ML20042B561
| ML20042B561 | |
| Person / Time | |
|---|---|
| Site: | Yankee Rowe |
| Issue date: | 09/11/1981 |
| From: | Bernard D YANKEE ATOMIC ELECTRIC CO. |
| To: | |
| Shared Package | |
| ML20042B557 | List: |
| References | |
| NUDOCS 8203250423 | |
| Download: ML20042B561 (4) | |
Text
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L YANKEE ATOMIC NUCLEAR POWER STATION MONTHLY STATISTICAL REPORT 81-8 FOR THE MONDI 0F AUGUST, 1981 S
4 P203250423 810913
{DRADOCK 05000029 PDR
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OPERATING DATA REPORT DOCKET NO.
50-29 DATE R10911 COSIPLETED BY n
M_
Rernard TELEPHONE _617-R72-8100 X239C OPERATING STATUS Yankee Rowe Notes
- 1. Unit Name:
- 2. Reporting Period:
Anon" 10R1 Power level restricted by
- 3. Licensed Therms! Power (SIWt):
600 installation of baffle 185 plates in turbine.
- 4. Namepiste Rating (Gross SIWE):
175
- 5. Design Electrical Rt. ting (Net SIWE):
180
- 6. 51sximum Dependable Capseity (Gross atWe):
- 7. Sinimum Dependsble Capseity (Net SIWE):
175
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report. Give Res ons:
' 9. Power LevelTo Which Restricted.If Any (Net alwe):
150 MWe
- 10. Reasons For Restrictions.!f Any:
See Notes This 5!onth Yr..to.Date Cumulative 744.00 5.831.00
!!. Hours In Reporting Period
- 12. Number Of Hours Reactor Was Critical 736 7%
1 671 Ra taa nnR 12
- 13. Resctor Reserve Shutdown Hours 0.00 0.00 P.JO 14, Hours Cenerator On.Line 727.70 3.547.R2 139.559.55
- 15. Urdt Reserve Shutdown Hours -
0.00 n nn 0.00
- 16. Gross Therms! Energy Generated (31WH) 503.234.00 1;407 901 71 74.871.080.52
- 17. Gross Electrical Energy Generated (51WH) 103.880.00,_.
503.226.00 22.888.366.50
- 18. Net Electrics! Energy Generated C,1WH) 96.293.01 465.063.77 21.423.173.46
- 19. Unit Service Factor 97.81 61.70 76.54 l
- 20. Unit Avsilability Factor 97.81 61.70 76.54
- 21. Unit Capacity Factor (Using alDC Net) 73.96 45.58 69.23
- 22. Unit Capacity Factor (Using DER Net) 73.96 45.58 69.23
- 23. Unit Forced Outage Rate 2.19 2.41 5.31
- 24. Shutdowns 5cheduled Over Next 6 Stonths (Type.Date.snd Durstion of Each1:
i
- 25. If Shu' Down At End Of Report Period. Estimated Date of Startup:
t
- 26. Units in Test Ststus (Prior to Commercial Operation):
Forecast Achieved INITIA L CRITICALITY INITIA L ELECTRICITY CONISIERCIAL OPERATION (9/77)
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AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-29 UNIT Yankee Rowe DATE 810911 COSIPLETED BY D. M. Bernard TELEPHONE 617-872-8100 X2390 alONTH AUGUST, 1981 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (31We Net)
(h!We. Net) 1 57.2 17 141.4 142.4 2
93.4 gg 142.0 3
104.2 39 4
106.8 20 48 5 5
121.9 21 132.2 6
127.3 144.3 22 7
131=1 23 144 2 8
132.3 24 143.5 9
133.0 25 143.5 10 133.8 26 143 4 Il 135.7 27 143.2 12 136.5 23 143.3 13 137.6 29 143.4 14 138.8 30 143.3 15 139.8 143.3 3g 16 140.6 l
l l
l INSTRUCTIONS i
On this format. list the average daily unit power leselin 5!We Net for each day in the reporting month. Compute to the nearest whole megawatt.
(9/77)
9 UNITSilUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50-29 UNIT NAME Yankee Rowe DATE 1110911 REPORT AIONTil AUGilST. 1981 COMPLETED liy n M.
Rorn a rd TELEfilONE 617-872-8100 X2390 "E
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..Ek Licensee
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!*o Cause & Currective No.
Date g
3g
.g g 5 Event u?
- E.3 Action to c$ 6 5' j5y Repori
- N0 0
Prevent itecurrence g
3 8/1/81 F
5.5 A
2 81-21 CD VdLV0P Failure of an "0" Ring on the Main Steam Non-Return Valve Operator.
4 8/20/81 F
10.8 A
2 NA NA NA No. I fleater Drain Pump lower bearing seized. The resulting pump failure caused a low suction pressure trip of the Boiler Feed pumps producing a loss of feed. The operator manually tripped the plant.
I 2
3 4
F: Fins ed Hesson:
Method:
Exhibii G. instructions S: Stlieduled A l?quipment Failure (Explain) 1-Manual for l* separation of Data B. Maintenance of Test 7-Manual Scram.
Entry Sheets fin Licensee C Itefueling 3 Automatic Scram.
Evens ItepanI (Llittl Fde INUltEG.
D.Itegulaimy itestriction 4-Other (Explain) 0161I li Opciator Training & License Examination I: Ailminiusative 5
G Operational I nor (limplain)
Exhil it I. Same Source
('8/ 77)
Il Ollici (limplain)
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DOCKET NO.
50-29 UNIT Yankee Rowe DATE giogli CO.lPLETED BY D. M. Bernard TELEPHONE 617-872-8100 X2390 REPORT NONTH AUGUST. 1981 SU'-DIARY OF OPERATING EXPERIENCES 8/1/81 0043 Reactor Critical, recovering from plant trip on 7/31/81 0530 Phased. generator to the high lines 2400 Plant load at 100 MWe and slowly being increased 8/19/81 2400 Plant load at 153.7 MWe 8/20/81 0105 Plant tripped manually due to a loss of feedwater caused by failure of No.1 Heater Drain Pump 0738 Reactor critical, recovering from plant trip 1154 Phased generator to the high lines 8/21/81 2300 Plant at full load i
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