ML20028D047
ML20028D047 | |
Person / Time | |
---|---|
Site: | Washington Public Power Supply System |
Issue date: | 12/30/1982 |
From: | Root R WASHINGTON PUBLIC POWER SUPPLY SYSTEM |
To: | Sternberg D NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V) |
References | |
10CFR-050.55E, 10CFR-50.55E, GO1-82-0833, GO1-82-833, NUDOCS 8301140438 | |
Download: ML20028D047 (3) | |
Text
7 Dockr.,t Noa. 50-460/513 50.55 (c) . R; port p $'N ,
Washington Public Power Supply System .!
! P.O. Box 968. 3000 George Washington Way - Richtand, Washington 99352'fj l372-5000 ~ l
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December 30, 1982 9 pg O' 30 G01-82-0833 UC.' Cit y Nuclear Regulator Commission-Region V 1450 Maria Lane, Suite 210 Walnut Creek, California 94596 Attention: Mr. D. M. Sternberg Chief, Reactor Construction Projects Branch No. 1
Subject:
NUCLEAR' PROJECTS 1 AND 4 DOCKETS NOS. 50-460 AND 50-513 POTENTIALLY REPORTABLE CONDITION RCS ATTACHED PIPING
Reference:
1)- Telecon, TJ Houchins, Supply System to DF Kirsh, Region V, Nuclear Regulatory Commission
- 2) G01-80-380, DW Mazur to RH Engelken, Director, dated December 12, 1980
- 3) G01-81-198, DW Mazur to RH Faulkenberry, dated July 2, 1981
- 4) G01-81-331, DW Mazur to RH Faulkenberry, dated October 5, 1981 5).. G01-82-03, DW Mazur to RH Faulkenberry, dated January 6, 1982
- 6) G01-82-0118, RW Root to RH Faulkenberry, dated April 2,1982
- 7) G01-82-0414, DW Mazur to RH Faulkenberry, dated July 2,1982 In reference 1), the Supply System informed your office of a potentially reportable deficiency under 10 CFR 50.55(e) and references 2), 3), 4),
5), 6), and 7) were interim reports on the subject condition.
l Based on the current WNP-1 slowdown, it is still not possible to provide i a final completion date for the subject design analysis. Progress
! reports have changed very little based on the reduced level of effort being expended to complete the analysis verification and redesign. As a result the Supply System will provide the next interim report when the analysis verification is completed or not later than construction restart.
I 8301140438 821230 f n ~7 PDR ADOCK 05000460 7
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.D.M. Sternberg RCS Attached. Piping-Page 2 G01-82-0833 As per Reference 6, an ' update of Attachment A will not be provided unless there is a: change to it. Attachment- B will' be provided in each interim
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report. -
If you have any questions or desire further information, please advise.
A ,
R. W. Root Acting Program Director-RWR:LCO:kd Attachment cc: JP Laspa, Bechtel (861)
V. Mani, UE&C (897)
A Toth, NRC-V. Stello, Director of Inspection, NRC FDCC (899)
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! ATTACHENT 8 ' ,
, LOCA-ANCHOR DISPLACEMENT REANALYSIS t-PROGRESS' REPORT NO. 6 - 12/82 SYSTEM TOTAL % -REMARKS OF WORK
-COMPLETED:
MSS 75- -LAD reanalysis for these lines has been-completed and the pipe stresses and'sup-port loads for ' this load-case must be combined with other- load-cases and the
.results evaluated.
FWS 75 ' LAD reanalysis for these lines has been
& completed and the pipe stresses and sup--
FWA port loads for this load-case must be combined- with other load-cases and the results evaluated.
DHR- 100 Pipe stresses have increased; however, Drop Line they are within acceptable limits. Due to increased loads resulting from the dynamic reanalysis, four supports out of nine were found to be unacceptable and must be modified. Nozzle (B&W) loads have exceeded the limits.
CFS & 75 LAD reanalysis for these lines has been DHR (LiI) completed and the pipe stresses and sup-port loads for this load-case have been combined with other load-cases and the stresses have been found acceptable.
Supports are being checked for accep-tance. Nozzle (CF Tank Outlet) loads have been exceeded slight?y. B&W's acceptance is required.
MUS (HPI) 0 Time history data is required from 8&W.
Reanalysis has not started.
Instrument 20 Time history data has been received from Lines (10) B&W. Reanalysis has started.