RO#77-054/03X-1 on 771102:CRD H-5 Uncoupled During Functional Testing Caused by Unlatched Inner Filter & Abnormally Long Uncoupling Rod.Inner Filter Pull Test in Reassembly Procedure & Improved QA Coverage IncorporatedML20027A332 |
Person / Time |
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Site: |
Dresden |
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Issue date: |
10/27/1978 |
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From: |
Wujciga J COMMONWEALTH EDISON CO. |
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To: |
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Shared Package |
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ML17173A367 |
List: |
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References |
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NUDOCS 7811160125 |
Download: ML20027A332 (2) |
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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO
MONTHYEARML20027A3321978-10-27027 October 1978 RO#77-054/03X-1 on 771102:CRD H-5 Uncoupled During Functional Testing Caused by Unlatched Inner Filter & Abnormally Long Uncoupling Rod.Inner Filter Pull Test in Reassembly Procedure & Improved QA Coverage Incorporated ML19352A1171974-12-16016 December 1974 Ro:On 741213,during Refueling Outage Circumferential Cracks Found in Unit 2 Stainless Steel Loop B Bypass Line.Cause Not Stated.Corrective Action Being Reviewed ML20003C3781974-05-27027 May 1974 Ro:On 740527,diesel Generator 2/3 Declared Inoperable Due to Unstable Load & Machine Inability to Carry Full Load. Cause Not Stated.Required Surveillance & Investigation Initiated ML19352A1191972-09-29029 September 1972 Ro:On 720919,during Routine Calibr of Reactor Low Pressure Permissive Switches,Two Setpoints Drifted Above Tech Specs Value of 350 Psig.Switches Reset & Will Be Sent to Ctr of Trip Setting Span in Future 1978-10-27
[Table view] Category:LER)
MONTHYEARML20027A3321978-10-27027 October 1978 RO#77-054/03X-1 on 771102:CRD H-5 Uncoupled During Functional Testing Caused by Unlatched Inner Filter & Abnormally Long Uncoupling Rod.Inner Filter Pull Test in Reassembly Procedure & Improved QA Coverage Incorporated ML19352A1171974-12-16016 December 1974 Ro:On 741213,during Refueling Outage Circumferential Cracks Found in Unit 2 Stainless Steel Loop B Bypass Line.Cause Not Stated.Corrective Action Being Reviewed ML20003C3781974-05-27027 May 1974 Ro:On 740527,diesel Generator 2/3 Declared Inoperable Due to Unstable Load & Machine Inability to Carry Full Load. Cause Not Stated.Required Surveillance & Investigation Initiated ML19352A1191972-09-29029 September 1972 Ro:On 720919,during Routine Calibr of Reactor Low Pressure Permissive Switches,Two Setpoints Drifted Above Tech Specs Value of 350 Psig.Switches Reset & Will Be Sent to Ctr of Trip Setting Span in Future 1978-10-27
[Table view] Category:TEXT-SAFETY REPORT
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Policy of Second Checking All Capacitors Is Being Adopted ML20247F3391998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Dresden Nuclear Power Station,Units 1,2 & 3 ML20217D0281998-04-22022 April 1998 Part 21 Rept Re Additive Constants Used in MCPR Determination for Siemens ATRIUM-9B Fuel by Core Monitoring Sys Were Found to Be non-conservative.SPC Personnel Notified All Customers w/ATRIUM-9B Lead Test Assemblies ML20216D4411998-03-31031 March 1998 First Quarter Rept of Completed Changes,Tests & Experiments for 10CFR5059 ML20216C9651998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Dresden Nuclear Power Station,Units 1,2 & 3 ML20216E2531998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Dresden Nuclear Power Station ML20202F7831998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Dresden Nuclear Power Station ML20199K1651998-01-23023 January 1998 Rev 65h to Topical Rept CE-1-A, Comm Ed QA Tr ML20198P5321997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Dresden Nuclear Power Station ML20198P7021997-12-31031 December 1997 Fourth Quarter Rept of Completed Changes,Tests & Experiments Per 10CFR50.59 ML20216D3611997-12-31031 December 1997 Unicom Corp 1997 Summary Annual Rept ML20203F8781997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Dresden Nuclear Power Station ML20199B0701997-10-31031 October 1997 Monthly Operating Repts for Oct 1997 for Dresden Nuclear Power Station ML20217H7201997-09-30030 September 1997 Monthly Operating Repts for Sept 1997 for Dresden Nuclear Power Station,Units 1,2 & 3 ML20210V2401997-09-19019 September 1997 Rev 65g to Topical Rept CE-1-A, Comm Ed QA Manual ML20216J3781997-08-31031 August 1997 Monthly Operating Repts for Aug 1997 for DNPS ML20210H5511997-07-31031 July 1997 Monthly Operating Repts for July 1997 for DNPS IAW RG 1.16 & GL 97-02 1999-09-30
[Table view] |
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ai:] (During Unit 2 refueling outage, control rod drive"(CRD) H-5 overtraveled indicating .
d It was recoupled and coupling verified in ac- g o ,3 ; j ufcoupiih:t,uring -functional testing.
CRD uncoupling had minimal safety signficance since it l
! 3 i .: i [cordance with T.S.3.3.B.1.
This was the first uncoupling
- o;3 [ occurred cniv when the rod war withdrawn to position. 48.
) of CRD H-5.' Several other CRD's have uncoupled in the past. Reportable occurrences: ;
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y 7 i50-237/77-14, 15, 22 & 29; 50-237/76-68, 72.
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33 4 wa !J.we@ 31 40 42 44 OALSE CESCRIPTICN AND CL',4RECTIVE ACTICNS 2s g;g ] An unlatched inner filter and abnormally long uncoupling rod resulted in the uncoupling functional testing. Drive had been overhauled in Jan. 1975. .A pull; gg j of CRD H-5 durin::
.7,,) ; test en the inner filter has now been incorporated in the overhaul and reassembly l
,ri I il I procedure. Revised procedute and improved QA coverage believed to be adequate to
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ATTACHMENT TO LICENSEE EVENT REPORT 77-054 /03X-1 i
- C0lt!ONWEALTH EDISON COMPANY (CWEl J-DRESDEN UNIT-2 (ILDRS-2) 3 DOCKET f/050-237 i
- During Unit 2 refueling outage, control rod drive (CRD H-5 overtraveled indicating uncoupling when withdrawn to posit'on'48 i during functional '
testing. CRD H-5 was recoupled and coupling verified in accordance with )
the requirements of T.S.3.3.B.I. CRD uncoupling had minimal safety sig- i '
nificance since it occurred only when the rod was withdrawn to position
- 48. This was the first uncoupling of CRD H-5.
( Five other CRD's had .
previously uncoupled since the 1975 Unit 2 refueling outage (reportable occurrences: 50-237/1977-14, 15, 22 & 29; 50-237/1976-68, 72).
On November 9, 1977 CRD H-5 was disassembled and inspected per Control Rod Drive Inspection and Maintenance Procedure DMP 209. To assure a -
comprehensive inspection a special operating procedure (SOP 216) was -
prepared and followed.
Upon inspection it was found that the inner filter was unlatched. In addition the distance between the CRD flange and the end of the fully seated uncoupling rod was abnormally long (173.406 + 0.562") . The abnormal length coupled with an unlatched inner filter resulted in the uncoupling of the CRD.
As part of the revised reassembly procedure, C.E.Co. Quality Control
^
personnel performed the inner filter installation and the reduced 20-30 pound pull test.
(- In Feb., 1978 the Control Rod Drive Inspection and Maintenance procedure DMP 209 was further changed to permit Maintenance l
Personnel to install the inner filter. This change occurred due to previously existing Management-Union work agreements. However, Quality Control Personnel will verify proper installation of the inner filter-and continue to conduct the 20-30 pound pull test. The. revised prohedure coupled with improved Quality Control coverage of CRD overhaul and reassem-bly are believed to be adequate to prevent future similar events. ;
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