ML20038C711

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Forwards LERs 81-046/03L-0,81-047/03L-0 & 81-049/03L-0
ML20038C711
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 12/02/1981
From: Clayton F
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20038C712 List:
References
NUDOCS 8112140064
Download: ML20038C711 (1)


Text

_

M iling Addr:ss 8

Alabama Power Company 600 North 18th Street Post Off.ce Box 2041 Birmingham. A:abama 35291 1!3 'IRC R EOi's N '

Te'ephone 205 783-6081

'NTA

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F. L. Clayton, Jr.

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Alabama Power 3; g g a8 40 ev s a vi m,u x s e m December 2, 1981

/;,4.~ \\, 's if Docket No. 50-364 F'./ '

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U. S. Nuclear Regulatory Commission

+,, g / O I3 l"o8 Office of Inspection and Enforc % c RQgp%gtog/A jQ I Region II y

s 101 Marietta Street, N.W.

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tat, eorgia 30303

Dear Sir:

Joseph M. Farley Nuclear Plant, Unit 2, Licensee Event Reports Nos.

LER 81-046/03L-0, LER 81-047/03L-0, LER 81-049/03L-0 are forwarded with three (3) copies of each, ir accordance with FNP Technical Specification 6.9 to provide thirty (30) days written notification of the occurrences.

If you have any questions, please advise.

Yours very tr IO

) 13,"h v >v/s i

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f.%. L. Clayton, Jr.

F FLCJr/KWti:nac Enclosures xc:

Director, IE (30 copies)

Director, MIPC (3 copies)

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CDyTROL BLOCCC: l l

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7 8 9 LICENSEE CODE 14 IS LICENSE NUVSEH 25 26 LICENSE TYPE JO 57 CAT 58 S$u'RC lL @l0 l5 l 0 l 0 l 0 l 3 l 6 l 4 hll l 1 10 I6 I 811 l@l1l21Ol218l1l@

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60 61 COCKET NUVSER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h 10121 l At 1517 on 11/6/81, it was determined that MP-0-STP-26.1 (control room ventilation l

lo l3 l l valve inservice test) had not been performed within the time interval specified by

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1 o 141 l Tech. Spec surveillance requirement 4.0.5.

Health / Safety of the public was not l

l o I s I l af fected.

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SYSTEM CAUSE CAUSE COMP.

VALVE CODE CODE SU8 CODE COVPON ENT CODE SU8 CODE SUSCODE ioisi 14141@ b.J@ L7J @ i z i z i z Iz Iz Iz l@ I z i@ I z l @

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9 10 11 12 13 18 19 20 SEQUENTI AL OCCURRENCE REPCRT REVISION

_ EVENT YE AR REPORT NO.

CODE TYPE NO.

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HOURS S8 IT FOR1 8.

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40 44 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h l i l o l lThis event was due to omission of the subiect valves from the Unit 2 inservice insnectinrl l plan which resulted in STP-26.1 being designated N/A for Unit 2 on the shared J

i i gig 7g [ surveillance schedule. STP-26.1 is on the schedule for Unit 1. b ut annlicable in modon l l,l3l l1, 2, 3 and 4 only.

The STP was not performed on the sche'duled date because Unit I was l 11 14I lin moda 5.

Immediatelv upon discoverv of the omission, WP-0-STP-26.1 war performed l

7 8 9

( At tachment) 80

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% POWER OTH ER STATUS BISCO RY DISCOVERY CESCRIPTION l1 15 l lE l@ l 1 l 0 l 0 l@l NA l

hl Surveillance Schedule Review l

ACTIVITY CO TENT RELEASED CF RELE ASE AVOUNT OF ACTIVITY LOCATICN OF RELEASE l1 l6l h

l NA l

l NA l

7 8 9 10 11 44 45 80 PERSONNEL EXPOSURES l 1 l 7 l l 0 l 0 l 0 lhdhlDESCRIPTIO'4 NUMBER TYPE NA l

,ERsoNNe't,N;uLS NUVBER DESCRIPTION li la l 1010 101@l NA I

7 8 9 11 12 80 LOSS OF OR DAYAGE TO FACillTY TYPE DESCRIPTION 1)bl dhl NA l

PuBt[TY 8112140085 811202 l 2 l a l l Nlhl ESCRtPTION @

PDR ADOCK 05000364 NRc WE ONW isSU E o C

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7 8 9 10 68 69 80 W. G. Hairston, III (205) 899-5156 NAME OF PREPARER PHONE.

LER 81-046/03L-0 CAUSE DESCRIPT1ui AND CORRECTIVE ACTIONS and successfully completed at 1604 on 11/6/81. The subj ect valves will be added to the Unit 2 Inservice Inspection Plan and the shared surveillance schedule will be changed to reflect the applicability of STP-26.1 to Unit 2.