ML20036A294

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Forwards Response to NRC Re Violation Noted in Insp Rept 50-334/93-01.Corrective Actions:Operators Involved in Event Counseled on Need for Procedure Compliance & Unit 1 Operating Manual,Chapter 18, Solid Waste... Revised
ML20036A294
Person / Time
Site: Beaver Valley
Issue date: 04/30/1993
From: George Thomas
DUQUESNE LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NUDOCS 9305110057
Download: ML20036A294 (4)


Text

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,s Shippingport. PA 15077-0004 f 412) 393-5206 utz) s43-ama rAX

-April 30, 1993 i

GEORGE S. THOMAS Dtwisiom Vice President

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Nuckar Semmes

-r Nuclear Power Diveion i

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S. Nuclear Regulatory Commission i

Attn:

Document Control Desk Washington,.DC 20555

Subject:

Beaver Valley Power Station, Unit No. 1 Docket No. 50-334, License No. DPR-66 Inspection Report 50-334/93-01 In response to. NRC. correspondence dated March 26, 1993, and-in-

-accordance with 10 CFR 2.201, the attached reply addresses the: Notice of Violation transmitted with the subject' inspection report.

If there are any questions concerning this response, please-contact'Mr. K. L..Ostrowski at (412) 393-5104.

Sincerely,

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S. Thomas Attachment cc: Mr. L. W.

Rossbach, Sr. Resident Inspector Mr. T. T. Martin, NRC Region'I Administrator Mr. W. J. Lazarus, Chief, Reactor Projects Section No. 3B Division of Reactor Projects, Region I Mr.

G.

E.

Edison, Project. Manager 1

Mr.-M. L. Bowling (VEPCO) 1

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AFFIDAVIT 1

COMMONWEALTH OF PENNSYLVANIA)

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COUNTY OF BEAVER

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Subject:

Beaver Valley Power Station, Unit No. 1 BV-1 Docket No. 50-334, License No. DPR-66 Inspection Report 50-334/93-01 Before me,

the undersigned notary public, in and for the County.

and Commonwealth aforesaid, this day personally appeared George S.

Thomas, to me known, who being duly sworn according to law, deposes and-says that he is Division Vice President, Nuclear Services of the Nuclear Power Division, Duquesne Light Company, he is duly authorized.

to execute and file the foregoing submittal on behalf of said

Company, and the statements set forth in the submittal are true and correct to the best of his knowledge, information and belief.

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.*e S George S.

Thomas Subscribed and sworn to before me on this b

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DUQUESNE LIGHT COMPANY Nuclear Power Division Beaver Valley Power Station, Unit No. 1 Reply to Notice of Violation Combined Inspection Report 50-334/93-01 and 50-412/93-01 Letter dated March 26, 1993 VIOLATION (Severity Level IV; Supplement I)

Description of Violation (50-334/93-01-01)

Technical Specification 6.8.1.9 requires that written procedures be established, implemented and maintained, covering activities listed in Appendix A of Regulatory Guide 1.33, Revision 2, February 1978.

Operating Manual procedure 1.18.4.A,

" Flushing Resin from any Group I Ion Exchanger,"

Issue 2,

Revision 34, specifies that if the level change in the resin waste hold tank (ISW-TK-2), as indicated by level instrument LI-1SW-202, does not agree with the initial resin volume, then the resin transfer shall be repeated.

Contrary to the above, on January 21, 1993, operators flushed resin from deborating demineralizer 1CH-I-3A to the resin waste hold tank with an identified out-of-service resin waste hold tank level instrument (LI-1SW-202) and were unable to verify the level change in the resin waste hold tank.

Reason for the Violation:

The operators failed to properly implement procedure OM 1.18.4.A,

" Flushing Resin From Any Group I

Icn Exchanger to [1SW-TK-2]" by performing a

resin flush with LI-1SW-202 out-of-service.

The operators inappropriately relied on experience with previous resin

flushes, by observing pump discharge
pressure, to complete the evolution.

Corrective Action Taken:

The operators involved with the event were counseled on the need for procedure compliance.

The Unit 1

Operating

Manual, Chapter 18

" Solid Waste Disposal System,"

Section 4 Operating Procedures were reviewed, revised where appropriate, walked

down, and reissued on April 16, J993.

These procedures now refer to the use of the digital indication on LIS-ISW-202 to determine the level in the resin waste hold tank 1SW-TK-2.

l Maintenance Work Request No. 018321 was initiated on March 3,

1993, to have the malfunctioning analog meter LI-1SW-202 permanently l

removed from service.

e-Reply to Notice of Violation Inspect. ion Reports 50-334/93-01 and 50-412/93-01 Page 2 Action Taken to Prevent Recurrence:

The operations personnel involved with solid waste processing attended the refresher training module " Beaver Valley Site Procedure Compliance,"

to re-emphasize the importance of strict procedure compliance.

A Human Performance Enhancement System evaluation was completed on the activities which resulted in this violation.

The circumstances surrounding this violation will be reviewed in the Solid Waste / Process Control Program Module of the Radioactive Waste Shipping and Handling Retraining Course with emphasis on procedure compliance.

Date of Full Compliance:

The station is in full compliance at this time.

The Radioactive Waste Shipping and Handling Retraining Course will be completed by December 15, 1993.