ML20035E802

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Monthly Operating Repts for Mar 1993 for Jm Farley Nuclear Plant,Units 1 & 2
ML20035E802
Person / Time
Site: Farley  Southern Nuclear icon.png
Issue date: 03/31/1993
From: Hill R, Woodward J
SOUTHERN NUCLEAR OPERATING CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NUDOCS 9304190269
Download: ML20035E802 (9)


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Southem Noclear Operating Company Post Offce Box 1295 '.

Birmingham Alabama 35201

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Triephone 205 868-5086 j

SOuthem Nudear Operating Company J. D. woociard ce Ps gent

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April 13,1993 j

l Docket Nos. 50-348

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l 50-364 U. S. Nuclear Regulatory Commission i

ATTN: Document Control Desk I

Washington, D. C.

20555 Joseph M. Farley Nuclear Plant l

Unit I and 2 Monthly Operatina Data Reports Gentlemen:

Attached are the March 1993 Monthly Ope,ating Reports for Joseph M. Farley Nuclear Plant Units I and 2, as required by Section 6.9.1.10 of the-

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Technical Specifications.

If you have any questions, please advise.

I Respectfully submitted, l

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dM J.

. Woodard l

AEJ:edb3014 Attachrrents cc:

.Pr. S. D. Ebneter Mr. G. F. Maxwell Mr. G. F. L'under i

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I-930411PO269 930331

-PDR ADOCK 05000348 R

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1 JOSEPH M. FARLEY NUCLEAR PLANT UNIT 1 NARRATIVE

SUMMARY

OF OPERATIONS I

March 1993 l

At 0524 on 3-6-93, the unit was taken off line for a forced outage. The primary focus of the outage was to replace the #4 governor valve to the main turbine. The unit returned to 100 percent power at 1609 on 3-17-93.

There were no other unit shutdowns or major power reductions during the month

[

l of March.

The following major safety related maintenance was performed during the month:

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l 1.

Performed miscellaneous corrective and preventive maintenance on j

the diesel generators.

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2.

Replaced the #4 governor valve to the main turbine during the

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outage.

3.

Replaced the rotor in the #1 river water pump motor.

4.

Repaired the #2 Conoseal on the reactor head during the outage.

l 5.

Repaired the IB main steam atmospheric relief valvt during the outage.

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OPERATING DATA REPORT 4

00CKET NO.

50-3A8 DATE April 5. 1993 COMPLETED BY R. D. Hill TELEPHONE (205) 899-5156 OPERATING STATUS

1. Unit Name:

Joseph M. Farley - Unit 1 Notes

2. Reporting Period:

March 1993

1) Cumulative data since
3. Licensed Thermal Power (MWt):

2.652 12-1-77, date of

4. Nameplate Rating (Gross MWe):

860 commercial operation.

5. Design Electrical Rating (Net MWe):

829

6. Maximum Dependable Capacity (Gross MWe):

855.7 7 Maximum Dependable Capacity (Net MWe):

812.0

8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons: N/A
9. Power level To Which Restricted, If Any (Net MWe):

N/A

10. Reasons For Restrictions, If Any:

N/A This Month Yr-to-Date Cumulative

11. Hours In Reporting Period 744.0 2.160.0 134.400.0
12. Number Of Hours Reactor Was Critical 526.6 1.942.6 105.063.9
13. Reactor Reserve Shutdown Hours 0.0 0.0 3.650.0
14. Hours Generator On-Line 506.9 1.922.9 103.306.6
15. Unit Reserve Shutdown Hours 0.0 0.0 0.0
16. Gross Thermal Energy Generated (MWH) 1.293.223.7 4.997.395.7 264.998.471.5
17. Gross Electrical Energy Generated (MWH) 415.638,0 1.620.712.0 85.387.514.0
18. Net Electrical Energy Generated (MWH) 387.604.0 1.531.336.0 80.597.586.0
19. Unit Service Factor 68.1 89.0 76.9
20. Unit Availability Factor 68.1 89.0 76.9
21. Unit Capacity Factor (Using MDC Net) 64.2 87.3 73.6
22. Unit Capacity Factor (Using DER Net) 62.8 85.5 72.3
23. Unit Forced Outage Rate 31.9 11.0 6.. P
24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):

N/A

25. If Shut Down At End Of Report Period, Estimated Date of Startup: N/A
26. Units In Test Status (Prior to Commercial Operation):

Forecast Achieved INITIAL CP.ITICALITY 08/06/77 08/09/77 INITIAL ELECTRICITY 08/20/77 08/18/77 COMMERCIAL OPERATION 12/01/77 _ 12/01/77 DATARPT.01

DOCKET NO.

50-348 UNIT 1

DATE April 5. 1993 COMPLETED BY R. D. Hill TELEPHONE (205) 899-5156 MONTH March DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)

(MWe-Net) 1 823 17 595 2

820 18 809 3

792 19 813 4

819 20 818 5

819 21 816 6

92 22 815 7

0 23 813 8

0 24 816 9

0 25 817 10 0

26 825 11 0

27 818 12 0

28 817 13 0

29 816 14 0

30 815 15 0

31 810 16 224 INSTRUCTIONS On this format, list the average daily unit power level in MWe-Net for each day in the reporting month.

Compute to the nearest whole megawatt.

AVGDLY.PWR

UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO.

50-348 UNIT NAME J M. F*rity - Unit 1 DATE April 5.1993 _

COMPLETED BY R. D Hill REPORT MONTH: April TELEPHONE (205) 899-5156 ME%D OF UCENSEE CAUSE & CORRECTIVE DURATION

'dUTTif0 EVENT SYSTEM COMPONENT ACTION TO NO.

DATE TYPE' (HOURS)

REASON' 'DOWN REACTOR' REPORT #

CODE

  • CODE
  • PREVENT RECURRENCE 002 930306 F

237.1 A

1 N/A N/A N/A At 0524 on 3/6/93, the unit was taken off line for a forced outage.

The primary focus of the outage was to replace the #4 governor valve to the main turbine. The unit returned to 100 per:ent power on 3/17/93 at 1600.

1:

2:

3:

4; 5:

F: Forced Reason:

Method:

Exhibit G-Instructions for Exhibit I-Same Source S: Scheduled A - Equipment Failure (Explain) 1 - Manual Preparations for Data Entry 8 - Maintenance or Test 2 - Manual Scram.

Sheets for Licensee Event C Refueling 3 Automatic Scram.

Report (LER) File (NUREG4161)

D - Regulatory Restriction 4 Other (Explain)

E Operator Training & Ucensing Examination 5

F - Administrative G - Operational Error (Explain)

H - Other (Explain)

a, JOSEPH M. FARLEY NUCLEAR PLANT UNIT 2 NARRATIVE

SUMMARY

OF OPERATIONS March 1993 1

1 1

i At 1000 on 3-20-93, the unit was rauped down to 55 percent reactor power to perform maintenance on the 2B steam generator feedwater pump. The unit i

returned to 100 percent power at 0510 on 3-21-93.

There were no other unit shutdowns or major power reductions during the month of March.

The following major safety-related maintenance was performed during the month:

l 1.

Miscellaneous corrective and preventive maintenance was performed l

on the diesel generators.

2.

Eighteen tubes in the 2C component cooling water heat exchanger were plugged.

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OPERATING DATA REPORT DOCKET NO.

50-364 DATE April 5.1993 L

0 (b5 8 5156 i

l OPERATING STATUS j

1. Unit Name:

Joseoh M. Farley - Unit 2

'.htes

2. Reporting Period:

March 1993 1)Cualative data since

3. Licensed Thermal Power (MWt):

2.652 7-30-81, hte of j

4. Nameplate Rating (Gross MWe):

860 commercial operation i

5. Design Electrical Rating (Net MWe): 829
6. Maximum Dependable Capacity (Gross MWe):

863.6 l

4 1

7 Maximum Dependable Capacity (Net MWe):

822.0 t

5

8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, 2 -

Give Reasons:

N/A

9. Power Level To Which Restricted, If Any (Net MWe):

N/A

10. Reasons For Restrictions, If Any:

N/A l

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i This Month Yr-to-Date Cumulative i

11. Hours In Reporting Period 744.0 2.160.0 102.313.0 i
12. Number Of Hours Reactor Was Critical 744.0 2.101.0 88.122.9 i

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13. Reactor Reserve Shutdown Hours 0.0 0.0 138.0 li. Hours Generator On-Line 744.0 1.906.0 86.822.7 i
15. Unit Reserve Shutdown Hours 0.0 0.0 0.0 l
16. Gross Thermal Energy Generated (MWH) 1.936.119.4 4.929.693.5 221.460.641.3 l
17. Gross Electrical Energy Generated (MWH) 637.301.0 1.621.494.,0 72.633.672.0
18. Net Electrical Energy Generated (MWH) 606.995.0 1.536.918.0 68.876.116.0
19. Unit Service Factor 100.0 88.2 84.9 i
20. Unit Availability Factor 100.0 88.2 84.9

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21. Unit Capacity Factor (Using MDC Net) 99.3 86.6 82.1

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22. Unit Capacity Factor (Using DER Net) 98.4 85.8 81.2
23. Unit Forced Outage Rate 0.0 11.8 4.3
24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):

Refuelino/ Maintenance Outaae September 24. 1993 Approximately 60 days

25. If Shut Down At End Of Report Period, Estimated Date of Startup: N/A
26. Units In Test Status (Prior to Commercial Operation):

Forecast Achieved INITIAL CRITICALITY 05/06/81 05/08/81 INITIAL ELECTRICITY 05/24/81 05/25/81 COMMERCIAL OPERATION 08/01/81 07/30/81 DATARPT.U2

i DOCKET NO.

50-364

.j UNIT.

2 i

DATE April 5. 1993 i

COMPLETED 8Y R. D. Hill TELEPHONE 1205)'899-5156

'i i

I MONTH March DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)

(MWe-Net) 1 827 17 824 l

t 2

824 18 827 i

3 823 19 828 4

824 20 622 i

5 826 21 776 i

6 827 22 818 7

827 23 817 8

825 24 821 9

823 25 822 10 823 26 820-l 11 827 27 824 12 827 28 822 i

l 13 827 29 823

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14 826 30 824 15 826 31 816 f

i 16 82t.

INSTRUCTIONS On this format, list the average daily unit power level in MWe-Net for each day in the reporting month.

Compute to the nearest whole megawatt.

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AVGDLY.PWR

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UNIT SHUTDOWNS AND POWER REDUCTIONS

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DOCKET NO.

50-364 UNIT NAME J M Fartov - Unit 2 DATE Aoni5.1993 COMPLETED BY R. D Hill REPORT MONTH: kiril TELEPHONE (205) 899-5156 METHOD OF LICENSEE

. CAUSE & CORRECTrn DURATION SHUTTING EVENT SYSTEM COMPONENT ACTION TO NO.

DATE TYPE' (HOURS)

REASON' DOWN REACTOR' REPORT #

CODE

  • CODE
  • PREVENT RECURRENCE 002 930320 F

19.2 A

N/A

.N/A N/A N/A At 1000 on 3-20 93, the unit was ramped down to $5 percent reactor power to perform maintenance on the 28 steam generator feedwater pump. The j

unit returned to 100 percent power at 0510 on 3-21-93.

6 9:

2.

3.

4:

5:

F: Forced Reason:

Metnod:

Exhibit G-Instructions for Exhibit 1 Same Source S. Scheduled A Equipment Faiiure (Explain) 1 - Manual Preparations for Data Entry B - Maintenance or Test 2 Manual Scram.

Sheets for Ucensee Event C Refueling 3 - Automatic Scram.

Repcrt (LER) File (NUREG4161)

D - Raoulatory Restriction 4 - Other (Explain)

E Ope.o or Training & Ucer: sing Examination F Administrative G - Operational Error (Exp;a.n)

H - O her (Explain)

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