HL-1183, Forwards Owners Data Rept for Inservice Insp Ei Hatch Nuclear Plant Unit 1 Feb-June 1990
| ML20028G844 | |
| Person / Time | |
|---|---|
| Site: | Hatch |
| Issue date: | 08/27/1990 |
| From: | Hairston W GEORGIA POWER CO. |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| Shared Package | |
| ML20028G845 | List: |
| References | |
| HL-1183, NUDOCS 9009050118 | |
| Download: ML20028G844 (3) | |
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l Goova Power company 333 Pcomont Avenue
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Attanta. Geor0,a 3030B letphano 404 526 3195 Wing Awen 40 inenest Cordor Parway Puut O' hee Du 1295 Bam,ngham. Aid.ama 3LP01 leiophone $35 868 65B1 V8('!Dif* V.nf4'.CfK SV'le m W. O. Hairston,111 Gentof Wcti Pretdeqt Noes Or>9 rat <ons HL-ll83 000748 i
August 27, 1990 U.S. Nuclear Regulatory Commission ATIN:
Document Control Desk Washington, D.C.
20555 J
PLANT HATCH - UNIT 1 NRC DOCKET 50-321
. OPERATING LICENSE DPR-57 INSERVICE INSPECTION ASSOCIATED WITH THE SPRING 1990 CONDENSER RETUBE/ REFUELING OUTAGE Gentlemen:
Pursuant to the requirements of Article IWA-6000 of the ASME Code, i
Section XI, enclosed for your review is the Owner's Data Report for Inservice Inspection (form NIS-1) for the inservice inspection activities conducted at Plant Hatch Unit I during the Spring 1990 condenser retube/ refueling outage.
The Owner's Data Report is included as.
Georgia Power Company (GPC) has performed several inspections not j
specifically required by ASME Code Section XI, on selected Class 1, 2, and 3 components.
The results of the Code and augmented inspections performed at Unit I are summarized below and reported in the Owner's Data Report, o Ultrasonic examinations of austenitic stainless steel piping welds in the primary coolant pressure boundary per Generic Letter 88-01 and NUREG-0313, Revision 2.
Results are discussed in the Enclosure under " Class 1 Examinations." A detailed report on flaw evaluations i
ud weld overlay designs was submitted to the NRC via letter dated June 29, 1990, o Ultrasonic examinations of seven (7) welds in the non-safety related portion of the reactor water cleanup (RWCU) piping were pe-formed per commitments to the NRC related to Generic Letter 88-01.
No reportable indications were detected.
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GeorgiaPowei A U.S. Nuclear Regulatory Commission August 27, 1990 Page Two o All twenty (20) jet pump hold down beams were replaced with beams made of itaproved material.
This new material is considered a permanent resolution of IGSCC in hold down beams by NUREG/0R-3052, and will eliminate the need to perform ultrasonic testing each outage.
Remote visual examinations were performed on twenty (20) jet pump inlet mixers.
Evidence of erosion was detected, but was deemed acceptable, o Ultrasonic thickness measurements were performed on selected components in the extraction steam and condensate /feedwater system piping per GPC's ongoing erosion / corrosion program, o Eddy current testing was performed on several feedwater heaters, the main generator stator water coolers, and the generator hydrogen
- coolers, o The core spray sparger and associated piping was visually examined per Cu11etin 80-13.
No reportable indications were detected, if you have any questions in this regard, please contact this office at any time.
Sincerely, J.A &
W. G. Hairston, 111 GXM/eb
Enclosure:
Owner's Data report for Inservice Inspection - Edwin 1. Hatch Nuclear Plant Unit 1 - February 1990 - June 1990.
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(See next page.)
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Geonylalbwer d l-U.S. Nuclear Regulatory Commission August 27, 1990 Page Three c:
Georaia Power Company Mr. H. C. Nix, General Manager - Nuclear Plant Mr. J. D. Heldt, Manager Engineering and Licensing - Hatch NORMS U.S. Nuclear Reaulatory Commission. Washinaton. D.C.
Mr. L. P. Crocker, Licensing Project Manager - Hatch U.S. Nuclear Reaulatory Commission. Reaion 11 Mr. S. D. Ebneter, Regional Administrator Senior Resident Inspector - Hatch j'
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