ML20027E432

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Monthly Operating Rept for Feb 1981
ML20027E432
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 03/02/1981
From: Gillett W
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
Shared Package
ML20027E429 List:
References
NUDOCS 8211150235
Download: ML20027E432 (5)


Text

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'g OPER.AT:NC DATA RIPORT

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DCC* CIT NO. 50-315 DATI 3-2-81 COM?!.*TED ?.Y W.T. Gillett T t :MiCNg 616-m 6001 CPE?JTING STATUS Not:s Donald C. Cook 1

1. Uni:.v =e:

February

'.981

2. Reporting Pe:iod:

3250

3. L2==sedT1---1 ?cwer C,1W:):

1089

4. N== epi:te R d ;(Cro:s MW ):

1054

5. Design Elec=i=1 R::ia:(Nec MWe):

1080

6. Sf- : :u= Dependshte Capaci:7 (Grou MFe;:

~1044

7. afui=c:s Dep=d.:ble C:p: i:7 (Net MWe):

S. If Ch:=;:s Oc=tr in C:pacity R::!:.gs (It=..s Nu:n5:: 3 Threugh 7) Sinc Lu: Repor:. Che Reasons:

9. Power Level To Which Res=i.ed.If Any (Ne-MWe):
10. R= sons For R:s: ':.*cas.If A=y:

This 51onth Y ao. Data Cu==I::ive 672 1,416 54.024

11. Hours !s Repor:is: P=iod 672 1.290.1 40,811.1
12. Nc=h=r Cf Ecus T.==:er W:s Cri:f=I 463 0

-G-12 Rc:c:or R:se:ve Shu::iove..o =

a 672 1.780.4 10 A17 si

14. Ec=:s Ge==:::ce Cn.L12e 0

0 3?1

15. Uni: R:se:ve Shutdown Ho::=

2,176,463 4,070.703 113.297.709

16. Crcss The=:.1 I:=;y Cene=:ed (Mw!'.)
17. Cross Ele==i=!Iser:7 Cece::: d G.tWH1 727,710 __,

1,359,500 37,215,160 702 W 1,312.495 35,771,636 l

13. Ne: EIes::i=1I:: ;y Cen==:=d (MWE) 100 90.:4 76.9

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19. Uni: Sci = ?:c=r 100 90.4 76.9 F

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20. Uci: Aril:hi!I:7 :cror ltN..

88.8 68.3 l

21. Unit C:pscity 7:c:or (Usi=; MDC See) 913 R7.4 64 p
22. Ucis Caescity F:c:or (Using DER Net) 0 1.5 6.7
23. U=i For::d Oct;: Rat,
24. Shutdowns Scheduled Over Nec 5 Moe:hs IType. D:te.:nd Cc= tion of I:ch):

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5. !! Sh : Dowr At End of R:pr.:t ?=iod. Isti==:ed Date of Scz.-::p:

. 25. Units la Tes: S ::24 (P:ior io Ce====i:1 Oper::iocr:

Forec=st Achieved INITIA L CRIT;CA LITY

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INiTIA L I*.ICTR:C;W Cor.:.*.:IRC:.C. 0 ?I?.a 7:0N

  • Corrected for error in January 1981.

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8211150235 810311 1

PDR ADOCK 05000315 R

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AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.

50-315 UNIT 1

DATE 3-2-81 COMPLETED BY W.T. Gillett TELEPHONE 616-465-5901 MONTH February 1981 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWE-Net)

(MWe-Net) 1 1048 17 1047 2

1048 18

_1048 3

1048 19 1048 4

1050 20 104o 5

1049 21 Inas 6

1n49 22 inam 7

1035 23 1n49 8

104g 24 1050 9

1048 25 1018 10 1051 26 1049 11 1050 27 insn 12 10s1 28 in1A 13 Inso 29 14 1039 30 15 1049 31 1050 INSTRUCTIONS

_ On this format list the average daily unit power level in MWe-Net for each day in the reporting month. Ccmpute to the nearest whole megawatt.

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UNIT SilUTHOWNS AND POWER REDUCTIONS DOCKET NO. 50 - 315 UNIT NAhlE D.C. Cook - Unit 1 DATE 3-11-81 REPORT hlONTil February, 1981 COntPLETED HY B.A. Svensson T ELEPilONE (616) 465-5901 v.

.2 Elcensee

,E 4, Cause & Cenreclive g

3g

.gg12 livent gy n.'8 Atilon to No.

Date o

$6 if3 lleport di Ed U U

H Prevent itecingence 6

None There were no unit shutdown; or sig-nificant power reductions during the month.

The unit operated at a capac-ity factor of 100.2% (using MDC Net).

i 2

3 4

F: Finceal iteason:

klethoil:

lixhible G. Insernctions S: Scheiluleil A-l!<inipment Failme(Explain) l-blannal for Preparation of Data ll hlaintenance of Test 2.hf anual 5 cram.

linity Sheets fm 1.icensee C Reincling

.l. Automatic Scram.

liven Repini (1.l!R) File INultt!G.

D.Itegulatiny itestiiction 4-Other (Explain) 0161) li Operator Training & license lixaminailon F-Ailministrative 5

s G Operational Eirur (lixplain)

'lishibii i. Saine Somce I'l/77) 11 Other (lixplain)

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Docket No.:

50-315

~ Unit Name:

D. C. Cook Unit #1 Completed By:

D. R. Campbell Telephone:

(616) 465-5901 Date: March 10, 1981 Page:

1 of 1

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MONTHLY OPERATING ACTIVITIES - FEBRUARY, 1981 Highlights:

The Unit operated between 90 and 100% full power throughout the reporting period.

The pressurizer PORV's 151 and 152 have been isolated this entire period due to valves leaking through.

Total electrical generation for the month was 727,710 mw.

Equipment Derangements:

2/02/81 Radiation monitors R-11 an,d R-12 were out of service from 0820 to 1800 hours0.0208 days <br />0.5 hours <br />0.00298 weeks <br />6.849e-4 months <br />, to replace the pump.

2/26/81 R-15, the main turbine condensor, air ejector monitor i

was out of service from 1250 hours0.0145 days <br />0.347 hours <br />0.00207 weeks <br />4.75625e-4 months <br /> to 1445 hours0.0167 days <br />0.401 hours <br />0.00239 weeks <br />5.498225e-4 months <br /> to i

replace the G-M tube.

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m

r DOCKET N0.

50 - 315 UNIT NAME D. C. Cook - Unit No. 1 DATE 3-11-81 COMPLETED BY B. A. Svensson TELEPHONE (616) 465-5901 PAGE 1 of 1 MAJOR SAFETY-RELATED MAINTENANCE FEBRUARY,1981 M-1 The emergency leak-off line check valve for the west motor driven auxiliary feedpump, FW-160, leaked by. This resulted in pressurizing the suction piping when the east pump was tested. Cleaned valve in-ternals and had systems tested to verify proper performance.,

M-2 Auto vent to ESW aftercooler for CD diesel was leaking by.

Replaced ball float valve and gasket.

M-3 The reciprocating charging pump had stuffing box leaks.

Replaced all pump suction and discharge valves.

Repacked all five cylinders and installed new throat bushings. Also, replaced the plunger and packing parts in No. 1 cylinder.

The pump was tested to verify sat-isfactory performance.

C&I-l The containment pressure recorder was reading 2.5 psig low. The re-corder was found to be 1 psig low and was recalibrated.

Pressure transmitter, PPA-312, was also low and was recalibrated to restore correct indication to the containment pressure recorder.

C&I-2 Feedwater flow to transmitter, FFC-211, No. 1 steam generator had a leak in the high pressure side threaded tap. A defective tee fitting was repitced to eliminate leakage.

C&I-3 Unit 2 shutdown bank D, rod N-ll, was indicating 240 steps on the rod position indication system and 228 on the demand indication. After verifying the LVD transformer secondary voltages for all rods in SD bank D, the signal conditioning modules for rods N-ll and B-6 were adjusted to track the indications for these rods.

C&I-4 CFA-411, component cooling water flow to the east centrifugal charging pump would not indicate a flow change when the valve was adjusted.

The instrument lines were plugged and were blown down.

The instrument calibration was verified.and returned to normal operation.

C&I-5 Dual bistable,1 TB-412 D/G, A T/TAVG Protection Set 1 was found to be out of specification during performance of the surveillance test procedure.

The bistable was replaced and the new bistable was re-calibrated in accordance with procedure 1 THP 6030 IMP.094.

C&I-6 Critical Control Room power switched over to its emergency power supply.

Water leaking from an overhead ventilator on to the power supply circuit board had caused a fuse to blow. Other components on the board were checked and were found to be intact.

The power supply inverter was protected from water and returned to service.