ML20031E305

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/03L-0:on 810921,during Hot Shutdown,Safety Relief Valve Position Secondary Indicator Pressure Switches Found to Actuate Above Required Limit.Caused by Setpoint Drift. Switches Recalibr
ML20031E305
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 10/06/1981
From: Nix R
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20031E298 List:
References
NUDOCS 8110150358
Download: ML20031E305 (2)


Text

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60 61 DOCKET NUMSER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION ANo PROF ABLE CONSEQUENCES h.

10I21l With the plant in hot shutdown. 2B21'-N301E'.H and K. Safety Relief Valve l

Position Secondary Indicator Pressure Switches, were found to acttste at f

l0 i3i l l 014 l l 26,14.4 and 25.6 psig respectively.

Tech Specs Section 4.4-2, Item b, I

i O i s l' I requires' actuation at 20 +/-5'psig. Redundant secon'da'ry position indicator i

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1O is 1 I 2B21-R614 was operable.

plant operation or public health and safety was 1

not affected by this event. This is a repetitive event as last reported.

l l0l7]l on Reportable Occurrence Report'No.'50'-366/1979-009.

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CODE TYPE N O.

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switches were recalibrated then functionally tested successfully and I

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-returned to. service..

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NAME OF PREPARER PDR ADOCK 05000366 S

PDR

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LER No. :

50-366/1981-095 Licensee:

Georgia Power Company Facility:

Edwin I. Hatch Docket. No :, 50-366 s

Narrative Report for LER 50,366/1981-095.

With the plant in hot shutdown, 2B21-N301E, H and K, Safety Relief Valve Position Secondary Indicator Pressure switches, were found to actuata at

. psig.14.4. psig.and 25.6..psig. respecttvely... Tect). Specs.Saction.4..h2,..

Item b, requires actuation.at 20 +/-5 psig.

Redundant secondary position.

indicator, 2B21-R614, was operable. ' Plant operation or'the public's health a.nd~ safety. was not,a.ffec.ted. :This',is' a repetitive' event as.last reported, '

on Reportable Occ' rrence Report' Nb. 50-366/1979'009.

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  • u The cause of this event has been attributed'to setpoint drift. The switch'es' were recalibrated per HNP-2-5240, Static-0-Ring Pressure Switch Calibration, thek function'a'lly tested and returned to service.

Unit I uses the same type pressure switches for this application; however, a generic review revealed no inherent problems.

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