ML20033A244

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Quarterly Rept for Jul-Sept 1981
ML20033A244
Person / Time
Site: West Valley Demonstration Project
Issue date: 09/30/1981
From: Duckworth J
NUCLEAR FUEL SERVICES, INC.
To:
Shared Package
ML20033A241 List:
References
19849, NUDOCS 8111250022
Download: ML20033A244 (12)


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1 NUCLEAR FUEL SERVICES, INC.

WEST VALLEY REPROCESSING PLAtlT QUARTERLY REPORT FOR JULY 1, 1981 THROUGH SEPTEMBER 30, 1981 1

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i J. P. DUCKWORTH

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GEtiERAL fW AGER NUCLEAR FUEL SERVICES, INC.

P. O. BOX 124 WEST VALLEY,f4EW YORY, 14171 l

l 8111250022 811022 PDR ADOCK 05000201 R

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TABLE OF C0tlTErlTS EflVIRONfIEtiTAL i10:1ITORING LOW LEVEL LIQUID EFFLUEtiTS GASEOUS EFFLUErlTS SURVEILLANCE TESTS LOW LEVEL LIQUID WASTE TREATf1EflT PLAtlT PERFORMA!lCE TABLE 1 LIQUID EFFLUEftTS - 1981 TABLE 2 GASEOUS EFFLUEflTS - 1981 TABLE 3 SURVEILLAiCE TESTS TABLE 4 FILTER REPLACEMEtiT PROCESSING Sui 0tARY NUCLEAR FUEL SUf4 MARY TABLE 5 NUCLEAR FUEL STATUS - JUNE 30, 1981 RADI0 ACTIVE WASTE FACILITY FERFORMA! ICE AND MODIFICATI0flS

ENVIRONMENTAL l'ONITORING As a result of chances in Technical Snecifications, sampling milk for 1311 was dis-continued on September 21, 1973.

Thirty-nine (39) samales were obtained durina the third ouarter from the perimeter monitorino stations and were aralyzed for aloha and beta activity. The aloha activitv ranaed frcm 1.38 (10~16) to 7.28 '(10 15) uCi/ml for an average of 2.95 (10'16) uCi/m1'.

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The' beta activity ranged from 6.96 (10 15) to 9.85 (10~14) uCi/ml with an average of 3.73 (10'1") uCi/ml.

LOW LEVEL LIOUID EFFLUENTS The amounts of radioactivity in liouid discharced from the plant during this ceriod and their relationship to the maximum permissible concentration (MPC) in the Cattaraugus Creek are shown in Table 1.

G,ASEOUS EFFLUENTS The amcunt of particulate radicactivity discharged via the plant stack and the relationshio to the release limit in the Technical Specifications is shown in Table 2.

Chance 20 to the Technical Scecifications discor.tinued the recuirements of Krypton-85 and Iodine-131 monitoring while plant operations are suspended.

SURVEILLANCE TESTS During this period, tests were performeu in accordance with Section 6 of the Technical Speci fications.

The ccmpletion dates are shown in Tables 3 and 4 LOW LEVEL LIOUID WASTE TREATMENT PLANT PERFORMA"CE During this ceriod, the LLWT was in ooeration a total of 18 days and treated 1.7C8,0^9 gallons of water.

Fifty-five drums of concentrated sludge were removed each havino a radiation level of <10 mr/hr.

Decontamination of waste water continues to be cood.

All water discharced has been below 2.0 x 10 5 uCi Cs l37/ml. Average removal factors for this period are shown below.

AVERAGE REMOVAL FACTOR Isotoce Previous Quarter This Quarter Cs-137 96.8 97.9 Sr-90 99.9 Not Yet Available l

Ru-Rh-106 Below Detection Limits Below Detection Limits l

Gross Beta 90.8 91.7 l

A 150-gallon sulfuric acid day tank was installed on the first floor of the low level waste treatment facility.

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Table 1 LIQUID EFFLUENTS--1981 (Curies)

% MPC* fieasured 90 129 Month Gross a Gross e Tritium Sr I

In Cattarauaus Creek Jan 0.00004 0.178 681 0.0008 0.0006 1.66 Feb 0.00011 0.244 834 0.0015 0.0005 0.78 c

Mar 0.000001 0.00003 0.0006 0.00001 NR 1.68 Apr 0.00009 0.057 325 0.0006 0.0001 0.60 May 0.00017 0.123 1300 0.0009 0.0004 2.31 Jun 0.00007 0.033 295 0.0003 0.0001 0.97 c

Jul 0.000001 0.00003 0.0008 0.00001 NR 0.49 b

c Aug 0.000001 0.00003 0.0007 NA NR NA b

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Sep 0.000001 0.00003 0.0010 NA NR NA d

8 1981 0.00048 0.635 3435 0.0041 0.0017 1.22 a

7 90 analyses are not available MPC (S) = 1.0 (10 5)) uCi/ml when Sr90 analyses are included separately MPC (B) = 3.0 (10-uCi/ml when Sr MPC (2) = 5.0 (10 6) pCi/ml Not yet available cNot required; there were no lagoon 3 effluent releases for the month Release through July,1981

  • MPC through July, 1981

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Table 2 PARTICULATE GASEOUS EFFLlJE!!TS - 1981 Month Curies

% Monthiv Limit January

.00016 0.05 February

.00005 0.02 March

.00019 0.08 April

.00006 0.02 May

.00007 0.02 June

.00006 0.02 July

.00003 0.01 August

.00008 0.03 September

.00032 0.13 1981

.00102 0.043 l

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Table 3 SURVEILLANCE TESTS Comments Spec. #

Subject Comnleted This Quarter 6.1 Raschig Ring Tanks Tanks are to be scheduled criar to' next processica use 6.2 Sumo Alarns and Eductors XC-2 7-21, 8-11, 9-1, 9-22 Satisfactory XC-3 7-21, 8-11, 9-1, 9-22 Satisfactc:v PPC 7-21, 8-11, 9-1, 9-22 Satisfactor/

6.3 Waste Storace Tank Pan Instrumentation 8D-1, 8D-2 7-13, 8-3, 8-25, 9-15 Satisfactory 8D-3, 8D a 7-13, 8-3, 8-25, 9-15 Satisfactory _

6.4 Emergency Utility Ecuicment 30T-1 7-7 Satisfactcrv 31K-1 7-7 Satisfactory 32G-4 7-7 Satisfactcry 31G-2, 2A 8-12 Satisfactory 31K-2, 2A 8-12 Satisfactcry 32G-2A, 2B 8-12 Satisfacto ry Diesel Fuel 7-6, 7-13, 7-20, 7-27, 8-3, 8-10, 8-17, 8-24, 8-31, 9-7, 9-14, 9-21, 9-28 Satisfactory Propane Fuel 7-6, 7-13, 7-20, 7-30, 8-3, 8-10, 8-17, 8-24, 8-31, 9-8, 9-14, 9-21, 9-28 Satisfactcry 15K-10A 7-7, 9-4 Satisfactory 15F-21 7-7 Satisfactory 6.5 Fil ters 7-10, 7-17, 7-22, 7-27, 8-5, 8-13, 8-18, 8-26, 9 a, 9-15, 9-25 Satisfactory 6.6 Dilution Air Not required this period 6.7 Boric Acid Not required this period 6.8 Locking Out Not recuired this period ~

6.9 Water Activity Alarms 9-30 Satisfactory 6.10 Poisoned Dissolver Baskets Not required this period 6.11 Solvent Analysis Not required this period

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Table 4 FILTER REPLACEf'ErlT

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There were no filter replacements during this reporting period.

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I PROCESSING SU:tARy J

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During this period there was no processing of fuel.

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1

NUCLEAR FUEL

SUMMARY

The following information is based upon nuclear material accountability records and indicates the disposition of nuclear material in fuel at the 2

reprocessing plant.

A.

INVENTORY The total on-site inventory on September 30, 1981 was 166,759 kilograns of uranium and 1,033,065 grams of plutonium. An inventory description by source and material type is presented in Table 5.

B.

PECEIPTS AND SHIPMENTS During the quarter, there were no shipments or receipts of spent fuel assenblies at the West Valley site.

C.

MEASURED WASTE AND ADJUSTMENTS There were no losses of uranium or plutonium during the reportino period as reasured waste.

No adjustments for uranium and plutonium to NFS Lot 27A were required.

D.

LOSS ON DECAY During the prior period, there was a decrease of 1,767 grams of I

plutonium due to loss on decay of the Pu-241 isotope. A correction due to an earlier computational error reduced inventory an additional 1,201 grams, resulting in a total decrease of 3,033 grams to the nlutonium inventory.

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Table 5 NUCLEAR FUEL STATUS AS OF SEPTEMBER 30, 1981 Kilocrams Grams Total U U-235 U-233 Total Pu I.

INVENTORY (7/1/ 31)

NFS 3,271 8.01 306 Cresden-1 20,429 144.03 0.30 116,43d RGsE 46,156 722.48 284,769 Consumers 11,130 238.68 63,962 WEPC0 43,017 462.61 336,928 Jersey Central 42,756 463.42 233,699 TOTAL 166,759 2,039.23 0.30 1,036,098 II.

RECEIPTS (7/1/81-9/30/81)

No receipts during this period.

III.

REM 3V"LS (7/1/81-9/30/81)

A.

Measured Waste Lot 27A 0

0 0

0 B.

Adjustments Lot 27A (0)

(0) 0 (0)

C.

Loss on Cecay 0

0 0

3,033 TOTAL 0

0 0

3,033 l

IV.

INVENTORY (9/30/81) l NFS 3,271 8.01 306 l

Dresden-1 20,429 144.03 0.30 116,216 l

RG&E 46,156 722.48 283,042 Consumers 11,130 238.68 63,887 WEPC0 43,017 462.61 336,221 Jersey Central 42,756 a63.42 233,393 TOTAL 166,759 2,039.23 0.30 1,033,065 l

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T RADI0 ACTIVE WASTE A.

Solid Waste The radioactive plant waste buried during this quarter consisted of 906.27 cu. ft. containing 17.258 curies.

This material was buried in the NRC-licensed burial area.

B.

High Level Licuid Waste As of June 30, 1981, the high level storage tank 8D-2 contained 581,800 gallons of neutralized waste with an activit.v of 3,732 pCi Cs-137/ml and 28 uCi Cs-134/ml.

FACILITY PERFORMAtlCE AtlD MODIFICATI0flS This secticn describes:

1.0 Major Modifications 1.1 Installed a pH meter and probe in the FRS storage pool area to monitor the pH of the water in the storage ocol. The probe is located in the northwest corner of the storage cool.

The meter is located on the control panel board in the East Mechanical Operating Aisle.

1.2 Installed a 150-gallon sulfuric acid day tank on the first floor of the low level waste treatment plant.

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