ML20029A453

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Monthly Operating Rept for Jan 1991 for Waterford 3 Steam Electric Station.W/910215 Ltr
ML20029A453
Person / Time
Site: Waterford Entergy icon.png
Issue date: 01/31/1991
From: Burski R, Cintolanzi P
ENTERGY OPERATIONS, INC.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
W3F1-91-0030, W3F1-91-30, NUDOCS 9102220174
Download: ML20029A453 (7)


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. W3F1-91-0030 -

A4. 05 QA February 15,'1991 .

_ U.S. Nuclear Regulatory Commission ATTN: Document Control Desk '

_ Washington,: D.C. 20555 -

Subject:

. Waterford 3 SES

. Docket No.' = 50-382-License No. NPF-38 ,

cMonthly Operating Report ,

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' Gentlemen:

. Enclosed is the subject monthly report which covers the operating statistics for

!!~- - the month of January,1991'. This report is submitted por Section 6.9.1.6 of L the Waterford 3 Technical Specifications for Facility Operating License No. NPF-

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-. Very truly yours,

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cR.F. Bur' ski- '

- Director, Nuclear Safety :

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Enclosure :

h- _ fcc: ' Messrs. JR.D. Martin, NRC Region-IV I

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_D!T!;*Wigginton*,*N RC-NRR+ -

- E.Li Blake ' _ _ 'i R.B. McGehee ?

. J.T.1Wheelock _(INPO Records Center) i

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NRC MO.NTHLY OPERATING REPORT

SUMMARY

0F OPERATIONS-WATERFORD 3 l JANUARY 1991 The unit operated at an average reactor power of 99.7% and experienced no  ;

shutdowns or'significant power reductions during the period.

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PRESSURIZER SAFETY VALVE FAILURES AND CHALLENGES .

'WATERFORD 3 During the~ month of January 1991, there were no pressurizer safety valve failures or challenges, i

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W310204B

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.0PERATING. DATA REPORT UNIT NAME: WATERFORD 3 CITY / STATE: KILLONA/LA DATE: FEBRUARY 1991

-OPERATING STATUS =

1. Docket: 50-382' Notes

=2. Reporting Period: JANUARY, 1991 l3. Utility

Contact:

PATRICK CENT 0LANZI

-Phone Number: (504) 739-6683 4.-Licensed-Thermal Power (HWt):-3390-

, 5. Nameplate Rating (Oross Hve): 1200 1 6. Design Electrical Rating (Net MWe): J104

7. Maximum Dependable l Capacity (Gross HWe): 1120 a J8'.IMaximum' Dependable Capacity (Net HWe): 1075 ,

-9. If Changes Occur in Capacity Ratings (Items Number 4 Through.8) Since 'Last Report, Give Reasons:

S10.<-. Power Level To Which Restricted, if Any'(Net MWe): NONE r

M ' c 11. Reasons'For Restrictions, If Any: N/A

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This Month Yr,-to-Date cumulative I

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i: ' 12 . LHours In Reporting Period -744 744 46,945

13. Number of Hours Reactor Was' Critical 744 744 38,836.7
14. Reactor Reserve ~ Shutdown Hours 1 0 - 1
15 ' - Hours Generator On-Line 744 744 38,252.0

.16. Unit Reserve Shutdown Hours 0 -W310204B

OPERATING DATA REPORT (Continued)

This Month Yr.-to-Date Cumulative

17. Gross Thermal Energy

_2,515,171 2,515,171 Generated (FMI) _

_ 125,143,964

18. Gross. Electrical Energy 833,680 833,680 Generated (MVd) 42,078,350
19. Net Electrical Energy 800,056 800,056 Generated (PMI) 40,074.573
20. ~ Unit Service Factor i 100.0 100.0 81.5
21. Unit Availability Factor 100.0 100.0 81.5
22. Unit Capacity Factor (Using MDC Net) 100.0 100.0 79.4
23. Unit Capacity Factor (Using DER Net) 97.4 97.4 ~ 77.3
24. Unit Forced Outage Rate 0 0 4.6
25. Unit Forced Outage IIours 0 0 1,859.5 26.

Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):

-Refueling, 3/15/91, 58 Days

-27.

28.

If Shut Down At End of Report Period, Estimated Date Of Startup:

Units In Test Status-(Prior to Commercial Operation):

a Forecast Achieved INITIAL CRITICALITY 3/4/85 INITIAL ELECTRICITY 3/18/85 COMMERCIAL OPERATION 9/24/85 W310204B

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AVERAGE DAILY UNIT POWER LEVEL i

DOCKET NO. 50-382 UNIT WATERFORD 3 DATE FEBRUARY 1991 COMPLETED BY PATRICK CEMTOLANZI TELEPfl0NE 504-739-6683 MONTil JANUARY, 1991 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) (MWe-Net) 1 1078 17 1076 2 1078 18 1034 3 7076 19 1075 4 1079 20 1078 5 1078 21 1076 6 1078 22 1077 7 1077 23 1077 8- 1077 24 1076 9 1079 25 1074 10 1078 26 1074 11 1077 27 1076 12 1078 28 1075 13 1077 29 1076 14 1077 30 _

1075 15 1077 31 1076 16 1078 INSTRUCTIONS On this format, list the average daily unit power level in MWe-Net for each day in the reporting month. Compute to the nearest whole megawatt.

W310204B

. UNIT SHUTDOWNS AND POWER' REDUCTIONS ~ ..

REPORT FOR JANUARY 1991 -

DOCKET NO 50-382 . '

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. UNIT NAME WATERFORD 3 ._,

DATE FEBRUARY 1991 -

COMPLETED BY' PATRICK CENTOLANZr TELEPHONE 504-739-6683 Method of Licensee Cause & Corrective Duration Shutting Event System Component Action.to No. 'Date Type l '(HOURS) REASON 2 Down Reactor 3 Report # Code 4 Codes Prevent Recurrence NONE 1 2' 3 F: Forced Reason: Method S: Scheduled A-Equipment Failure (Explain) 1-Manual B-Maintenance or Test 2-Manual Scran.

C-Refueling .

3-Automatic Scram.

D-Regulatory Restriction 4-Continuation 4 E-Operator Training & 5-Load Reduction IEEE Std. 805-1984 License Examination 9-Other 5 F-Administrative.. IEEE Std. 803A-1983 G-Operational Error-(Explain)

H-Other (Explain) i W310204B

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