ML20027A332

From kanterella
Jump to navigation Jump to search
RO#77-054/03X-1 on 771102:CRD H-5 Uncoupled During Functional Testing Caused by Unlatched Inner Filter & Abnormally Long Uncoupling Rod.Inner Filter Pull Test in Reassembly Procedure & Improved QA Coverage Incorporated
ML20027A332
Person / Time
Site: Dresden Constellation icon.png
Issue date: 10/27/1978
From: Wujciga J
COMMONWEALTH EDISON CO.
To:
Shared Package
ML17173A367 List:
References
NUDOCS 7811160125
Download: ML20027A332 (2)


Text

'

.........~...........', . . . . . . , . . .

~

. ~ . . ..

' ~775 ' ' UPDATE REPORT:

L!ChNSEE EVENT REPORT PREVIOUS REPORT DATE 12/2/7) l l (PLE ASE PRINT OR TYPE ALL REQUIRED INFORMATIONI CONTROL GLOJx. l 1

l l l 0

lh' '

11$8l@

i a liA l9l t i t. ! D'! R ! s 11@l 010 l-Lf1010-!0 L. cia.is; Oc;I 14 :S CE'.SE *.u'.'6EM l010 l- 10 !0 l@l_ 25 JG LICEP.SE 41 TYPE 11 JQ 11 $7 CAT 1!@l TON'T , . '

oi:i 3,'[0] l L @l 01 5l 010 } 012 l 3 64l 7 @l1 63 l1 l0 l2 l7 l7 @l1 l0RE8CRT EVENT OATE le 75 l2 l7 l7 l880l@

C ATE

$ oJ 68 COCKET NU'. 6 ge EVENT CESC.*LIPTION AND PRQ9 A6.'.5 CONSEOUENCES h ,

ai:] (During Unit 2 refueling outage, control rod drive"(CRD) H-5 overtraveled indicating .

d It was recoupled and coupling verified in ac- g o ,3 ; j ufcoupiih:t,uring -functional testing.

CRD uncoupling had minimal safety signficance since it l

! 3 i .: i [cordance with T.S.3.3.B.1.

This was the first uncoupling

o;3 [ occurred cniv when the rod war withdrawn to position. 48.

) of CRD H-5.' Several other CRD's have uncoupled in the past. Reportable occurrences: ;

[

y 7 i50-237/77-14, 15, 22 & 29; 50-237/76-68, 72.

I

~

10 l 80 CO*. P. VALVE C J5E CauSE SY S T E *.1 SUSCCOE SuBCOCE COMPONENT CODE SUSCCOE COCE CCOE

.oi9) j RlBj@ [AJ@ ;1 , 1.

[F j@ l C; Rj Dj Rl V[Ej@ y@ y@

10 - Ib 13 2 ~s

, ' s .*

REPCRT REVISION N

. 2CUENTl

  • L CCCUPPINCE ODE TYPE N C.

.CeTTEAR RtFORT NO.

f6 i y :,

n no
1. 7 ! 7! i_t 1,01 51 41 l -l l 0I 3I [x l ll l 1l 23 ;9 30 31 32 IP 22  ?; ~4 26 27 ATT ACHaa E N T NPRD4 PRIME COMP. COMPONENT 2L Th in g (=;ECT SHUT':O'.'.'N MANUFACTURER 1.C?'t1N
  • A E*. -C r;a?. ON AL,11.7 :A ETr'OD MOURS .2 stauiTTED PORMdV8. SL PP LI ER I1.j@l Z j@  ! Z!@ l Of O! O! Of f41 Yl@ [Y_j@ l43Nl@ lG l0 l8 l047l@

33 4 wa !J.we@ 31 40 42 44 OALSE CESCRIPTICN AND CL',4RECTIVE ACTICNS 2s g;g ] An unlatched inner filter and abnormally long uncoupling rod resulted in the uncoupling functional testing. Drive had been overhauled in Jan. 1975. .A pull; gg j of CRD H-5 durin::

.7,,) ; test en the inner filter has now been incorporated in the overhaul and reassembly l

,ri I il I procedure. Revised procedute and improved QA coverage believed to be adequate to

,a..,; prevent future similar events. 80 e c. is 5 4 C1L'TY

- METHODOF OTH E R STATUS DISCOVERY OtSCOVERY DESCRIPTION 34 t iv4 * ,POWE R Fthictional Testing l

7 i Hi@ l010 i 0 f(j~ i: 12 NA 44 l l45Bl@l^46 80 5 4 ; to t'

/. ,*ivtTY OCN Tsi4T UO 4MOJNT CF ACTIV' TY "3

  • LGCATION OF RELEASE i t.Z At! 3,*]F RELE Ar.E NA l t i c : ? Z i (2.;t iZl@l NA l l 45 80 -

44 s 3 :0 1 P3 ASC***.E L t A PC'.bR ES d

'du vo E p' j Q l . 0 l 0 lhj@l ESCRIPTICN

- TYPE D NA )' # ///4h/ M l

' 80

. 9 er is

. :i M'Z37'S PC'R3CNN!L INJURIE3 nU.m E s, :ESCniPTicN 42 l

W!

-W [0l 0 ' 016)l V,

NA 80 ms er :a see.:,oE c tr. cit.Tv Q3

-5  ::nmeTLw v NA' l l V ! >i [,__Zj@l 80 6 3 . .;

NRC USE ONLY ,

isueo"NESLn.PucN h/ lIII!!!ll11Ili 2l0ie :)I dI6'l to NA OS 69 83. h

..NA*,M QF PR@ PAR @R 6.

J. Wujciga __

pgang 465 ,{,

". 1"-

, =

ATTACHMENT TO LICENSEE EVENT REPORT 77-054 /03X-1 i

  • C0lt!ONWEALTH EDISON COMPANY (CWEl J-DRESDEN UNIT-2 (ILDRS-2) 3 DOCKET f/050-237 i
  1. During Unit 2 refueling outage, control rod drive (CRD H-5 overtraveled indicating uncoupling when withdrawn to posit'on'48 i during functional '

testing. CRD H-5 was recoupled and coupling verified in accordance with )

the requirements of T.S.3.3.B.I. CRD uncoupling had minimal safety sig- i '

nificance since it occurred only when the rod was withdrawn to position

48. This was the first uncoupling of CRD H-5.

( Five other CRD's had .

previously uncoupled since the 1975 Unit 2 refueling outage (reportable occurrences: 50-237/1977-14, 15, 22 & 29; 50-237/1976-68, 72).

On November 9, 1977 CRD H-5 was disassembled and inspected per Control Rod Drive Inspection and Maintenance Procedure DMP 209. To assure a -

comprehensive inspection a special operating procedure (SOP 216) was -

prepared and followed.

Upon inspection it was found that the inner filter was unlatched. In addition the distance between the CRD flange and the end of the fully seated uncoupling rod was abnormally long (173.406 + 0.562") . The abnormal length coupled with an unlatched inner filter resulted in the uncoupling of the CRD.

As part of the revised reassembly procedure, C.E.Co. Quality Control

^

personnel performed the inner filter installation and the reduced 20-30 pound pull test.

(- In Feb., 1978 the Control Rod Drive Inspection and Maintenance procedure DMP 209 was further changed to permit Maintenance l

Personnel to install the inner filter. This change occurred due to previously existing Management-Union work agreements. However, Quality Control Personnel will verify proper installation of the inner filter-and continue to conduct the 20-30 pound pull test. The. revised prohedure coupled with improved Quality Control coverage of CRD overhaul and reassem-bly are believed to be adequate to prevent future similar events.  ;

I 1

y Y* . .

5 , . . ,,

a

  • ___