ML20041G215
| ML20041G215 | |
| Person / Time | |
|---|---|
| Site: | Trojan File:Portland General Electric icon.png |
| Issue date: | 02/03/1982 |
| From: | Kent G PORTLAND GENERAL ELECTRIC CO. |
| To: | |
| References | |
| NUDOCS 8203190403 | |
| Download: ML20041G215 (6) | |
Text
'
. -r -
OPERATING DATA REPORT 50-344 DOCKET NO.
DATE 2-3-82 COh!PLETED BY _
G.J. Kent TELEPHONE (snH " W 3713 extension 294 OPERATING STATUS N"'**
'mm nN
- 1. Unit Name:
JANUARY, 1981
- 2. Reporting Period:
3411
- 3. Licensed Thermal Power (SIWt):
l'16
- 4. Nameplate Rating (Gross StWe):
1130
- 5. Design Electrical Rating (Net 51We):
1122
- 6. Maximum Dependable Capacity (Gross 51We):
1080
- 7. Maximum Dependable Capacity (Net SIWE):
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report. Give Reasons:
NA e
NA
- 9. Power LevelTo Which Restricted lf Any(Net 31We):
NA
- 10. Reasons For Restrictions. If Any:
'Ihis Month Yr to.Date Cumulative 744 744 47,496-II. Hours In Reporting Period _
643.2' I
643.2 30,106.4
- 12. Number Of Hours Reactor Was Critical 0
0 2.171.s
- 13. Reactor Reserve Shutdown Hours 620.8 620.8 29,108.9
. - 14. Hours Generator on Line 0
0 1,508.7
- 15. Unit Reserve Shutdown Hours
'1,953,317 1,953,317 91,472,093
- 16. Gross Thermal Energy Generated (SIWH) 626,200 626,200 29,795,571
- 17. Gross Electrical Energy Generated (SIWH) 588,987 588,987 28,119,676
- 18. Net Electrical Energy Generated (51WH)
~~/ 83.4 83.4 61.3
' 19. Unit Service Factor
/
83.4 83.4 64.5
- 20. Unit Availability Factor
/
73.3 73.3 s4.n
- 21. Unit Capacity Factor (Using SIDC Net)
/
70.1 70.1 52.4
- 22. Unit Capacity Factor (Using DER Net)
I /,
16.6 16.6 21.7
- 23. Unit Forced Outage Rate
- 24. Shutdowns Scheduled OverEe' ^ hehq.Ty[ns,i snd Duration of Eacht:
( Refueling - May, 1982 - 55 Days, NA
- 25. If Shut Down At End Of Report Period. Estimated Date of Startup:
Forecast Achieved
- 26. Units In Test Status (Prior to Commercial Operation):
NA NA
]
INITIAL CRITICALITY NA NA INITIAL ELECTRICITY f
NA Nn 4
COAISIERCIAL OPER ATION 7
9 f /77) A
.I 82O3190403 020303 PDR ADOCK 05000344 R
pop
AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.
50-344 LWIT Troian 2-03-82 DATE
~
COMPLETED llY 1ELEPHONE (503)556-3713 extension 294 MONT!!
JANUARY, 1982 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe Net)
(MWe Net)
I 1047 37 367' 1046 1010 2
gg 3
1046 39 1046 4
1047 20 1047 1046 1048 5
21
'1034 6
1050 22 1045 1034 7
93 3
1034 24 1044 32 991 9
25 e
- 20 671 10 26 m
705.
124 gg 27 1006 64 23 32
- 38 g3 29 14 5,67 30 1034 1035 15 961 3
382 l
16 INSTRUCTIONS On this formst, list the average daily unit puwer levelin MWe.Nc for each day in the reporting month. Compute to the nearest whole megswatt.
D (gj77) l
- Zhu,
50-344 UNITSHUTDOWNS AND POWER REDUCillNS DOCKET NO.
UNIT NAME TROJAN DATE 2-03-82 REPORT MONTil JANUARY, 1982 COMPLETED BY G.J. Kent TELEPilONE (503)s56-3713 extension 294 w.
.E E
.5'E 3
$.53 Licensee Eg Cause & Currective No.
Date g
3g g
jg5 Event u?
e1 Action to o
H
$E 5
j;gg
. Report *
@0 y0
- Prevent Recurrence 6
82-01 01-09-82 F
59.7 A
2 NA HJ PIPEXX ELBOW FAILU'RE ON 18-INCH EXTRACTION SIN LINE 'IO 5B FW HEATER DUE TO MOISTURE EROSION. ' REPLACED ELBOW AND INVESTIGA'EED OTHER ELBOWS WITII SIMILAR STEAM FLOW &
MOISTURE CONTENT (SA,6A,6B,7A,7B) USING UT.
82-02 01-12-82 F
W A
2 NA EB GENRA' NO.2 INVERTER to Y22 FAILED DUE'TO FAl LTY Qp TRANSFORMER AND DIODE.
TRANSFORMER &
DIODE REPLACEb. WESTINGHOUSE INVESTIGI TION CONTINUES.
82-03 01-16-82 F
20.5 A
3 NA EB GENRA NO. 2 INVERTER 'IO Y22 FAILED DUE TO FAl LTY TRANSFORMER.
CAUSED AN SI SIGI AL AND REACTOR TRIP DUE TO THE STEAM DUMP.
VALVES OPENING AND CAUSING ACTUAL HIGH STEAM FLOW BISTABLE TRIPS CONCURRENT WITH LOW STEAM LINE PRESSURE. LOSS OF 1 JS Y22 FAILED PT-506 AND ARMED THE STEAM I UMP AND ALSO FAILED THE SUMMATOR USED TO CC MPUTE TREF WHICH THEN SAW AN APPARD4T LOAD RI JECTION TO OPEN THE DUMPS.
'see attached)
I 2
3 4-F: Forced Reason:
Method:
Exhibit G - Instructions S: Scheduled A Equipment Failure (Explain) 1-Manual for Preparation of Data i
B-Maintenance of Test
- 2. Manual Scram.
Entry Sheets for Licensee C Refueling J. Automatic Scram.
Event Report (LER) File (NUREG-4 Other(Explain) 0161)
D Regulatory Restriction E-Operator Training & IJcense Examination F-Administrative 5
G-Operational Error (Explain)
Exlubit I-Same Source (9/77) ll-Other (Explain)
UTIIT SIIUTDOW'IS AND PONER REDUCTIONS Page 2 IS PERFORMING A CONTROL LOOP SEPARXTION ANALYSIS 'IO DETERMINE FEASIBILITY FOR POD CONTROL, STEAM DUMP, AND OTIIER POWER SUPPLY CIIANGES AT TROJAN., STEAM DUMP LOAD REJECTION CONTROLLER FUSE (PB-506C)
WAS PULLED PER WESTINGIIOUSE RECOtr-tENDATION UNTIL ANALYSIS IS COMPLETED.
[
81-04 01-26-82 S
0.0 B
NA IIII IITEXCII SCIIEDULED POWER REDUCTION TO PLUG TUBES IN 2A FW IIEATER.
s
.d 0F OPERATING EXPERIENCE DOCIGT NO:
50-344 DATE:
2-03-82 COMPLETED SY:
G. G. Bair TELEPHONE:
503-556-3713 Ext. 234 OPERATION:
The plant entered January at 100% power. Operation continued until Jan 9, 1982 when a manual reactor trip was ordered due to a failed elbow in an 18-inch steam line to the 5B FW heater. The elbow was replaced and the main generator was synchronized i
onto the gr-id January 11, 1982. The following day the reactor was manually tripped due to a failure of No. 2 inverter and loss of instrument bus Y22.
Two and one-half hours later a high temperature (205'F) appeared for the reactor vessel flange leak-off; a containment entry was made to cycle the reactor vessel flange leak-off manual isolation valves which caused the temperature to return to normal. Later in the day a spurious 4
safety injection (SI) signal was received when instrument bus Y22 was shif ted from YO2 to No. 2 ir erter. The SI was caused by Tave < 553*F briefly and steam line high flow indication. When Y22 was deenergized the steam flow bistables on each loop powered...
(See Attached Page for Continuation)
MAJOR SAFETY RELATED MAINTENANCE:
Completed semiannual preventive maintenance on the east auxiliary FW pump. Completed quarterly preventive maintenance on the diesel fire pump driver. Replaced transformers in Uos. 2 and 4 inverters.
I f
MISCELLANEOUS MAINTENANCE: Completed repairs to the non-ESF electric auxiliary FW- -
pump when it failed to start after the reactor trip on January 9, 1932.
Replaced mechanical seal on north BIT recirc pump.
1 Plugged 16 tubes in 2A FW heater.
t
.i i
t LICENSE CHANCES:
NONE i
l MISCELLANEOUS: IAEA was on site to inspect their camera surveillance equipment.
The primary activity that has been increasing during the current cycle has reached about 75% of technical specification limit.
}
-r,--,
,n..
,___.__,_,~%
m_,,,.,,,-,,
.m,-,
7 SUMMANY OF OPERATING EXPERIENCE Page 2 from Y22 tripped, completing the SI logic. The main generator was sychronized on the grid early January 14, 1982.
On January 16, 1982 No. 2 inverter failed while at 100% power. An SI with e reactor trip followed due to the steam dump valves opening causing actual high steam flow bistable trips concurrent with low steam line pressure. Loss of bus Y22 failed PT-506 and armed the steam dump and also failed' the summator used to compute TREF which then saw an apparent load rejection and opened the dumps. Laring the reactor startup on January 18, 1982 control rod D2 would not move. The startup was terminated and all rods inserted into the core. A diode in the movable gripper assembly was replaced.
The main generator was sychronized onto the grid at 0550 hours0.00637 days <br />0.153 hours <br />9.093915e-4 weeks <br />2.09275e-4 months <br /> the same day.
On January 26, 1982 power was reduced to 70% power to remove the FW heater string from service. Sixteen tubes were plugged in the 2A FW heater and the train was placed back in service. The plant completed the month'at 100% power.
r I
n.