ML20034A595

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Monthly Operating Repts for Mar 1990 for Susquehanna Steam Electric Station
ML20034A595
Person / Time
Site: Susquehanna  Talen Energy icon.png
Issue date: 03/31/1990
From: Keiser H, Keith Young
PENNSYLVANIA POWER & LIGHT CO.
To: Mcdonald W
NRC
References
NUDOCS 9004230551
Download: ML20034A595 (10)


Text

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PPal P0nnsylvania Power & Light Compcny-Two North Ninth Street

  • Allentown, PA 18101
  • 215/7745151 Harold W Kelser e or i President Nuclear g

Technical Specifications Section 6.9.1.6 APR 161990 l

Mr. William G. Mcdonald Director, Office of Administration and Resources Management U.S.

Nuclear Regulatory Commission Washington, D.C.

20555 SUSQUEHANNA STEAM ELECTRIC STATION MONTHLY OPERATING REPORTS Docket Nos. 50-387/NPF-14 j

PLA-3381 FILE R41-2A and 50-388/NPF-22

Dear'Mr. Mcdonald:

The March 1990 monthly operating reports for Susquehanna SES' Units 1 and 2 are attached.

Very truly yours, l

L l

H.

W.

Keiser Attachment vn.newxm m-an~ w "iDeskzysyNy w wdinal')

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NRC Region I l

Mr. G.S. Barber, NRC Resident Inspector l

Mr. M.C. Thadani, NRC Project Manager 9004230551 900331 PDR ADOCK 05000387 R

PDC

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///

4 AVERAGE DAILY UNIT POWER LEVEL 3 838, %

1 I

DOCKET NO.

50-387 UNIT One L

J D

E O

DATE f

4-5-90 7

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g COMPLETED BY TELEPHONE (717)542-3251-a MONM March 1990

+

DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-NeO (MWo Neo i

1055 1042-g g7 1052 2

1naa

.18 3

1027 19 1osa 1043 4

20 933 1055 5

21 62 6

1099 513 22 7

1056 704 23 8

1055 24 i n9r, 9

1022 25 1053 10 994 26 1055 g3 1046 1055.

27 1041 1054-12 28 13 in1R 29 1055 14 1041 30 1019 15 1041 775-33 1038 16 INSRUC710NS On this format list the average daily unit power levelin MWe Net for each day in the reporting month. Compute o the nearest whole megawatt.

(9/77) s.

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. --.r. J OPERATING DATA REPORT '

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DOCKET NO.

50-387 DATE 4-5-90 kg 9

- COMPLETED BY Y A. Young. ;

TELEPHONE f7171542-3251 OPERATING STATUS

l. Unit Name:

Susquehanna Steam Electric Station Notes

2. Reporting Period:

March 1990 j

3. Licensed Thermal Power iMht s:

3293

4. Namepiste Rating (Gross MWel:

1152

5. Design Electrical Rating (Net MWel:

1050 j

6. Maximum Dependable Capacity (Gross MWe):

1069;3 l

.i

7. Maximum Dependable Capacity (Net MWel:

1032.7 i

8. If Changes Occur in Capacity Ratings (items Number 3 Through 7) Since Last Report, Gise Reasons:

No chances were made,

9. Power Level To Which Restricted. lf Any (Net MWe):

None

10. Reasons For Restrictions. If Any:

N/A This Month Yr..to.Date Cumulatise

11. Hours in Reporting Period 744 2160 59,737
12. Number Of Hours Reactor Was Critical 7d4

'1 M4 ?

45 4RR.5

13. Reactor Reserve Shutdown Hours 0^

0 1,032

14. Hours Generator On Line 732.3 1,908.7 44,510.1

!!. Unit Reserve Shutdown Hours 0

0 0

I.

16. Gross Thermal Energy Generated (MWH) 2.289.647 6.015.736 139.186,382
17. Gross Electrical Energy Generated (MWH) 751,378 1,980,114 45,43/,954
18. Net Electrical Energy Generated (MWH) 725,083 1,906,925 43,621,597
19. Unit Service Factor 98.4 88.4 74.5
20. Unit Availability Factor 98.4

_. 88.4 74.5

21. Unit Capacity Factor IUsing MDC Neti 94.4 85.5 70.7
22. Unit Capacity Factor (Using DER Neti 92.8 84.1 69.6
23. Unit Forced Outage Rate 1.6 11.6 9.6
24. Shutdowns Scheduled Over Next 6 Months iType, Date, and Duration of Eaeio:

4 Unit One is scheduled for its Fifth Refueling and Inspection Outage from 9-8-90 through 11-23-90.

.25. If Shut Down At End Of Report Period. Estimated Date of Startup:

26. Units in Test StatusiPrior to Commercial Operation):

Forecast Achiesed INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCI AL OPER ATION 1

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50-387 M

UNIT SHUIDOWNS AND POWER REDUC 110NS E

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s#4fC 8 REPORTMONTH arch 1970--

TELEPHONE (7171542-3251 M

copyLETED BY K.A. Youna j

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... 75 Licensee E-t Eg Cause & Corrective 5;

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i Unit One ecmenced manual shutdown 3

900321 F

11.7 B

1 N/A FK DISC at 1800 hours0.0208 days <br />0.5 hours <br />0.00298 weeks <br />6.849e-4 months <br /> March 20 and opened main generator output breaker at 0603 hours0.00698 days <br />0.168 hours <br />9.970238e-4 weeks <br />2.294415e-4 months <br /> March 21.

Reactor remaimd critical at low power level' during forced outage. Ebreed outage was required to make repairs to 230KV switchyard Generator #1 disconnects that were developing hot spots.

Repairs were made and Unit synchronize 1 to PJM grid at 1746 hours0.0202 days <br />0.485 hours <br />0.00289 weeks <br />6.64353e-4 months <br /> March 21.

Pom r ascension was held at 60%

level for 26 leurs while condenser tub 2 leaks were identified and repaired.

Unit One reacled 100% power at midnight March 23.

1 2

3 4

F: Forced Reason:

Method:

Exhibit G-Instructions S: Scheduled A Equipment Failure (Explain) 1-Manual for Preparati<m of Data B-Maintenance of Test 2-Manual Scram.

Entry Sheets for IAvnsee

- C-Refueling 3-Automatic Scram.

Event Report (LERI File iNUREG-

. D-Regulatory Restriction 4-Continuation 0161) '

E-Operator Training & Ucense Examination from previous month F-Administrative 5-Reduction Goperational Error (Explain)

. Exhibit 1 - Same Source i

19/77)

Ilother(Explain) 9-Other 4

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-M UNIT SHUTDOWNS AND POWER REDUCTIONS TNO.

50- E g

g UNIT NAME h

p DATE 1-5-96 4fc 8 REPORTMONTH March 1990 NTED W U-hung TELEPHDNE (717)542-3251

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E Licensee P,

Cause & Corrective No.

Date g

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Event p

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jgg Report a mO O

H Prevent Recurrence d

4 900331 S

0.0 B

5 N/A XX ZZZ Ccrvnencing at 2000 hours0.0231 days <br />0.556 hours <br />0.00331 weeks <br />7.61e-4 months <br /> March 30.

Unit One Reactor power was reduced to 60% for scheduled maintenarx:e outage. Control rod sequence exchanger was cunpleted and Unit returned to 100% power level at 0900 luurs April 1.

4 f

I 2

3 4

F: Forced Reason:

Method:

Exhibit G-Instructions 5: Scheduled A-Equipment Failure (Explain) 1-Manual for Preparation of Data B-Maintenance of Test 2-Manual Scram.

Entry Sheets for Licensee C Refueling 3-Automatic Scram.

Event Report (LE RI File INUREG-D-Regulatory Restriction 4-Continuation 0161)

E-Operator Training & License Examination from previous month F-Administrative 5-Reduction 5

' G-Operational Error (Explain)

Exlubit I - Same Source N/77)

Il-Other (Explain) 9-Other

.. _ _.. _ _ = _. _ _

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4 AYERAGE DAILY UNIT POWER LEVEL E

.yyyy DOCKET NO.

50-388 t =9 ki Two g

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4-5-90

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DATE -

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p gg J717)S42-3251 March 1990 m

DAY AYERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe Net) iWWe Net) -

3 10sf; M

37 i

2 1056 13 1055

[

3 1057 3,

1056 4

insn 1057 20 s

1 n; 7 1057 7

21 6

1058 1054 22 7

1058

.995 1058 8

1002 24 1057 105f 10 26 1056 Ii 1050

'1055 1046 12 1056 28 13 1043 1055-3 14 1043 30 1055 1043 15 3

1053 16 1041 INSTRUCTIONS On this format, list the average daily unit power levelin MWe Net for each day in the repomng month. Compute to the nearest whole rnegawatt.

(0/77 ) -

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~kJ OPERATING DATA REPORT l

DOCKET NO. 50-388

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k DATE 4-5-90 J

    1. fC rp COMPLETED BY K.A.

Young

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TELEPHONE (7171542 -3251 '

.r OPERATING STATUS

- Unit Two 1, Unit Name: Susquehanna Steam Electric Station Notes

2. Reporting Penod:

Mare'h 144A j-

3. Licensed Thermal Power (MWel:

3293

4. Nameplate Rating (Gross MWel:

1152 3.-

$. Design Electrical Ratin5 INet MWel:

1050

6. Maximum Dependable Capacity (Gross MWel:

1074.6

7. Maximum Dependable Capacity (Net MWeI:

1038.2 t

8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report. Give Reasons:

No chances were made.

9. Power Level To which Restricted,if Any (Net MWe):

None

10. Reasons For Restrictions,if Any:

N/A This Month Yr..to Date Cumulatise

11. Hours in Reporting Period 744
2,160 44,976
12. Number Of Hours Reactor Was Critical iaa 2.011.3

'36,676.6

13. Reactor Reserve Shutdown Hours 0

0 717.9

14. Hours Generator On Line 744 1,992 35,887.3 1
15. Unit Reserve Shutdown Hours 0

0 0

16. Gross Thermal Energy Generated (MWH) 2,445,719 6,478,298 113,286,273'
17. Gross Electrical Energy Generated (MWH) 808,952 2,142,798-

'37,130,711

18. Net Electrical Energy Generated (MWH) 781,057 2,064,821 35,725,502-
19. Unit Service Factor 100 92.2 79.8
20. Unit Availability Factor 100 92.2 79.8
21. Unit Capacity Factor (Using MDC Nett 101.2 92.1 76.5
22. Unit Capacity Factor (Using DER Net) 100 91.0 75.7
23. Unit Forced Outage Rate 0

'7.P 6.7

24. Shutdowns Scheduled Over Next 6 Months iType. Date. and Duration of Eneh e None scheduled.
25. If Shut Down At End Of Report Period. Estimated Date of Startup:
26. Units In Test Status (Prior to Commercial Operation):

Forecast Achiesed INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION 1

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Wd LEMT$NUTDOWM5 ANDFUWER REDUCTIONS N-g inwTmmE WO Dnis 4-s-on 6 gy Y_A_

Ynirwy REFORT MONTW March 1990 1EE.ErgeoNE (717) 542-3251 t

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No regort required for this nonth.

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4 F: Forced Reason:

Method:

Ed@lt G. Insermetions S: Scheduled A-Em,__.: Faihme(Explain) 1-Menesi

&n % seism of Does B temineenance of Test FRennest scrass.

- Esey spets For IAcesee C-Refueling 4-Continuation 986f1 3-Ameommeic Screm.

Ewas Report (LERI File tMfREG-D-Regeistory Rewrictium E-Operefor T;,mwig a txenee Examiesiem front previous month F-Adwesuwretive Reduction 5

G-Operational Error (Explain)

Esh3Mt 6 -Same 5.wece (9/77)

HOsher (Explain) 9-Other 4

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M SUSQtEHANta STDM ELBCTRIC STATIO4 '

Docket Ntuber 50-388 Date March 1990 omnpleted By X. A. Young Teleph:me (717)S42-3251 il Qa11enges to Main Steam Safety Relief Valves None Changes to t}u offsite Ibse Calculation Manual None Major ChangesLto Radioactive Waste Treatment Systems None

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Docket Ntaber 50-387-

Date March,1990 Ctmpleted by K. A. Young Teleghone (717) 542-3251 '

i Challenpa to Main Steam Safety Relief Valves -

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Changes to the Offsite Dose Calculation Manual.

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.t Major Changes to Radioactive Waste Treatment' Systemsi

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