ML20043G134
| ML20043G134 | |
| Person / Time | |
|---|---|
| Site: | Farley |
| Issue date: | 05/31/1990 |
| From: | Hairston W, Dennis Morey ALABAMA POWER CO. |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| NUDOCS 9006190103 | |
| Download: ML20043G134 (5) | |
Text
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':--:? I Atb;rna Power CompW 40 inntness Ccnter Parkway i
Post Office Dox 1295 Birmingham, Alabama 35201.
- f Telephone 205 868 5581
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. W. G, Hairston, til J Senior Vice President Nuclear Operations Alabama Power.
g Itesouthern electrc system I
June 12, 1990 I
Docket No. 50-364 U. S.' W elcar Regulatory Commission ATIN: DCc.m@t Control Desk Washington, D.
C.-
20555 I
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Joseph M. Farley Nuclear Plant Unit 2 i
Monthly operating Data Report 1
l Attached is the May 1990 Monthly Operating Report for' Joseph M. Farley.
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Nuclear Plant Unit 2, required by section 6.9.1.10 of the Technical 9
Specifications.
If you have any questions, please advise.
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Respectfully submitted, i
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-G. ;NB ED on,:III 3
- l JGS: map /1.6 Attachment 4
cc: Mr. S. D. Ebneter Mr. S. T. Hoffman Mr. G. F. Maxwell j
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JOSEPH M. FARLEY 'NUCIE\\R plMr UNIT 2-NARRATIVE SUbMARY OF OPERATIONS May, 1990-
. The outage to replace containment coolers continued thivugh May 12. The outage-
- was extended approximately three days due to oil leaks on 2A and 2B residual
' heat removal ptanp, motors., The reactor was unde critical at 0047 on May 12.
At 0615 on May 12, during the unit startup, the reactor. tripped due to low-low water level in the. 2A steam generator. - The low-low water level occurred'when:
t.he steam supply valves for the on-service steam generator feedwater planp (SGFp) closed. Testing being perforsned in 'accordance with ~ FNp-2-STp-151'.4j (Main Turbine Protective-Device Test,) resulted in' low electro-hydraulic fluid j
presaure which caused the SGFP valves to close.
-t The unit was synchronized to the grid at 2216 on May 12 and returned to full; power on May 14.
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There were no other unit shutdowns or significant power reductions during the '
month of Sy..
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i The following major safety-related maintenance was perforwxi in the morith of'
'May:
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- 1. - Replaced two cont.ainment coolers. The fan motors were refurbished-on the-two rennining coolers.
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- 2. _ Repaired oil leaks on the 2A and 2B RIIR pump motors.
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- 3. : Replaced blown fuses in auxiliary relay-cabinet to restore main steam:
1 atmospheric relief valve 2B _ to_ full stroke.
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4.
Replaced.the rotating assembly on the 2n charging ptunp. Also, replaced:
existing seal assembly with~a mechanical seal-assembly.
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Miscellaneous corrective and preventive maintenance was perfonned on i
the diesel generators,.
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OeERATING o m REem T DOCKET NO.
50-364 DATE June 6, 1990 s
03tPLETED BY D. N. Morey
'IELEPfENE (205)899-5156 OPERATING STATUS Notes
- 1. Unit Name:
Joseph M. Farley - Unit 2
- 1) Cumulative data since
- 2. Reporting Period:
May 1990 7-30-81, date of
- 3. ' Licensed 'Ihermal Power (Mt):
2,652 comercial operation.
- 4. Nameplate Rating (Gross Me):
860
- 5. Design Electrical Rating (Net NWe):
829 6.: Maximum Dependable Capacity (Gross NWe):
868.6
- 7. Maximum Dependable Capacity (Net MWe):
828.2
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons: N/A
- 9. Power Level To Which Restricted, If Any (Net MWe):
N/A
- 10. Reasons For Restrictions, If Any:
N/A
'Ihis Month Yr-to-Date Cumlative
'11. Hours In Reporting Period 744 3,623 77,472
- 12. Number Of Hours Reactor Was Critical 474.0 3,279.4 59,957.3
- 13. Reactor Reserve Shutdown Hours 0.0 0.0 138.0
- 14. Hours Generator On-Line 457.7 3,262.8 66,334.8
- 15. Unit Reserve Shutdown Hours 0.0 0.0 0.0
- 16. Gross Thermal Energy Generated (MWH) 1,168,621 8,436,301 168,692,568
- 17. Gross Electrical Energy Generated (MWH) 380,622 2,782,340 55,448,882
- 18. Net Electrical Energy Generated (MWH) 355,632 2,641,644 52,585,034
- 19. Unit Service Factor 61.5 90.1 85.6
- 20. Unit Availability Factor 61.5 90.1 85.6
'21. Unit Capacity Factor (Using MDC Net) 57.7 88.0 82.9
.22.. Unit Capacity Factor (Using DER Net) 57.7 88.0 81.9
- 23. Unit Forced Outage Rate 16.6 2.7 4.5
- 24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):
Refueling / Maintenance Outage, September 14, 1990, approximately 7 weeks.
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.25. If Shut Down At End Of Repoit Period, Estimated Date of Startup: N/A
.26. Units In Test Status (Prior to Commercial Operation):
Forecast Achieved INITIAL CRITICALITY 05/06/81 05/08/81 INITIAL ELECTRICITY 35/24/81 U5723/81 -
COMMERCIAL OPERATICN V8/01/81 07/30/81-L Form 2/30 l
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DOCKET NO.
50-364 UNIT-2' DATE ' June 6, 1990 COMPLETED BY D. N. Morey TELEPHONE (205)899-5156 M0tml -
May i
DAY AVERAGE DAILY POWER LEVEL DAY AVrEAGE DAILY POWER LEVEL (M4e-Net)
(MWe-Net) 1 0
17 821 2
0 18 834 l
-3 0
19 831 4
0 20 824 5
0 21 823 6
0 22 829-7 0
23 834 8
0 24 829 9
0 25 825 10 0
26 824 t
11 0
27 823 12 0
28 811 13 276 29 829 14 764 30 835 15 824 31 831 16 825 INSTRUCTIONS On this format, list the average daily unit power level in MWe-Net for each day in the reporting month. Compute to the nearest whole megawatt.
I Form 13/21 i
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7 UNIT SHUTDOWNS AND POWER CEDUCTIONS DOCKET NO.
'50-364 m
UNIT NAME J. M. FARLET - UNIT 2, DATE June 6-1990-C
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COMPLETED BT-D. N.'MOPTT~
8 REPORT MONTH mat
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TELEPHONE:
(2051899-5156 l
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l METHOD OF l LICENSEE l l
l CAUSE & CORRECTIVE l
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l l DURATION l l SHUTTING l EVENT l SYSTEM l COMPONENT l
ACTION TO l
lNO.
l DATE l TTPE l (HOURS)
.l. REASON l DOWN REACTCR l REPORT $ l CODE l CODE l
PREVENT RECUR 2E*fCE
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l l 002 l 900501 l
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195.3 l
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. l N/A l BK l
MO lThe outage to replace containment coolers continued l l
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lfrom 4/27/90.
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l 002 l 900508 l
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75.0 l
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N/A l BP l
MO lThe outage was extended approximately three days l
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l ldue to oil leaks on 2A and 2B residual beat
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jremoval pump motors. The reactor wac made l
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l 003 l 900512 l
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16.0 l
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3 l90-001-00 l SJ l
P lAt 0615 on 5-12-90, during a unit startup, the l
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l2A steam generator. The low-low water level l
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l lon-service steam generator feedwater pump {SGFP) l l
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l lwith FNP-2-STP-151.4 (Main Turbine Protective l
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l l Device Test) resulted in low electro-hydraulic (EN)l l
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l fluid pressure which caused the SGPP valves l
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l lThis event was caused by procedural inadequacy.
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l lFNP-2-STP-151.4 did not provide adequate guidance l l
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lconcerning the initial conditions required to l
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l lnot appropriate to perform this procedure while l
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l feedwater is b.ing provided by a SGFP.
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l lFNP-2-STP-151.4 has been revised to provide l
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l lthe procedure when a SGTP is in service.
j h: Forced Reason:
Method:
Exhibit G-Instructions S: Scheduled A-Equipment Failure (Explain) 1-Manual for Preparation of Data B-Maintenance or Test 2-Manual Scram.
Entry Sheets for Licensee C-Refueling 3-Automatic Scram.
Event Report (LER) File (NUREG-D-Regulatory Restriction 4-Other (Explain) 0161)
E-Operator Training & License Examination F-Administrative Exhibit I -Same Source G-Operational Error (Explain)
H-Other fxplain)
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