ML20037B808
| ML20037B808 | |
| Person / Time | |
|---|---|
| Site: | Trojan File:Portland General Electric icon.png |
| Issue date: | 12/03/1980 |
| From: | Bair G PORTLAND GENERAL ELECTRIC CO. |
| To: | |
| Shared Package | |
| ML20037B807 | List: |
| References | |
| NUDOCS 8012150057 | |
| Download: ML20037B808 (4) | |
Text
OPERATING DATA REPORT DOCKET NO V - i +.
DATE I'
"4 COMPLITED S)
_t c
TELEPHONE e
OPERATINC ST ATUS i
J Notes
_.roian NoeIear Pla t l
T
- f. UrJi Name:
Neve-krr 19R1 L
. 2. EsprtW Puiod:
M11
- 3. Lice sed Thermal Power (Mht):
1216 f
- 4. Namepbre Rating (Cross MWel:
113d L
- 5. Dehs Dict 6cs! Ratm3 (Net MWe):
1?77 i
- 6. Muhm:: Dependable Capecity (Gross Mwe:
1050
[
- 7. Muhenc: Drpendable Capscity (Net MWe):
)-
- 8. W Cht,cs Occurin Capacity Rategs (lessas Nwnbee 3 Through 7)Since Last Report.Give Reanoas:
P i-
)f f
- 9. Poetr Level To whkh Rescieted. If Any (Net MWe):
f
- 10. Remru For Res:nctans.lf Any:
i i
' This Meeth YrAs-Dete Camulative l
7?0 so 0 37 ;g k
!!. Reen In Repenting Period 720 5714.3 22017.1
- 12. Nember Of Hoon Resctor was Cricks!
[{
- 13. Esactor Re:arve Shutdown Hours n
n 337;.o i
- 14. fleur3 Gmerator On4.ine 720
$621.7 212:9,t 0
0 tsog.7 f
- 15. Utdt Rear *e Shutdown Hows Id. Cre".s Thmas! Energy Genersted (MWH) 244_4274 1739335) ee2u%;
30E000 5645111 21630';6
- 17. Cren Electde:! Energy Generated (MWH) 76F218 sus 614 2019" is
- 18. Net Elervial Energy Generated (MWH) 100.0 69.9 s7.o it. Ur:lt Serne Factor 100.0 69.9 61.1
- 20. Unit Avaihbi!ity Factor 98.8 61.8 so.7
- 21. UrJi Capacity Feetor (Using MDC Nee) 96 4 s9.1
- s.s
- 23. Unit Capadty Factor (Uning DER Net) l
}~
- 23. Unit Forced Outage Rate O.0 10.8 6.,
i
- 24. Shvidown:5cheduled Over Next 6 Months (Type.Date. sad Dwsteoa of Eacht:
N P
fa line. Arril 1981. 45 days
- A h
NA
[
- 33. If Shut Down At End Of Repoet Period.Eubnated Date of Startus:
- 36. Unks to Ted Sutui t Prwe so Corrmercial Operativer.
Forecas Achieved t:
h M.
h N'
^
t* FIT 1AL CIIIT1CALITY
'IA NA INITIAL El.ECTRICITY f
COMMERCIAL OPER ATION u
n, c
l i _
1 N ')
lSff?i[00$F '
'I.)<.
p
s I-I AVER AGE D AILY UNIT POWER LEVEL i.
f DOCKETh0.
50-344 f
UNIT -Troj an i
DATE l-2-80
)
COMPLETED BY C. C. Bair
[
TELEPitONE sn1 s %-171 *)
g
. Ext. 234
- gg;7;;
Nave 'r-1080 5
FAY AVIP. ACE dan.Y POWER LEVEL DAY AYER ACE DAILY POWER LEVEL h,
(Mhchi)
(Mwe.w)
P.
fi 10'1 37 1074 t
{2
- 33 1075 10 0 I;)
1 DfM 3,
1076
.4 10'J 3g i1077 g ;
10 3 1075 33
- je 19/M 21 1079 i7 l 'L, 7 23 1079 f
r
- 8 10' 34 1079 ff 10R -
25 1076 l$
1073 3
1075 6,
(1 in11_
27 1074 f) 3 1076' 1074 l) in?$
39 1075 30 1075 k
in73 jg 1074 NA 33
..c
- p z is l
?
^'
Ol}
_ \\ 1_.
t'c NSTRUCTION$
...' :-.,u y, ;
~
k.ttis forms.la: the pvte:ge d*Dy unh pwwce kvelin MWe Net for each day 6n the rePewims meth. Compete w i
fhe rumt shde rne;2vatt.
k 2
\\p.
c I
Q.
1
,3
$[I73 r.
p s
w;
' b -< T *~ ~ '. ~ W.~ f '.'"~~' " '~~
~
}j,.
Wn 'c.fQidc%. e'-;'-
m@ ? ':* x y w: c a ; m r
- t, '
,g;m p,'qy &;p-n.-@ w% g;:..m: m:n @m,,,;p %,hp64~.wa7,
. "~, ; #.
e
?
' -~
n.m r
': -M'
~;
' ~.
. R-M-
.m
+
a.,
XS, ";K,h.t.w
'~ ~ EWWFSitVID0155 AND FCWDI REDUCT10NS. _
DOCKtT NO.
50-W*
T-UNIT NAME T rnj m o-e J
DATE _17-3-M 3
~
.. ? -
mumg M<rceeber 1980 i~^.
ggeC".ETED BY c
C-
- tr t
, : 4..%,.
+ ;,,
.. *.~v r:. -, tp :
TE1.!T110NE 5nt-s%- 1711 l
- %.]V. ' & ' 'y 4'
- " n- -
Q.,
est, 23s
~
I{:I%>&ND, Jh'W7-: u[n--.L %. x..[ c. n
>?'. r !
k
[,
U,9 7.
c
. ~
- s v.r,, -
.~
.,mv w.
..:f..s.%
. y q 3' "m-v 3-2 2:
e 4,
[ }. '
i)QY
'*5 AS: "Q
'rf TN. f* ' ! '4*
' i "-
m g g(
y
, pen,;.
- w.
yg
- f. ] g,e Event Fg 1-Ate.an sie j,';..,)
f" Cf og
- g Report e eVLa
" w Recorrence e
x n:
4
.s.
ec s
1 a.
l l,'t. 60.
'i.. C 40110 801808 O s
'O B
RA IIA NA IIA The power was reduced f roen 1001 to 75% power to allow the perforin.ince
- I' f
of the incore/F.xcore Calibratton
~'
Physica testing. The power was reduced for 16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br />.
j',
J
+
3 je 2
l t
ee!
'1.-
t 8
4 i
e,.
I
.2 3
4 F: Fored 5: Scheduled A Equipment Fattwo(Enyleen)
Methed:
Exhibit G. Instructhwis Reason:
I-Liscuss fo, r,epseatkm of Data
" B4faintenance of Test 2 Pf animal Setssa.
Entry Sheets for I.kemee
(
C-Refueling 3-Automatic Sceae.
Event Reput (f.ER) Fde (NUREG.
D-Regulatmy Restrictiese 40ber(Emplate) 01611 E-Operatoe Teanning A t.kasse Eme,amneten F-Admic:strative 5
GOperational Errue(Emplean) 19ff7)
Ilothet(Empfsin)
Exhibit I-Sauer 5.weet 1
[
D0CKET No:
50-344 DATE:
12-2-80 k,o 4
COMPl.ETED BY:
C. G.
Bair TELEPHONE:
503-556-3713 r
Ext. 2 34 SUN 9.ARY OF OPERATINC EXPERIENCC f
OPERATION:
L The plant operated the entire month at or near full power. The steam f
generator primary-to-secondary tube leakage ir. creased from about 20 gallons per day at the start of the month to about 45 gallons per day at the end of the month. The leakage is suspected to be in steam generators A and D.
M UCR SATETY RELATED MAINTENANCE:
Werk continued on improvement modifications to the Plant Security and Fire Protection System.
Work continued on modifications to the Control and Auxiliary Building walls to improve seismic integrity.
L Work continued on TMI-related codification work.
t 6
(
Ehe East emergency diesel-generator psriodic maintenance was completed on dr 11-23-80.
HISCEIMNEOl'S MAINTENANCE:
j The positive displace =ent charging pump periodic inspection and overhaul was coralet ed 11-25-80.
,t The A Residual Heat Removal pump was' investigated for its 3 mil vibration.
Discussions with the pucp vendor continue regarding the preferred torque
[
for the purp hold-down bolts.
The scheduled diesel fire pump psriodic maintenance inspection was completed P
on 11-13-80.
s Thk scheduled diesel auxiliary feedvater pump periodic maintenance inspection p
g was coupleted on 11-19-80.
L, Electrical inverter # 4 was tenporarily repaired with a replacement f
transformer.
h!
LICENSE CHANCES:
p u
g C
None
,r-MISCELLA.NEOUS:
I 1 *-
s 6.
7
$,1r U
.y., y >
s
'*f g
e'
- a.
p.
7 y
- e
+
E O
r
(
, ~.
3 g ~
- a i
~
mm
..