(p)(2).Changes Proposed Have Been Implemented & Constitute Increase in Plant Defense Plan Commitments.Encl Withheld,Per 10CFR73.21 ML20195G3721999-06-0707 June 1999 Informs That Proposed Indicators Failed QA Assessments for Digital Verification,Validation & Control of Software. Proposed Mod Can Be Completed on-line ML20195B5021999-05-27027 May 1999 Provides Suppl Info to 990203 Request of Beco That NRC Consent to Indirect Transfer of Control of Util Interest in License DPR-35.Request Described Proposed Merger of Bec Energy with Commonwealth Energy Sys ML20207D4681999-05-24024 May 1999 Provides Addl Info to That Included in Beco Ltr 98-123 Dtd 981001,addressing NRC Concerns Described in GL 96-06, Concerning Waterhammer in Reactor Bldg Closed Cooling Water Sys ML20195B9051999-05-20020 May 1999 Forwards Completed Renewal Applications for Listed Operators.Without Encls ML20206J4901999-05-0606 May 1999 Forwards Completed License Renewal Application,Including Forms NRC-398 & 396 for Sc Power,License OP-6328-3 ML20206P0711999-05-0606 May 1999 Forwards NRC Form 396, Certification of Medical Exam by Facility Licensee, for K Walz,License SOP-10886-1.Encl Withheld IAW 10CFR2.790(a)(6) ML20206D3621999-04-27027 April 1999 Informs NRC That Final Five Sys self-assessments Required to Fulfill Commitment Made in 980828 Response to Insp Rept 50-293/98-04 Were Completed on 990422.Completion Was Delayed by High Priority Refueling Outage 12 Preparatory Work ML20205R9871999-04-21021 April 1999 Forwards Affidavit of JW Yelverton of Entergy Nuclear Generation Co Supporting Request for Withholding Info from Rept on Audit of Financial Statements for Year Ended 971231. Pages 16 & 18 of Subj Rept Also Encl ML20207B0891999-04-20020 April 1999 Forwards e-mail Message from Constituent,J Riell Re Y2K Compliance of Nuclear Power Plant in Plymouth,Massachusetts. Copy of Article Entitled Nuke Plants May Not Be Y2K Ready Also Encl ML20206A2741999-04-16016 April 1999 Dockets Encl Ltr Which Was Sent to AL Vietti-Cook Re Condition of Approval of Transfer of License & License Condition for DPR-35.Encl Resolves Issues Between Attorney General of Commonwealth of Massachusetts & Applicants ML20205P9131999-04-16016 April 1999 Submits Applicant Consent to Listed Condition of Approval of Transfer of License & License Condition for License DPR-35 & Affirmatively Request That NRC Adopt Listed Language in Order ML20205P9271999-04-16016 April 1999 Withdraws Motion for Leave to Intervene & Petition for Summary Or,In Alternative,For Hearing.Requests That NRC Adopt Condition of Approval of Transfer of License & License Condition Agreed to Beco & Entergy Nuclear Generation Co ML20205Q9231999-04-15015 April 1999 Forwards Proprietary & non-proprietary Addl Info in Support of Request to Transfer of Plant FOL & Matls License to Entergy Nuclear Generation Co.Proprietary Info Withheld,Per 10CFR2.790 ML20205P9631999-04-15015 April 1999 Provides Attachments a & B in Support of Request for Transfer of Plant Operating License & NRC Matl License from Beco to Entergy Nuclear Generation Co as Submitted in Ref 1. Info Provided in Response to Request at 990413 Meeting ML20205H9281999-04-0707 April 1999 Requests Withdrawal of Uwua Locals 369 & 387 Unions Joint Intervention in Listed Matter ML20205F3731999-04-0202 April 1999 Submits Addl Info Provided in Support of Request for Transfer of Pilgrim Nuclear Power Station Operating License & Matls License.State of Ma Order Authorizing Divestiture & Copy of Financial Arrangement Encl ML20204H3771999-03-26026 March 1999 Informs That Local 387,Utility Workers Union of America,AFL- Cio Voted to Approve New Contract with Entergy Nuclear Generation Co & Voted to Accept Boston Edison Divestiture Agreement ML20205D4231999-03-24024 March 1999 Forwards Decommissioning Funding Rept for Pilgrim Nuclear Power Station,In Accordance with 10CFR50.75(f)(1) 1999-09-09
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. . gf 10 CFR 2.201 l
BOSTON EDISON l- Pilgrirn Nuclear Power Station i Rocky Hill Road Plymouth, Massachusetts 02360 ,
E. T. Boulette. FnD Senior Vice President-Nuclear !
June 18, 1993 :
BECo Ltr. 93-77 U.S. Nuclear Regulatory Commission l Attn: Document Control Desk <
l Washington, D.C. 20555 l
i Docket No. 50-293 License No. DPR-35 r
SUBJECT:
REPLY TO NOTICES OF VIOLATION (REFERENCE NRC REGION' INSPECTION REPORT NO. 50-293/93-06)
Dear Sir:
i Enclosed is Boston Edison Company's reply to the Notices of Violation contained in the- .
subject inspection report. Enclosures 1 and 2 respond to Notices of Violation 'A' and i
'B', respectively. .
Please do not hesitate to contact me if there are any questions regarding the enclosed reply. }
db.
Enclosure:
Reply to Notices of Violation !
cc: Mr. Thomas T. Martin Regional Administrator, Region I U.S. Nuclear Regulatory Commission 475 Allendale Rd.
King of Prussia, PA 19406 Mr. R. B. Eaton Div. of Reactor Projects I/II ,
Office of NRR - USNRC One White Flint North - Mail Stop 1401 11555 Rockville Pike Rockville, MD 20852 3
~
Sr. NRC Resident Inspector - Pilgrim Station 9306280129 930618 "PDR ADOCK'05000293
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!. . ENCLOSURE 1 REPLY TO NOTICE OF VIOLATION 'A' Boston Edison Company Docket No. 50-293
[
Pilgrim Nuclear Power Station License No. DPR-35 1
L During an NRC inspection conducted on March 14, 1993 - April,19, 1993, two violations ~of i NRC requirements were identified. In accordance with the " General Statement of Policy and Procedure for NRC Enforcement Actions," 10.CFR Part 2, Appendix C (1991), violation ' A' is listed below:
NOTICE OF VIOLATION 'A' Technical specification 3.6.A.2 states that critical core operation shall not be conducted.
unless the reactor vessel temperatures are above those defined by the appropriate curves on Figures 3.6.1, 3.6.2,'and 3.6.3._ At stated pressure, the reactor vessel bottom head may be maintained at temperatures below those temperatures corresponding to the: adjacent reactor vessel shell as shown in Figures 3.6.1 and 3.6.2.
Technical Specification 3.6.A.2 further states that in.the event this requirement is not met, achieve stable reactor conditions with reactor vessel temperature above that. defined by the appropriate curve and obtain an engineering evaluation to determine the appropriate course of action to take.
Contrary to the above, on March 13-14, 1993, during reactor depressurization, the reactor vessel bottom head pressure-temperature limits for subcritical cooldown as defined by Technical Specification Figure 3.6.2 were exceeded for approximately three hours and twenty minutes; however, an engineering evaluation to determine the appropriate course of action to take was not obtained until March 19, 1993 after:recctor restart and in response to NRC questioning.
This is a Severity Level IV violation (Supplement: 1).
REASON FOR THE VIOLATION The engineering evaluation. specified by Technical . Specification 3.6. A.2 was not conducted prior to reactor startup because the Reactor Vessel pressure-temperature (P-T) limit was not identified as having been exceeded until after the startup. The P-T' limit was exceeded during the March 13-14, 1993 cooldown. The condition was reported in LER 93-004-00. The cooldown occurred after the load rejection scram that occurred on March 13, 1993. The cooldow.n was complicated by a subsequent loss of preferred offsite power (345KV) that de-energized nonsafety-related components including the drive motors of the Recirculation System Loops ' A' and 'B' motor-generator (MG) sets / pumps. A loss of forced circulation in the' Reactor Vessel (RV) occurred as a-result of the de-energization of the MG sets / pumps 'A' and 'B'. A post trip review was conducted.
Licensed operator activities related to cooldown, loss of forced circulation in the RV, and post trip review are governed by approved procedures. The procedures include:
Procedure 2.1.7, " Vessel Heatup and Cooldown"; Procedure 2.4.24, " Reactor Vessel Cold Water Stratification"; and, Procedure 1.3.37, " Post-Trip Reviews". The administrative controls in these procedures, individually and/or collectively, were not sufficient-to-ensure the performance of an engineering evaluation if the P-T limit were exceeded.
1
l l . An overview of the procedures is provided as follows:
- Procedure 2.1.7 is the principal method of monitoring RV metal temperature and pressure during a heatup or cooldown. The' procedure referenced Technical Specifications 3.6.A.1/4.6.A.1 and 3.6.A.2/4.6.A.2. The procedure included Attachment 1 for logging temperatures and pressures and also included Technical ,
Specifications Figures 3.6.1, 3.6.2, and 3.6.2. Attachment 1, however, did not !
specify a check or comparison of the recorded pressure and pressure to the P-T !
limit.
- Procedure 2.4.24 did not direct the operators to review Technical Specification Figure 3.6.2 if a loss of recirculation flow occurred during a heatup or cooldown or Figure 3.6.3 if a loss of recirculation flow occurred during power operation.
The loss of preferred offsite power that occurred after the scram on March 13, 1993, resulted in a loss of forced circulation in the RV. The operators did not check or compare the resulting or subsequent RV pressure-temperature condition to Figure 3.6.2 because Procedure 2.4.24 did not direct this action.
l l
- Procedure 1.3.37 did not specifically require an evaluation or comparison of j transitory parameters governed by Technical Specifications to Technical Specifications including Figure 3.6.2. The RV pressures and temperatures recorded during the cooldown on March 13-14, 1993, were not compared to the P-T limits of Figure 3.6.2. Therefore, the P-T limits were not identified during the post trip review as being exceeded during the cooldown. Consequently, an engineering evaluation of the P-T condition experienced during the cooldown was not requested to determine the appropriate course of action to take as specified by Technical Specification 3.6. A.1.
The licensed operator training program includes simulator training. This training includes simulated cooldowns. The cooldown simulation, however, assumed an uninterrupted cooldown. Consequently, operator simulator training for a cooldown did not include operator actions if a RV pressurization or P-T condition requiring action occurred during a cooldown.
An INP0 document (SER 5-93) describing two industry events in 1992 involving RV cooldown and heatup rates and P-T limits being exceeded due to the loss of recirculation flow l following a scram was issued on February 24, 1993. The document was processed as part of l the Operating Experience Review Program (0ERP). The document was assigned for disposition
, by the Operations Section (comments 1 and 3) and Nuclear Training Department (comment 2) l on March 8, 1993. The Operations Section disposition was that comments 1 and 3 were addressed by procedure 2.4.24. The comments were dispositioned on March 10, 1993.
Comment 2 was dispositioned by the Nuclear Training Department on May 4, 1993.
Essentially, the disposition was to incorporate SER 5-93 into the Licensed Operator j Requalification Training Program and the training module for Shift Technical Advisors and i Senior Reactor Operator candidates.
i 1
2
. 00'RRECTIVE ACTION TAKEN AND RESULTS ACHIEVED 1 l
P'rocedures 2.1.7 (then Rev. 27), 2.4.24 (then Rev. 8), and 1.3.37 (then Rev. 7) have been j revised. Essentially, the purpose and focus of the changes were to specifically reference and/or incorporate Technical Specifications Figures 3.6.1, 3.6.2, and 3.6.3, as applicable. The changes to procedure 2.1.7 included additional steps that compare RV P-T conditions to the P-T limits and initiate actions, including an engineering evaluation, if a P-T limit is exceeded. The changes to procedure 2.4.24 included operator direction to refer to procedure 2.1.7 and determine that RV pressure-temperature is in compliance with-Technical Specifications limits. The changes to procedure 1.3.37 included a check of selected transitory parameters governed by Technical Specifications, and preliminary assessment of selected systems' responses.
Licensed operators received training as part of corrective action. The training included discussion and review of LER 93-004-00, the INP0 document SER 5-93, and the changes to procedures 2.1.7 (Rev. 29) and 2.4.24 (Rev. 9). The training was completed during the recent refueling outage (RF0 9) prior to.startup. ;
The effects of exceeding the P-T limit during the cooldown 'were evaluated. The evaluation l concluded the RV did not exceed ASME Section III structural limits nor did the RV exceed -
ASME Section XI fracture toughness limits. ]
Reports submitted to the NRC since 1972 and previous scram reports were reviewed. The review focused on events involving RV pressurization with no forced circulation. The review identified no previous event or condition involving a pressurization with no forced circulation in the RV.
CORRECTIVE ACTION TO PRECLUDE RECURRENCE The cooldown simulation is being evaluated for improvement. The focus of the evaluation is to consider an interruption during a cooldown and/or operator actions if a RV pressurization or P-T condition requiring action occurs during a cooldown.
The changes to Procedure 1.3.37 will be reviewed as part of the regularly scheduled training program for senior reactor operators.
Technical Specification 3.6.A will be evaluated for possible improvement. The focus for improvement is to specify and/or clarify the plant conditions in the same manner identified on Figures 3.6.1, 3.6.2, and 3.6.3. This additional action complements the changes made to Procedures 2.1.7, 2.4.24, and 1.3.37.
DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED Full compliance was achieved when the engineering evaluation of the P-T condition was completed. The evaluation was approved at the end of March 1993, and a copy was provided to the NRC Resident Inspector.
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. ENCLOSURE 2 REPLY TO NOTICE OF VIOLATION 'B' Boston Edison Company Docket No. 50-293 Pilgrim Nuclear Power Station License No. DPR-35 During an NRC inspection conducted on March 14, 1993 - April 19, 1993, two violations of NRC requirements were identified. In accordance with the " General Statement of Policy and Procedure for NRC Enforcement Actions," 10 CFR Part 2, Appendix C (1991), violation 'B' is listed below:
NOTICE OF VIOLATION 'B' 10 CFR 50 Appendix B, Criterion III, " Design Control" states that design changes shall be subject to design control measures commensurate with those applied to the original design.
Boston Edison Quality Assurance Manual Volume II, Section 3.3.2.8 requires that methods for verifying design changes, such as design reviews, alternative calculations, and .
' qualification testing be properly chosen and followed; the most adverse design conditions be specified for test programs used to verify the adequacy of designs. ;
Contrary to the above, the licensee failed to establish adequate design controls to ensure that the trip setpoints for the main input breakers to the voltage regulating i
transformers, which were installed via plant design change during the 1992 mid cycle outage to service the safety related 120 VAC Y-3 and Y-4 busses, were proper.
REASON FOR THE VIOLATION The main input circuit breakers of the soltage regulating transformers X55 and X56 tripped open and 120 VAC Safeguards Buses 'A' and 'B' consequently became de-energized because the ,
trip settings of the main input breakers were too low. The event was reported in LER 93-004-00. A root cause analysis concluded the settings were set too low because of an unauthorized change to the trip settings. The analysis included review of the design package (PDC 91-59A), dedication plan test instructions, receipt inspection, and pre-operational test procedure (TP 92-58). The supplier test documents indicated the trip ,
settings were left at the correct setting of '5'. The receipt inspection activities included documentation, physical damage, identification and/or markings, protective covers and seals, cleanliness, and electrical tests, but did not include a requirement to check or verify the trip settings. After installation, transformers X55 and X56 were pre-operationally tested (TP 92-58). The testing included voltage regulation, input breaker contact resistance, current leakage, initial startup and energization, transformer ratio, relay and alarm functional tests. The testing did not include a requirement to check or verify the trip settings since there were no installation or testing activities that would have caused the settings to be changed. The analysis could not determine when the change to the trip settings occurred.
CORRECTIVE ACTION TAKEN AND RESULTS ACHIEVED The trip settings of the main input breakers for X55 and X56 were increased. The change was implemented via a modification change (FRN 93-02-03) on March 15, 1993. The new trip settings included additional margin to preclude a recurrence. The original design trip setting of '5' was sufficient to prevent an unnecessary trip of the input breakers.
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i i l . C0'RRECTIVE ACTION TAKEN TO PRECLUDE RECURRENCE i Visual irispections of selected electrical equipment were conducted while shut down during i RF0'9. The purpose of the inspections was to provide additional assurance the i unauthorized change of the input breakers' trip setting was an isolated occurrence. The inspections were completed with satisfactory results. The inspection results indicated the unauthorized change of the input breakers' trip setting was an isolated occurrence.
Appropriate nuclear engineering organization personnel were made aware of the root cause of the trip of the main input breakers. Interim corrective action consisted of reminding engineering personnel to include in-process verification of adjustable trip settings, when appropriate. Long term corrective action consists of revising NED procedure 3.02' (currently Rev. 30), " Preparation, Review Verification, Approval and Revision of Design Documents for Plant Changes". The change is focused on including verification of the setting of a device having an adjustable setting. When appropriate, the verification would be specified as part of post installation or preoperational testing. The change is expected to be approved by August 1993.
Preventive action supplementing the above noted corrective action was also assessed. The focus for preventive action was the root cause analysis conclusion regarding the unauthorized change to the trip setting of the main input breakers. The preventive action will be to include a summary of the response to this violation in the weekly nuclear ;
organization Division Managers' meeting for discussion with their personnel. <
DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED Full compliance was achieved when the trip setting of the input breakers of transformers X55 and X56 was changed via FRN 93-02-03 on March 15, 1993. j i
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