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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217H4661999-10-18018 October 1999 Forwards Changes to EPIPs IAW 10CFR50.54(q) & 10CFR50,App E, Section V.Details of Changes Encl ML20216J8241999-09-30030 September 1999 Notifies of Removal of NRC Headquarters & Region III Offices from Controlled Copy Distribution of Certain CE Documents. Specific Documents,Associated Controlled Copy Numbers & NRC Location Affected Are Shown on Attachment to Ltr ML20211G1221999-08-27027 August 1999 Forwards fitness-for-duty Program Performance Data for Each of Comm Ed Nuclear Power Stations & Corporate Support Employees within Scope of Rule for six-month Period Ending 990630,IAW 10CFR26.71(d) ML20210N5651999-08-0606 August 1999 Forwards Rev 8 to Nuclear Generating Stations Emergency Plan, for Plants.With Summary of Changes ML20210M9131999-08-0202 August 1999 Forwards Response to NRC AL 99-02, Operating Reactor Licensing Action Estimates, for Fys 2000 & 2001 for Comed ML20210L1061999-08-0202 August 1999 Forwards Insp Rept 50-010/99-13 on 990702-27.No Violations Noted.Insp Examined Activities in Areas of Facility Management & Control & Radiological Safety ML20210D2961999-07-20020 July 1999 Forwards Corrected Info for DNPS Unit 3 MOR for June 1999. Year-to Date Forced Outage Hours Should Have Read 70 Hours Instead of 0 on Page 8.Error Also Affected Cumulative Forced Outage Hours Which Should Have Been 24,761 ML20210B7071999-07-16016 July 1999 Responds to Requesting Review & Approval of Three Proposed Changes to Ceco QA TR,CE-1A Per 10CFR50.54(a)(3) & 10CFR50.4(b)(7) ML20196J9131999-07-0101 July 1999 Submits Status of Nuclear Property Insurance Currently Maintained for Braidwood,Byron,Dresden,Lasalle County,Quad Cities & Zion Nuclear Power Stations,Per 10CFR50.54(w)(3) ML20196J9061999-07-0101 July 1999 Provides Evidence That Util Maintains Guarantee of Payment of Deferred Premiums in Amount of $10 Million for Each of Thirteen Reactors,Per 10CFR140.21 ML20196K3231999-06-30030 June 1999 Informs That Effective 990703,NRC Project Management Responsibility for Dresden,Unit 1 Station Will Be Transferred to P Ray ML20209B8241999-06-30030 June 1999 Forwards Five 3.5 Inch Computer Diskettes Containing Revised Annual Dose Repts for 1994 Through 1998 for Individuals Receiving Neutron Dose Not Previously Included in Reported Total Effective Dose Equivalent Values.Without Diskettes ML20196D3491999-06-18018 June 1999 Forwards Insp Repts 50-237/99-08 & 50-249/99-08 on 990408-0521.Four Non-Cited Violations Noted.Maint on safety- Related Emergency CR Not Performed Well.Low Impact Issues Re Communications Present in Operations,Maint & Security ML20212J0541999-06-17017 June 1999 Responds to Requesting That NRC Staff ...Allow BWR Plants Identified to Defer Weld Overlay Exams Until March 2001 or Until Completion of NRC Staff Review & Approval of Proposed Generic Rept,Whichever Comes First ML20195E3451999-06-0707 June 1999 Forwards 3.5 Inch Computer Diskette Containing Revised File Format for Annual Dose Rept for 1998,per 990520 Telcon Request from Nrc.Each Station Data Is Preceded by Header Record,Which Provides Info Necessary to Identify Data ML20195D6351999-06-0404 June 1999 Notifies NRC of Actions That Has Been Taken in Accordance with 10CFR26, Fitness for Duty Programs ML20207G2571999-06-0303 June 1999 Informs That Effective 990328,NRC Ofc of NRR Underwent Reorganization.Within Framework of Reorganization,Division of Licensing Project Management Created ML20195B2301999-05-19019 May 1999 Requests Approval of Proposed Changes to QA Topical Rept CE-1-A,rev 66a.Attachment a Describes Changes,Reason for Change & Basis for Concluding That Revised QAP Incorporating Proposed Changes Continues to Satisfy 10CFR50AppB ML20206Q3111999-05-18018 May 1999 Final Response to FOIA Request for Documents.Forwards App a Records Being Released in Entirety ML20206P2431999-05-13013 May 1999 Forwards Insp Rept 50-010/99-09 on 990325-0506.Two Violations of NRC Requirements Occurred & Being Treated as non-cited Violations Consistent with App C of Enforcement Policy ML20206F5381999-04-30030 April 1999 Forwards Magnetic Tape Containing Annual Dose Repts for 1998 for Braidwood,Byron,Dresden,Lasalle County,Quad Cities & Zion Nuclear Power Stations,Per 10CFR20.2206(c).Without Magnetic Tape ML20206B1501999-04-22022 April 1999 Forwards 1998 Occupational Radiation Exposure for Dresden Nuclear Power Station,Units 1,2 & 3. Rept Was Revised to Rept Only Individual Radiation Exposures Greater than 100 Mrem ML20206B2471999-04-20020 April 1999 Informs That SE Kuczynski Has Been Transferred to Position No Longer Requiring SRO License.Cancel License SOP-31030-1, Effective 990412 ML20205K5521999-04-0202 April 1999 Forwards Partially Withheld Security Insp Repts 50-010/99-07,50-237/99-07 & 50-249/99-07 on 990308-12.Two non-cited Violations Identified Involving Failure of Security Personnel to Implement Required Measures ML20205K5841999-03-31031 March 1999 Submits Rept on Status of Decommissioning Funding for Reactors Owned by Comm Ed.Attachment 1 Contains Amount of Decommissioning Funds Estimated to Be Required Pursuant to 10CFR50.75(b) & (C) ML20196K7001999-03-31031 March 1999 Forwards Dresden Nuclear Power Station,Units 1,2 & 3 Radioactive Effluent Release Rept,Jan-Dec 1998. ODCM Was Submitted by Ltr in Accordance with Dresden TS 6.9.A.4 of Dresden Tech Specs Section 6.14.A.3 ML20205D7231999-03-26026 March 1999 Informs That Region III Emergency Preparedness Inspector Will Be Provided Copy of Comed Exercise Manual for 990526 Annual Exercise at DNPS ML20205B4241999-03-23023 March 1999 Provides Results of drive-in Drill Conducted on 990208,as Well as Augmentation Phone Drills Conducted Since 981015,as Committed to in Util ML20207L7141999-03-0808 March 1999 Discusses Transmitting Changes Identified as Rev 59 to Security Plan for Dresden Nuclear Power Station,Units 1,2 & 3.Staff Determined That No NRC Approval Required in Accordance with 10CFR50.54(p) ML20207D6831999-03-0101 March 1999 Forwards fitness-for-duty Program Performance Data for Each Comed Nuclear Power Station & Corporate Support Employees for Six Month Period Ending 981231,per 10CFR26.71(d) ML20207E0931999-02-26026 February 1999 Informs That Region III EP Inspectors Will Be Provided One Copy of Exercise Evaluation Objectives for 990526 Annual Exercise at Dresden Station as Enclosure to Ltr for Review. Proprietary Encl Withheld ML20203F2541999-02-10010 February 1999 Informs That Beginning 990216,DE Hills Will Be Chief of Operations Branch Which Includes Operator Licensing Function ML20203G3631999-02-10010 February 1999 Forwards Insp Rept 50-010/99-02 on 981218-990129.No Violations Noted.During Insp,Activities in Area of Facility Mgt & Control,Decommissioning Support Activities & Radiological Safety Were Examined ML20203C7001999-02-0202 February 1999 Informs That Mhb Technical Associates No Longer Wishes to Receive Us Region III Docket Info Re Comed Nuclear Facilities.Please Remove Following Listing from Service List ML20202G0621999-01-25025 January 1999 Forwards 1998 Revs to Commitments Rept Made in Docketed Correspondence for Dresden Nuclear Power Station ML20199F3291999-01-14014 January 1999 Ack Receipt of Ltr Dtd 981230,transmitting Changes Identified as Rev 59 to Plant Security Plan,Submitted Under Provisions of 10CFR50.54(p) ML20199E0201999-01-12012 January 1999 Forwards Change to Bases of Dnps,Unit 1 TS Section 3.10, Fuel Handling & Storage. Change Eliminates Reference to Initiation of Generating Station EP Action That Is Incorrect & Not Part of Reason for Min FSP Water Level TS ML20199C8851999-01-11011 January 1999 Forwards Monthly Operating Repts for Dec 1998 for Dnps,Units 1,2 & 3,as Required by TS 6.9.A.5.Year-to-date Generator Hours for Unit 2 for Oct 1998 & Nov 1998 Corrected in Rept ML20206P7411999-01-0707 January 1999 Informs of Delay in Implementation of Strategic Reform Initiative Action Steps.Util Mgt Now Preceeding to Implement Succession Planning Steps for Corporate Ofc & Expects Completion of Action Steps 2 & 3 by 990128 ML20198N7691998-12-30030 December 1998 Forwards Rev 59 to Security Plan for Dresden Nuclear Power Station,In Accordance with 10CFR50.4(b)(4).Rev Withheld ML20198A2531998-12-10010 December 1998 Ack Receipt of Which Transmitted Changes Identified as Rev 57 to Plant Security Plan,Per 10CFR50.54(p).No NRC Approval Is Required ML20198A2511998-12-10010 December 1998 Ack Receipt of ,Which Transmitted Changes Identified as Rev 58 to Plant Security Plan,Per 10CFR50.54(p).No NRC Approval Is Required ML20196E2371998-11-27027 November 1998 Discusses Licensee ,Requesting That Agreement in Be Changed to Reflect Latest NRC Conditions Requiring Licensees to Notify NRC of Transfer of Assets to Affiliates Imposed in Connection with Approval of Transfer ML20196B5871998-11-20020 November 1998 Requests That Svc List for All NRC Correspondence Re Any of Six Comed Nuclear Stations Be Modified Per Attached List.All Other Names Previously Listed Should Be Removed ML20196A4121998-11-19019 November 1998 Forwards Safety Evaluation Accepting Proposed Changes to QA TR CE-1-A,Rev 66,by ,As Modified by Ltrs & 1027.Proposed QA Tr,Rev 66 Continues to Comply with Criteria of 10CFR50,App B ML20195J4271998-11-13013 November 1998 Forwards Insp Repts 50-010/98-18,50-237/98-27 & 50-249/98-27 on 981013-16 & Notice of Violation.Mgt Activities Were Focused Toward Maintaining Effective Security Program ML20195E6451998-11-12012 November 1998 Provides Results of drive-in Drill Conducted on 981007,as Well as Augmentation Phone Drill Conducted on 980917 ML20195F3461998-11-10010 November 1998 Forwards Rev 58 of DNPS Security Plan,Including Listed Changes,Iaw 10CFR50.4(b)(4).Encl Withheld Ref 10CFR73.21 ML20155D2701998-10-27027 October 1998 Forwards Changed Pages from 980423 Submittal Providing Addl Info Marked with Revision Bars & Revised Pages to QA Topical Rept Section 18,for Review ML20154P9051998-10-20020 October 1998 Ack Receipt of 980821 Submittal,Per 10CFR50.54(a),requesting Review & Approval of Proposed Changes That Reduce Commitments in QA TR,CE-1-A.Util Should Refrain from Implementing Subj Changes Until Formal Notification Given 1999-09-30
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217H4661999-10-18018 October 1999 Forwards Changes to EPIPs IAW 10CFR50.54(q) & 10CFR50,App E, Section V.Details of Changes Encl ML20216J8241999-09-30030 September 1999 Notifies of Removal of NRC Headquarters & Region III Offices from Controlled Copy Distribution of Certain CE Documents. Specific Documents,Associated Controlled Copy Numbers & NRC Location Affected Are Shown on Attachment to Ltr ML20211G1221999-08-27027 August 1999 Forwards fitness-for-duty Program Performance Data for Each of Comm Ed Nuclear Power Stations & Corporate Support Employees within Scope of Rule for six-month Period Ending 990630,IAW 10CFR26.71(d) ML20210N5651999-08-0606 August 1999 Forwards Rev 8 to Nuclear Generating Stations Emergency Plan, for Plants.With Summary of Changes ML20210M9131999-08-0202 August 1999 Forwards Response to NRC AL 99-02, Operating Reactor Licensing Action Estimates, for Fys 2000 & 2001 for Comed ML20210D2961999-07-20020 July 1999 Forwards Corrected Info for DNPS Unit 3 MOR for June 1999. Year-to Date Forced Outage Hours Should Have Read 70 Hours Instead of 0 on Page 8.Error Also Affected Cumulative Forced Outage Hours Which Should Have Been 24,761 ML20196J9131999-07-0101 July 1999 Submits Status of Nuclear Property Insurance Currently Maintained for Braidwood,Byron,Dresden,Lasalle County,Quad Cities & Zion Nuclear Power Stations,Per 10CFR50.54(w)(3) ML20196J9061999-07-0101 July 1999 Provides Evidence That Util Maintains Guarantee of Payment of Deferred Premiums in Amount of $10 Million for Each of Thirteen Reactors,Per 10CFR140.21 ML20209B8241999-06-30030 June 1999 Forwards Five 3.5 Inch Computer Diskettes Containing Revised Annual Dose Repts for 1994 Through 1998 for Individuals Receiving Neutron Dose Not Previously Included in Reported Total Effective Dose Equivalent Values.Without Diskettes ML20195E3451999-06-0707 June 1999 Forwards 3.5 Inch Computer Diskette Containing Revised File Format for Annual Dose Rept for 1998,per 990520 Telcon Request from Nrc.Each Station Data Is Preceded by Header Record,Which Provides Info Necessary to Identify Data ML20195D6351999-06-0404 June 1999 Notifies NRC of Actions That Has Been Taken in Accordance with 10CFR26, Fitness for Duty Programs ML20195B2301999-05-19019 May 1999 Requests Approval of Proposed Changes to QA Topical Rept CE-1-A,rev 66a.Attachment a Describes Changes,Reason for Change & Basis for Concluding That Revised QAP Incorporating Proposed Changes Continues to Satisfy 10CFR50AppB ML20206F5381999-04-30030 April 1999 Forwards Magnetic Tape Containing Annual Dose Repts for 1998 for Braidwood,Byron,Dresden,Lasalle County,Quad Cities & Zion Nuclear Power Stations,Per 10CFR20.2206(c).Without Magnetic Tape ML20206B1501999-04-22022 April 1999 Forwards 1998 Occupational Radiation Exposure for Dresden Nuclear Power Station,Units 1,2 & 3. Rept Was Revised to Rept Only Individual Radiation Exposures Greater than 100 Mrem ML20206B2471999-04-20020 April 1999 Informs That SE Kuczynski Has Been Transferred to Position No Longer Requiring SRO License.Cancel License SOP-31030-1, Effective 990412 ML20205K5841999-03-31031 March 1999 Submits Rept on Status of Decommissioning Funding for Reactors Owned by Comm Ed.Attachment 1 Contains Amount of Decommissioning Funds Estimated to Be Required Pursuant to 10CFR50.75(b) & (C) ML20196K7001999-03-31031 March 1999 Forwards Dresden Nuclear Power Station,Units 1,2 & 3 Radioactive Effluent Release Rept,Jan-Dec 1998. ODCM Was Submitted by Ltr in Accordance with Dresden TS 6.9.A.4 of Dresden Tech Specs Section 6.14.A.3 ML20205D7231999-03-26026 March 1999 Informs That Region III Emergency Preparedness Inspector Will Be Provided Copy of Comed Exercise Manual for 990526 Annual Exercise at DNPS ML20205B4241999-03-23023 March 1999 Provides Results of drive-in Drill Conducted on 990208,as Well as Augmentation Phone Drills Conducted Since 981015,as Committed to in Util ML20207D6831999-03-0101 March 1999 Forwards fitness-for-duty Program Performance Data for Each Comed Nuclear Power Station & Corporate Support Employees for Six Month Period Ending 981231,per 10CFR26.71(d) ML20207E0931999-02-26026 February 1999 Informs That Region III EP Inspectors Will Be Provided One Copy of Exercise Evaluation Objectives for 990526 Annual Exercise at Dresden Station as Enclosure to Ltr for Review. Proprietary Encl Withheld ML20203C7001999-02-0202 February 1999 Informs That Mhb Technical Associates No Longer Wishes to Receive Us Region III Docket Info Re Comed Nuclear Facilities.Please Remove Following Listing from Service List ML20202G0621999-01-25025 January 1999 Forwards 1998 Revs to Commitments Rept Made in Docketed Correspondence for Dresden Nuclear Power Station ML20199E0201999-01-12012 January 1999 Forwards Change to Bases of Dnps,Unit 1 TS Section 3.10, Fuel Handling & Storage. Change Eliminates Reference to Initiation of Generating Station EP Action That Is Incorrect & Not Part of Reason for Min FSP Water Level TS ML20199C8851999-01-11011 January 1999 Forwards Monthly Operating Repts for Dec 1998 for Dnps,Units 1,2 & 3,as Required by TS 6.9.A.5.Year-to-date Generator Hours for Unit 2 for Oct 1998 & Nov 1998 Corrected in Rept ML20206P7411999-01-0707 January 1999 Informs of Delay in Implementation of Strategic Reform Initiative Action Steps.Util Mgt Now Preceeding to Implement Succession Planning Steps for Corporate Ofc & Expects Completion of Action Steps 2 & 3 by 990128 ML20198N7691998-12-30030 December 1998 Forwards Rev 59 to Security Plan for Dresden Nuclear Power Station,In Accordance with 10CFR50.4(b)(4).Rev Withheld ML20196B5871998-11-20020 November 1998 Requests That Svc List for All NRC Correspondence Re Any of Six Comed Nuclear Stations Be Modified Per Attached List.All Other Names Previously Listed Should Be Removed ML20195E6451998-11-12012 November 1998 Provides Results of drive-in Drill Conducted on 981007,as Well as Augmentation Phone Drill Conducted on 980917 ML20195F3461998-11-10010 November 1998 Forwards Rev 58 of DNPS Security Plan,Including Listed Changes,Iaw 10CFR50.4(b)(4).Encl Withheld Ref 10CFR73.21 ML20155D2701998-10-27027 October 1998 Forwards Changed Pages from 980423 Submittal Providing Addl Info Marked with Revision Bars & Revised Pages to QA Topical Rept Section 18,for Review ML20154M4291998-10-15015 October 1998 Forwards 1998 Third Quarter 10CFR50.59 Rept of Completed Changes,Tests & Experiments.Completed SEs Compared to Previous Quarterly Repts as Docketed ML20154J4951998-10-0707 October 1998 Forwards Revised Security Plans for CE Listed Nuclear Power Stations,Per 10CFR50.4(b)(4).Changes Do Not Decrease Effectiveness of Station Security Plans.Encl Withheld ML20151Y5101998-09-11011 September 1998 Provides Results of drive-in-drill Conducted on 980804 & Augmentation Phone Drills Conducted Between 980601 & 0831 ML20151Y2931998-09-0909 September 1998 Notifies NRC of Results of Feasiblity Study of Seismically Qualified or Verified Path to Obtain Water from Ultimate Heat Sink & Deliver It to Shell of Isolation Condenser for Each Unit ML20238F7571998-08-28028 August 1998 Forwards fitness-for-duty Program Performance Data for Each of Util Nuclear Power Stations for Six Month Period Ending 980630 ML20237D9771998-08-21021 August 1998 Forwards Proposed Changes to Quality Assurance Topical Rept (QATR) CE-1-A,rev 66,modifying Ref Submittal & Clarifying Certain Changes to QATR Proposed in Util .Page A-1, 6 of 6 of Incoming Submittal Not Included ML20237A8611998-08-0707 August 1998 Requests Approval of Enclosed Qualified Unit 1 Supervisor Initial & Continuing Training Program, Which Ensures That Qualifications of Personnel Are Commensurate W/Tasks to Be Performed & Conditions Requiring Response ML20237A8871998-08-0707 August 1998 Documents Completion of Util Action Items Discussed at 980529 Meeting W/Nrc.Updated Proposal to Consolidate Near Site Emergency Operations Facilities Into Single Central Emergency Operations Facility,Provided ML20236W1311998-07-27027 July 1998 Forwards Response to NRC Re Violations Noted in Insp Repts 50-010/98-15,50-237/98-18 & 50-249/98-18, Respectively.Encl Withheld ML20236T7241998-07-24024 July 1998 Forwards Revised Epips,Including CEPIP-2000 Series Table of Contents & Rev 7 to CEPIP-2121-01, Augmentation Caller Instructions ML20236R2531998-07-16016 July 1998 Summarizes Results of drive-in Drill as Well as Preceeding call-in Drills Conducted Between Each drive-in Drill,As Committed to in 980326 Meeting Between Util & NRC ML20236F8041998-06-29029 June 1998 Forwards Rev 0 to Defueled SAR Dresden Nuclear Power Station Unit 1 Commonwealth Edison Co, Per Requirements of 10CFR50.71(e)(4).Decommissioning Program Plan Is Being Reformatted & Revised Into Defueled SAR SVP-98-170, Advises That AL Misak,License SOP-30832-1,is No Longer Required to Maintain Operator License1998-05-0101 May 1998 Advises That AL Misak,License SOP-30832-1,is No Longer Required to Maintain Operator License ML20247B6521998-04-30030 April 1998 Forwards 1997 Repts for Braidwood,Byron,Dresden,Lasalle,Quad Cities & Zion Nuclear Power Stations.Repts Being Submitted Electronically on Magnetic Tape.W/O Encl ML20217G8841998-04-23023 April 1998 Forwards Proposed Changes to QATR CE 1-A,rev 66.Change Constitutes Major Programmatic Rev to Onsite & Offsite Review Processes as Presently Described in Rept ML20246Q1391998-04-20020 April 1998 Provides Response to Violations Noted in Insp Repts 50-010/98-08,50-237/98-08 & 50-249/98-08.Corrective Actions: Described in Attachment Which Contains Safeguards Matl.Encl Withheld ML20217N3461998-03-31031 March 1998 Provides Basis for Plant Conclusion That Dam Failure Coincident W/Loca Is Beyond Design Basis of Dresden,Units 2 & 3.Licensing Amend Is Not Necessary & Clarifications to UFSAR May Be Made Through Provisions of 10CFR50.59 ML20216H4041998-03-13013 March 1998 Forwards Revs to Byron,Dresden,Lasalle & Zion Station OCDM, Current as of 971231,ODCM Manual & Summary of Changes Included ML20203L2911998-02-27027 February 1998 Provides Revised Schedule for Hazardous Matl Response Drill Described in 971121 Response to Insp Repts 50-010/97-13,50-237/97-13,50-249/97-13 & NOV 1999-09-30
[Table view] Category:UTILITY TO NRC
MONTHYEARML20059F0311990-08-27027 August 1990 Provides Schedule for Completion of Installation of Mods to Plants Reactor Water Level Instrumentation,Per Generic Ltr 84-23.Penetrations Will Be Installed During Outage 13 for Dresden & During Outage 12 for Quad-Cities ML20055H7631990-07-25025 July 1990 Forwards Financial Info Re Decommissioning of Plants ML17202L2861990-07-0202 July 1990 Forwards Dresden II Upper Vessel Contract Variation Review, La Salle II Upper Vessel Fabrication Summary & Quad-Cities II Upper Vessel Fabrication Summary. ML20043D3231990-06-0101 June 1990 Forwards Rev 31 to Security Plan.Rev Withheld (Ref 10CFR73.21) ML20043C8181990-05-30030 May 1990 Forwards Rev 1 to Core Operating Limits Rept,Dresden Station Unit 2,Cycle 12. Rev Reflects MCPR Limit Adjustment for Cycle 12 Due to Number of Reused Channels,Per Discussion of Channel Bow Effects in BWRs in NRC Bulletin 90-002 ML17202G7741990-02-0505 February 1990 Forwards Core Operating Limits Rept,Dresden Station Unit 2,Cycle 12,Rev 0 & Core Operating Limits Rept,Dresden Station Unit 3,Cycle 12,Rev 0. Cycle 12 Startup Expected on 900210 ML19332D3011989-11-15015 November 1989 Provides Update Concerning Evaluation of long-term Improvements to Unit 2 & 3 Isolation Condenser Shell Side Clean Demineralized Water Supply Sys ML19324C2271989-11-0909 November 1989 Forwards Response to Regulatory Effectiveness Review Insp on 890731-0804.Response Withheld ML17285A8081989-10-18018 October 1989 Responds to Request for Info on Environ Qualification of Taped Electrical Splices.Scotch Tapes Allowed by Electrical Test Guide Included Scotch 33,23 & 70 ML20248D0881989-09-21021 September 1989 Forwards Rev 56 to QA Program Topical Rept CE-1-A ML19325C5601989-09-13013 September 1989 Forwards Response to Allegation RIII-87-A-0074 Re Employment Discrimination,Per Eg Greenman 890801 Ltr to C Reid ML20245H3771989-08-0909 August 1989 Forwards Listed Policies,Including Endorsements 24 & 25 to Nelia Policy NF-294,Endorsements 19 & 20 to Maelu Policy MF-128,Endorsements 36 & 37 to Nelia Policy NF-277 & Endorsements 29 & 30 to Maelu Policy MF-114 ML20246L8141989-07-0101 July 1989 Forwards Dresden Nuclear Power Station Monthly Operating Summary Rept for June 1987.Info Previously Submitted on Annual Basis Now Included in Monthly Summary Rept ML20245L6831989-06-29029 June 1989 Forwards Addl Info on Emergency Planning & Fuel Handling Accident,Per E Erickson & R Beck Request ML20245G2411989-06-19019 June 1989 Forwards Endorsements 55,28,205,179,55,37,117,100,108 & 97 to Nelia & Maelu Policies NF-227,MF-114,NF-43,MF-22,NF-253, MF-104,NF-187,MF-54,NF-201 & MF-64.respectively ML20247J1051989-05-17017 May 1989 Responds to Items from SALP 8 Board Repts 50-237/89-01 & 50-249/89-01 for Feb 1988 - Jan 1989.Plant Security Program Now Implements All Aspects of Reporting All Events Identified,Per App E & Section 5.7,to NRC within 1 H ML20246B9501989-04-28028 April 1989 Forwards Rev 55 to CE-1-A, QA Program for Nuclear Generating Stations. Rept Reflects Organizational Changes Resulting from Current Self Analysis Performed in Effort to Improve Effectiveness ML20245J2421989-04-25025 April 1989 Forwards Rev 27 to Security Plan.Rev Withheld (Ref 10CFR73.21) ML20247B6021989-04-13013 April 1989 Forwards Results of Util Investigation of Allegation RIII-88-A-0147 Re Fitness for Duty.Encl Withheld (Ref 10CFR2.790(a)(7)) ML20245A1521989-04-12012 April 1989 Forwards Monthly Performance Rept for Mar 1989.W/o Encl ML20244B5081989-04-10010 April 1989 Forwards Addl Info Re Accident Analysis & Protective Action Plans During Emergency Conditions ML20244A7421989-04-0303 April 1989 Responds to 890201 Telcon Request for Addl Info Re Item 2.2.1.3, Use of Info Handling Sys & Item 2.2.1.4, Mgt Control of Generic Ltr 83-28 ML20244D1101989-03-28028 March 1989 Forwards Corrected Radioactive Effluent Rept for Jul-Dec 1988 for Plant.Final Data for Sr-89,Sr-90,Fe-55,tritium & Gross Alpha Included in Rept ML20248D9741989-03-27027 March 1989 Forwards Response to Requests for Addl Info Re Emergency Plan,Tech Specs & Decommissioning Plan.Info on Emergency Plan Requirements Will Be Provided by 890410,per 890323 Discussion W/P Erickson ML20247B2791989-03-23023 March 1989 Forwards Endorsements 23,18,34,27,202,176,54,36,114,97,105 & 93 to Nelia Policies NF-294,MF-128,NF-277,MF-114,NF-43, MF-22,NF-253,MF-104,NF-187,MF-54,NF-201 & MF-64, Respectively ML20246P2311989-03-20020 March 1989 Forwards Endorsements 203 & 204 to Nelia Policy NF-43, Endorsements 177 & 178 to Maelu Policy MF-22,Endorsements 115 & 116 to Nelia Policy NF-187 & Endorsements 98 & 99 to Maelu Policy MF-54 ML20247G5311989-03-20020 March 1989 Forwards Overheads Used at 890301 Meeting W/Region III Personnel in Working Group Level to Discuss Dc Ground Policy & How It Applies to Facilities ML20235V2721989-03-0101 March 1989 Forwards Corrected Rev 54 to Topical Rept CE-1-A, QA Program for Nuclear Generating Stations, Incorporating Pages 1-38 & 1-44 ML20235V5921989-02-28028 February 1989 Informs That Response to 880707,0927 & 890107 Requests for Addl Info Re Emergency Plan,Tech Specs & Decommissioning Plan Will Be Submitted by 890327,per 890228 Telcon W/P Erickson ML20235U4251989-02-28028 February 1989 Forwards Rev 26 to Security Plan.Rev Withheld ML20247E7771989-02-24024 February 1989 Forwards Radwaste & Environ Monitoring,Annual Rept 1988 ML20235Y6321989-02-22022 February 1989 Forwards Occupational Radiation Exposure Portions of Plants Operating Repts for 1988,per Reg Guide 1.16 ML20235Y8731989-02-14014 February 1989 Forwards Occupational Radiation Exposures Rept for 1988,per Reg Guide 1.16 ML20235Y6481989-02-14014 February 1989 Forwards Occupational Radiation Exposure Rept for 1988,per Reg Guide 1.16 ML20235U3411989-02-13013 February 1989 Forwards Corrected Radioactive Effluent Rept for Jan-June 1988.Final Data for Sr-89,Sr-90,Fe-55,tritium & Gross Alpha Included ML20235Y6541989-02-0606 February 1989 Forwards Occupational Radiation Exposure Rept for 1988,per Reg Guide 1.16 ML20235Y8491989-02-0202 February 1989 Forwards Occupational Radiation Exposure Rept for 1988,per Reg Guide 1.16 ML20235Y8571989-02-0101 February 1989 Forwards Occupational Radiation Exposures for 1988,per Reg Guide 1.16 ML20235Y6401989-01-27027 January 1989 Forwards Occupational Radiation Exposures Rept for 1988,per Reg Guide 1.16 ML20206K1501988-11-21021 November 1988 Provides Addl Info Re Util Decommissioning Plan & Tech Specs Per NRC 880927 Request.Info Provided Discussed W/P Erickson of NRC on 881117 ML20205P9231988-11-0101 November 1988 Discusses Proposed 881116 Meeting Re Dcrdr Mods & Enhancements,Including Program Overview,Summary of Completed & on-schedule Human Engineering Discrepancy Corrections & More Detailed Discussion of Items ML20154N8291988-09-23023 September 1988 Forwards Rev 25 to Security Plan.Rev Outlines Declassification of Unit 1 Reactor Sphere,Core spray/post- Incident Room & Cribhouse.Rev Withheld (Ref 10CFR73.21) ML20154D2881988-09-0808 September 1988 Responds to NRC Bulletin 88-005 & Suppls 1 & 2 Re Piping Supplies,Inc & West Jersey Mfg Co Matls Complying W/Asme Code Requirements.Itemized List of Components Received Encl ML20205A7531988-09-0202 September 1988 Responds to 880707 Request for Addl Info Re Emergency Plan Requirements for Facility Fuel Storage.Response Re Worst Case Skin Doses Projected Onsite & Worst Case Fuel Rod Rupture Provided ML20207F7261988-08-16016 August 1988 Forwards Endorsements 198 & 199,110 & 111 & 101 & 102 to Nelia Policies NF-43,NF-187,NF-201,respectively & Endorsements 172 & 173,93 & 94 & 89 & 90 to Maelu Policies MF-22,MF-54 & MF-64,respectively ML20155D2241988-06-0202 June 1988 Forwards Response to NRC Re Violations Noted in Insp Repts 50-010/88-02,50-237/88-07 & 50-249/88-08. Corrective Actions Withheld ML20154L8391988-05-27027 May 1988 Forwards Rev 24 to Security Plan to Correct & Make Current Identification on Number of Vital Area Doors on Various Levels.Rev Withheld (Ref 10CFR73.21) ML20154L7711988-05-19019 May 1988 Forwards Endorsements 197 to Nelia Policy NF-43,171 to Maelu Policy MF-22,50 to Nelia Policy NF-253,32 to Maelu Policy MF-104,109 to Nelia Policy NF-187 & 92 to Maelu Policy MF-54 ML20153G6091988-04-29029 April 1988 Forwards Environ Rept of Current Decommissioning Status of Dresden 1 & Decommisioning Program Plan for Dresden Nuclear Power Station Unit 1. Fee Paid ML20151U6961988-04-25025 April 1988 Forwards Endorsements 195 & 196 to Nelia Policy NF-43, Endorsements 169 & 170 to Maelu Policy MF-22,Endorsements 99 & 100 to Nelia Policy NF-201 & Endorsements 86 & 87 to Maelu Policy MF-64 1990-08-27
[Table view] |
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3 Commonwealth E
/ ) . Dresden Nucle:r Pow son g i ~ b"# / PRINCIPAL STAFF
\ / Morris, Illinois 604 . , g .g q,-~ Telephone 815/94M99 0.J g t>-
- ll/ 1 D/D PA0 At A/D no gp M' Q} N 6rt (N v &PI EU D mber 17, 1981 y P1ITT U DEP&Of File DJS Ltr. #81-998 Mr. James G. Keppler, Regional Administrator Directorate of Regulatory Operations - Region III U. S. Nuclear Regulatory Connission 799 Roosevelt Road Glen Ellyn, IL 60137
SUBJECT:
Additional Information Concerning the Failure of the Diesel Generator Cooling Water Pumps at Dresden Station on October 23, 1981, and November 19, 1981
REFERENCE:
(a) D. Scott letter to J. Keppler dated December 4, 1961
Dear Mr. Keppler:
On December 4, we provided information to your office concerning our investigation into the cause of the overheating of the Unit 3 and Unit 2/3 diesel generators at Dresden Station on October 23, 1981, and November 19, 1981. This information was provided in reference (a). We concluded that the overheating was the result of insufficient cooling water flow, which occurred because of flow restrictions caused by the failure of the cool-ing water pump discharge check valves. As a result of continuing dis-cussions with members of your staff, we are submitting the additional information below.
We are unable at this time to commit to a firm schedule for modify-ing the instrumentation in the diesel generator rooms to assist the oper-atora in determining flow through the diesel generator heat exchangers.
The engineering study discussed in reference (a) has just been initiated, and the detailed modifications that will result from that study have not yet been determined. When the final modifications are identified, it is our intention to proceed as expeditiously as possible in procurring equip-ment, scheduling the necessary outages, and installing the recommended instrumentation. The final modifications and their schedule for install-ation will be availabl=. for review by your resident inspectors upon com-pletion of the engineering study.
Also, as discussed with members of your staf f, we believe that the difference that we observed in " indicated" pressure at the diesel gener-ator cooling water pumps for the Unit 3 and the Unit 2/3 pumps (See page 3 of reference (a) ) was the result of significantly greater bearing lub-ricating water flow in the Unit 2/3 cooling water pump. At the time this test was conducted, we believe the bearing tolerances on the Unit 2/3 pump were greater than those of the Unit 3 pumps and allowed a signifi-cantly greater lubricating flow through the water lines. This increased flow led to a lower " indicated" pressure and contributed to the difference between the Unit 3 and Unit 2/3 pumps as reported to you in reference (a).
8201130007 811217 Il I[M J pon AnocK 05o00237 DEC S PDR 2319&f ~ f
We continue to believe that the operators had opened both the vent valve and the strainer blowdown valve in the lubricating water supply line, and that this resulted in the " apparent" low pump discharge pressure during the October and November events. We have now installed separate gages which indicate the pressure directly off the discharge volute of all three diesel cooling water pumps.
We believe this letter answers the questions raised by your staff regarding reference (a) and should permit them to allow us to return the operation of the diesel generator cooling water pumps to normal in accor-dance with the conditions of your Confirmatory Action Letter dated Novem-ber 25, 1981.
Very truly yours,
/ .1 -,
/
D. . Scott Station Superintendent Dresden Nuclear Power Station DJS/DLF/jrh cc: C. Reed F. Palmer J. Abc]
D. Farrar J. Brunner T. Rausch File /NRC File / Numerical
Commonwealth Edison Dresden Nuclear Power Sttion R.R. #1 M rris, tilinois 60450 Telephone 815/942-2920 December 4, 1981 DJS Ltr. #81-951 Mr. James G. Keppler, Regional Administrator Directorate of Regulatory Operations - Region III U. S. Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, IL 60137
SUBJECT:
Results of an Investigation into the Unit 3 and Unit 2/3 Diesel Generators at Dresden Nuclear Power Station on October 23, 1981, and November 19, 1981
Dear Mr. Keppler:
While conducting surveillance tests on October 23, 1981, Dresden Station experienced trips of both the Unit 2/3 and Unit 3 Emergency Diesel Generators. The cause of the trips of the diesels is believed to have been insufficient cooling water flow to the diesel heat ex-changers, resulting in protective action trips of the diesels from high temperature. On November 19, 1981, a similar high temperature trip of the Unit 3 Emergency Diesel Generator occurred. The cause of this trip is also believed to have resulted from insufficient cooling water flow to the diesel heat exchanger.
As a result of concerns raised about the operability of the diesel generator cooling water pumps, we have taken action to preclude recurr-ence of the diesel generator trips and to ensure that the pumps remain operable. Some of these actions have been detailed in Confirmatory Action Letters from your office on November 20, 1981, November 25, 1981, and December 2, 1981. As described in your December 2, 1981, 1cteer, the Unit 2/3 and the Unit 3 diesel cooling water pumps are presently operating continually, and all three cooling water pumps are being vented or inspected twice during each shift.
Operability of the Diesel Generator Cooling Water Pumps ,
We have conducted an extensive review of the operability of the Unit 2/3 and Unit 3 Diesel Generator Cooling Water Pumps. Our investi- .
gation has included the following:
- 1. Extensive testing of the pumps utilizing DOS 6600-11 (the diesel generator cooling water pump operability surveillance) and DOS 6600-1 (the diesel generator operability surveillance),
as well as special pump tests with different suction and discharge piping arrangements.
- 2. Review of the cooling water system piping and design. ,N [
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- 3. Review of the dicaal gensrator cooling watzr pump dssign and discussions with the pump manufacturer.
- 4. Review of testimony of the operators involved in these events.
1
- 5. Review of the diesel generator alarms received and printed on -
the computer alarm typer during the events.
l 6. Review of the diesel generator control and alarm system logic 1
and circuitry.
.The investigating team consisted of station personnel, personnel from our corporate Station Nuclear Engineering Department, and an out-side consultant. Based on our investigation, we conclude that the-Unit
- 2/3 and Unit 3 diesel generator high temperature trips resulted from re-stricted flow in the cooling water lines to the heat exchangers. The flow restriction resulted from failure of the discharge check valves in both the Unit 2/3 and Unic 3 cooling water pump discharge lines. In j both cases, the check valve disc had separated from the valve operating arm. This check valve disc causing the flow restriction is consistent with the tests performed and the observed behavior of the pumps. Both check valves have been replaced with new valves, and the similar valve for the Unit 2 diesel has also been replaced.- We are revising the diesel preventative maintenance procedures to require that these check j valves be inspected annually and replaced or repaired as required.
Further, we conclude that the diesel generator cooling water pumps were operable and did operate normally during the.0ctober and November
- events. The pumps have been operable throughout the period of our in-ves tigation. None of our testing has shown any indication of pump ab-normal behavior.
Instrumentation The results of our investigation indicated that two significant problems exist in determMug pump operability and in troubleshooting potential cooling water pump malfunctions.
At the heat exchangers in the Diesel Generator rooms, personnel are hampered in determining that the heat exchangers are receiving proper flow because of inadequate instrumentation. Pump running lights are installed in the diesel generator room, which are operated by. contacts at the pump breaker, to provide one indication of proper pump operation. However, the operators must infer pump flow from readings of cooling water pressure at the inlet and outlet of the heat exchangers. These pressure readings are indicated on gages which have a range of 0-200 psig. However, because the pressure drop across the heat exchanger is less than two psi, and because of vibrations at the heat exchangers, the installed gages provide l an unreliable indication of cooling water flow. We have concluded that a more accurate indication of flow should be installed, and we have initiated an engineering study to design and provide that instru-mentation. Currently, we believe that pressure gages with a narrower range, combined with temperature indication across the heat exchanger, should resolve this deficiency.
l l
b
Wa have clzo daterminrd th:t tha prazent pump discharga gtga piping and arrangement can result in unreliable readingo, or readings not in-dicative of the actual pump discharge conditions. Because these are canned rotor pumps, there are no local indications other than pump discharge pressure that the pumps are actually operating. The cooling water pump discharge pressure gage is installed on the line supplying lubricating water to the pump motor bearings. (See Sketch on page 6).
a During testing of the Unit 2/3 diesel cooling water pump, the following was observed:
- 1. The discharge pressure gage read 30 psig with the vent valve closed, "Y" strainer blowdown valve closed and the remaining two valves full open.
- 2. Upon opening the "Y" strainer blewdown valve, the discharge pressure gage reading decreased to zero.
The above test was then repeated on the Unit 3 diesel generator cooling water pumps. The discharge pressure gage reading decreased 25 psig (50 psig to 25 psig) when the strainer blowdown valve was opened. Thus, opening the vent and blowdown valves dramatically lowers the " indicated" pump discharge pressure, and can mislead an operator about the actual (higher) pump discharge pressure. We be-lieve this phenomena resulted in the " apparent" low pump discharge pressuras reported by the operators during the October events. We
.have added an additional discharge pressure gage directly off the dis- '
charge volute of all the diesel generator cooling water pumps to pro-vide an accurate indication of pump discharge pressure. (See sketch)
Also reported during these events was a low pressure stream of water while venting the pump. Subsequent tests showed that when vent-ing the pump with both the vent valve and the strainer blowdown cpen that the stream of water is only slightly greater when a pump is running. The observation of low pump noise during these events was proved to be consistent with flow restriction by subsequent tests which indicated that pump is actually quieter with the discharge valve closed than with that valve open.
, The review of the November 19 event has indicated that the same condi-tions were present as those that had occurred on October 23 with one exception.
A reported air / water mixture from the pump vent is now believed, based on subsequent tests, to be an atomizing effect that can occur only by par-tially opening the vent valve (gate valve) . We believe the air / water mixture which the operator reported as being observed was caused by this penomena.
Other Items Investigated As a result of the reported pump low discharge pressure during the October events, we suspected that the suction piping to the diesel generator cooling water pumps might have been blocked by debris or other material, or that the pumps may have become airbound during maintenance operations on the circulating water pumps which required dewatering the 3B suction bay. Also considered was the possibility
[. . .
~
$ of a pump runout condition. As a racult, we did ths following:
1.- Pumps were vented daily - no signs of air.
- 2. Checked for air in the suction piping using ultrasonic and X-ray techniques - no indications of air.
- 3. Injected air into the suction of the Unit 3 cooling water pump - were unable to airbind the pump.
- 4. Inspected the cooling water side of the diesel generator heat exchangers for debris and foreign material - no evi-dance of foreign material that might have blocked _the cooling water pump suction lines.
- 5. Opened another suction line to provide redundant suction lines to the Unit 2/3 diesel generator cooling water pump and chained and locked all pump suction, discharge, and cross connect valves in their proper position. We are reviewing the procedures for dewatering and filling a circulating water pump bay to ensure air is not trapped in the lines or pumps as a result of these operations.
- 6. Based on the review by Station Nuclear Engineering Department and an outside consultant, it was determined that a' large flow and low discharge piping restriction condition would be necess-ary to cause pump runout - this condition was not observed dur-ing the events.
In addition, the following should be noted:
- 1. All three diesel generator cooling water pumps were_ operated successfully on October 5,1981. (Surveillance DOS 6600-11) _.
which was after dewatering suction bay 3B.
- 2. The diesel cooling water pumps have a suction head (positive pressure at the pump suction) rather than suction lif t and air inlaakage is unlikely.
- 3. Blockage of the suction would reduce the net positive suction head available to pump resulting in cavitation and noisy pump operation - this was not observed during the events.
Based on the above and our investigation, we conclude that air binding and/or suction piping blockage or pump runout were not contrib-uting factors to the October and November events.
We also evaluated the possibility of a locked rotor. In this case, the pumps would trip on thermal overload and manually resetting at the motor control center would be required. This was not experienced during these events.
All parts of the electrical system related to the operation of the cooling water pumps have been checked and/or tested with no abnormalties -
noted.
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~
Conclustons We believe that the cause of the diesel generator trips in October and November was flow blockage by the disc of the cooling water pump discharge check valves. As described above, the conflicting observations to a check valve failure have been erniained. The apparent spurious starts and stops are now believed to have been either operator manual starts and stops or as an expected result of resetting the diesel generator high temperature. Therefore, the check valve failure is consistent with all the observations made during the event. The discharge check valves on all three diesel generator cooling water pumps have now been replaced with new valvea. Our review furrher indicates that no other failures have occurred. We have, however, made some additional changes (Page 4, Item 5) to further ensure that the diesel generator cooling water pumps re tain operable, and we are providing additional instrumentation to assist the operators in troubleshooting any further problems.
Based on our investigation, we believe that the circumstances which account for the observed behavior during the October and November events with the Unit 2/3 and Unit 3 diesel generator cooling water pumps have been identified and explained, and that the probability of similar e-vents occurring has been significantly reduced. We feel that the con-ditions of your November 25, 1981, Confirmatory Action Letter have been satisfied. After concurrence by your office, we will return the oper-ation of the Unit 2/3 and Unit 3 diesel cooling pump to their normal standby condition, and we will resume normal surveillances of thair operability.
Very truly yours, O
D. 'J. Sco tt Station Superintendent Dresden Nuclear Power Station DJS/DLF/jrh cc: C. Reed F. Palmer J bel
. Farrar File /NRC File / Numerical
~.
4 Installed
\ Pressure Gage Vent X Strainer Discharge Check Valve X .
Strainer Bearing ,
X Blow Down Lube Valve v Water
\ Ne w Gage O
r 5 0 Stator N Cooling g N Jacket Suction O
+
e l-l 4
. _ _ . - __