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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO
MONTHYEARML20045D9071993-06-24024 June 1993 Special Rept:From 930511-0611,7 Fire Detectors in Circuit FLP3-3 Out of Svc for 32 Days.Caused by Failed Fire Detector.Detector Replaced & Containment Air Temps Monitored Hourly ML20044G5371993-05-28028 May 1993 Rev to 910925,1231 & 930731 Special Repts,Correcting Administrative Error in Equipment Designation of Passive Triaxial Peak Accelerograph.All Other Info Remains Unchanged ML20024H3011991-05-22022 May 1991 Special Rept:On 910412,loose Parts Detection Sys Declared Inoperable Due to Repetitive Spurious Alarms & Inoperable pre-amplifier Unit.Loose Parts Monitoring Troubleshooting Currently Under Review ML20043F8251990-06-0808 June 1990 Special Rept:On 890425,gas Sample Drawn from PASS Indicated Reactor Gases Not Removed from Liquid Sample Rcs.Four RCS Liquid Samples Successfully Obtained & Two of 4 Samples Produced RCS Dissolved Gas Samples ML20042G8911990-05-0707 May 1990 Special Rept:On 900408,pressurizer Spray Valve Failed Open Causing Depressurization of Rcs.Caused by Equipment Malfunction.Feedback Arm Holding Screw on Pressurizer Spray Valves Replaced W/Longer Screws & Secured W/Locknuts ML20006C2141990-01-23023 January 1990 Special Rept:On 900102,radiation Monitor Removed from Svc & 7-day Time Allowed Exceeded During Calibr.Replacement Detector on Order Since Nov 1989 & Will Be Replaced & Recalibr ML20005G1281990-01-0202 January 1990 Supplemental Special Rept:On 890716,2 of 12 Loose Parts Monitor Channels Declared Inoperable When Monitors Alarmed Continuously.Caused by Malfunctions in Equipment Inside Containment Bldg.Replacement Scheduled for Next Outage ML19351C7341989-12-11011 December 1989 Special Rept:On 891110,turbine Electrical Trip Solenoid Valve Failed to Meet Surveillance Acceptance Criteria. Caused by Particulate Contamination in Secondary or Electronic Trip Valves.Valves Replaced W/Rebuilt Valves ML20024D0251983-07-15015 July 1983 Ro:On 830421,following Preliminary Manual Test Insertion (Mti)Test,Actuation Module Lights Came on Due to Module Energizing.Cause Unknown.Operators Stationed to Mitigate Problems or Actuation If Mti Required ML20052D7771982-04-29029 April 1982 Ro:On 820415,steam Generator 1 Increased Primary to Secondary Leakage Rate of 0.049 Gpm from Valve.Cause of Leak Rate Unknown.Increase Appears to Be Related to Plant Shutdowns/Trips Experience in Thermal Cycling ML20050A0081982-03-18018 March 1982 RO Re Steam Generator Tube Plugging as Specified in Tech Spec 4.4.5.1.4.Degradation Resulting in Tube Plugging Is Characterized by Localized Areas of Small Pits on Tube Outside Diameter.Investigation of Corrosion Cause Continues ML20040F6091982-01-29029 January 1982 RO:30-day Rept & 10-day Rept Per App B ETS Re Excessive Liquid Waste Discharge & Excessive Level of Radioactivity.Caused by Steam Generator Primary Side to Secondary Side Leakage.Doses within Bases for 2.5 Ci Limit ML20039E0401981-12-28028 December 1981 RO 50-336/81-41:discovered Abnormal Degradation of Reactor Coolant Sys Pressure Boundary,Specifically,Steam Generator Tubes.Frequency of Occurrence Primarily on Cold Leg Side. Two-wk Rept Will Be Submitted ML19350F1331981-06-17017 June 1981 RO 50-336/81-20:Dresser Industries Model 31739A Safety Valves Found to Have Less than Min Upstream Inside Diameter. Caused by Facility Design.Significant Impact Unlikely ML20004E3611981-06-0505 June 1981 RO 81-018/03L-0:insp of safety-related Pipe Hangers Inside Containment Containing Mechanical Snubbers Revealed Snubbers Installed on Small Diameter Piping.Caused by Listing Not Including Review of Diameter Piping ML20003B6491981-02-17017 February 1981 RO 50-336/81-8:as-built Hanger Review of Reactor Vessel Head Vent Piping Sys Determined Spring Can Type Hanger Was Installed Incorrectly,Resulting in Overstressing Socket Welded Joint.Spring Can Hanger Removed ML20002D6361981-01-13013 January 1981 Ro:On 801209,inservice Insp Revealed That Required Valve Operability Tests Not Performed During Third Calendar Quarter 1980.Valves Successfully Tested.Action Taken to Assure Timely Review of Valve Test Data ML19330C0201980-08-0101 August 1980 RO 80-26:water Seal for Piping Penetration in Refueling Water Storage Tank Pipe Tunnel Does Not Meet Design Requirements.Plugged Yard Storm Drain Caused Water Backup. Repairs to Water Seal Will Be Evaluated ML19323C3571980-05-0909 May 1980 RO 50-336/80-18:during Ongoing Hanger Base Plate Analysis Required by IE Bulletin 79-02,discovered That Several Svc Water Support Hangers Did Not Provide Factor of Safety Greater than Two.Repair Work on 12 Hangers Is Underway ML19294B6771980-01-23023 January 1980 Ro:On 791229,loss of Main Control Board Annunciators Occurred.Fourteen Power Supplies That Are Paralleled to Provide Voltages for Annunciator Electronics,Lamps & Field Contacts Failed.Surveillance Implemented ML19275A2751979-09-25025 September 1979 RO 50-336/79-27:during Engineering Review,Section of 4-inch Cast Iron Floor Drain Piping Passing Each Station Battery Was Found Not Supported in Accordance W/Design.Drain Working & Ductwork Removed 1993-06-24
[Table view] Category:LER)
MONTHYEARML20045D9071993-06-24024 June 1993 Special Rept:From 930511-0611,7 Fire Detectors in Circuit FLP3-3 Out of Svc for 32 Days.Caused by Failed Fire Detector.Detector Replaced & Containment Air Temps Monitored Hourly ML20044G5371993-05-28028 May 1993 Rev to 910925,1231 & 930731 Special Repts,Correcting Administrative Error in Equipment Designation of Passive Triaxial Peak Accelerograph.All Other Info Remains Unchanged ML20024H3011991-05-22022 May 1991 Special Rept:On 910412,loose Parts Detection Sys Declared Inoperable Due to Repetitive Spurious Alarms & Inoperable pre-amplifier Unit.Loose Parts Monitoring Troubleshooting Currently Under Review ML20043F8251990-06-0808 June 1990 Special Rept:On 890425,gas Sample Drawn from PASS Indicated Reactor Gases Not Removed from Liquid Sample Rcs.Four RCS Liquid Samples Successfully Obtained & Two of 4 Samples Produced RCS Dissolved Gas Samples ML20042G8911990-05-0707 May 1990 Special Rept:On 900408,pressurizer Spray Valve Failed Open Causing Depressurization of Rcs.Caused by Equipment Malfunction.Feedback Arm Holding Screw on Pressurizer Spray Valves Replaced W/Longer Screws & Secured W/Locknuts ML20006C2141990-01-23023 January 1990 Special Rept:On 900102,radiation Monitor Removed from Svc & 7-day Time Allowed Exceeded During Calibr.Replacement Detector on Order Since Nov 1989 & Will Be Replaced & Recalibr ML20005G1281990-01-0202 January 1990 Supplemental Special Rept:On 890716,2 of 12 Loose Parts Monitor Channels Declared Inoperable When Monitors Alarmed Continuously.Caused by Malfunctions in Equipment Inside Containment Bldg.Replacement Scheduled for Next Outage ML19351C7341989-12-11011 December 1989 Special Rept:On 891110,turbine Electrical Trip Solenoid Valve Failed to Meet Surveillance Acceptance Criteria. Caused by Particulate Contamination in Secondary or Electronic Trip Valves.Valves Replaced W/Rebuilt Valves ML20024D0251983-07-15015 July 1983 Ro:On 830421,following Preliminary Manual Test Insertion (Mti)Test,Actuation Module Lights Came on Due to Module Energizing.Cause Unknown.Operators Stationed to Mitigate Problems or Actuation If Mti Required ML20052D7771982-04-29029 April 1982 Ro:On 820415,steam Generator 1 Increased Primary to Secondary Leakage Rate of 0.049 Gpm from Valve.Cause of Leak Rate Unknown.Increase Appears to Be Related to Plant Shutdowns/Trips Experience in Thermal Cycling ML20050A0081982-03-18018 March 1982 RO Re Steam Generator Tube Plugging as Specified in Tech Spec 4.4.5.1.4.Degradation Resulting in Tube Plugging Is Characterized by Localized Areas of Small Pits on Tube Outside Diameter.Investigation of Corrosion Cause Continues ML20040F6091982-01-29029 January 1982 RO:30-day Rept & 10-day Rept Per App B ETS Re Excessive Liquid Waste Discharge & Excessive Level of Radioactivity.Caused by Steam Generator Primary Side to Secondary Side Leakage.Doses within Bases for 2.5 Ci Limit ML20039E0401981-12-28028 December 1981 RO 50-336/81-41:discovered Abnormal Degradation of Reactor Coolant Sys Pressure Boundary,Specifically,Steam Generator Tubes.Frequency of Occurrence Primarily on Cold Leg Side. Two-wk Rept Will Be Submitted ML19350F1331981-06-17017 June 1981 RO 50-336/81-20:Dresser Industries Model 31739A Safety Valves Found to Have Less than Min Upstream Inside Diameter. Caused by Facility Design.Significant Impact Unlikely ML20004E3611981-06-0505 June 1981 RO 81-018/03L-0:insp of safety-related Pipe Hangers Inside Containment Containing Mechanical Snubbers Revealed Snubbers Installed on Small Diameter Piping.Caused by Listing Not Including Review of Diameter Piping ML20003B6491981-02-17017 February 1981 RO 50-336/81-8:as-built Hanger Review of Reactor Vessel Head Vent Piping Sys Determined Spring Can Type Hanger Was Installed Incorrectly,Resulting in Overstressing Socket Welded Joint.Spring Can Hanger Removed ML20002D6361981-01-13013 January 1981 Ro:On 801209,inservice Insp Revealed That Required Valve Operability Tests Not Performed During Third Calendar Quarter 1980.Valves Successfully Tested.Action Taken to Assure Timely Review of Valve Test Data ML19330C0201980-08-0101 August 1980 RO 80-26:water Seal for Piping Penetration in Refueling Water Storage Tank Pipe Tunnel Does Not Meet Design Requirements.Plugged Yard Storm Drain Caused Water Backup. Repairs to Water Seal Will Be Evaluated ML19323C3571980-05-0909 May 1980 RO 50-336/80-18:during Ongoing Hanger Base Plate Analysis Required by IE Bulletin 79-02,discovered That Several Svc Water Support Hangers Did Not Provide Factor of Safety Greater than Two.Repair Work on 12 Hangers Is Underway ML19294B6771980-01-23023 January 1980 Ro:On 791229,loss of Main Control Board Annunciators Occurred.Fourteen Power Supplies That Are Paralleled to Provide Voltages for Annunciator Electronics,Lamps & Field Contacts Failed.Surveillance Implemented ML19275A2751979-09-25025 September 1979 RO 50-336/79-27:during Engineering Review,Section of 4-inch Cast Iron Floor Drain Piping Passing Each Station Battery Was Found Not Supported in Accordance W/Design.Drain Working & Ductwork Removed 1993-06-24
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217P5391999-10-25025 October 1999 Rev 0,Change 1 to Millstone Unit 1 Northeast Utils QA Program ML20217C8721999-10-0606 October 1999 Rev 21,change 3 to MP-02-OST-BAP01, Nuqap Topical Rept, App F & G Only B17896, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 1.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 1.With B17894, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 2.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 2.With B17898, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 3.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 3.With ML20216J4341999-09-24024 September 1999 Mnps Unit 3 ISI Summary Rept,Cycle 6 ML20211N8401999-09-0202 September 1999 Rev 21,change 1 to Northeast Utils QA TR, Including Changes Incorporated Into Rev 20,changes 9 & 10 B17878, Monthly Operating Rept for Aug 1999 for Mnps,Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Mnps,Unit 1.With B17874, Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 3.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 3.With ML20216F5141999-08-31031 August 1999 Rept on Status of Public Petitions Under 10CFR2.206 B17879, Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 2.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 2.With ML20211G9631999-08-30030 August 1999 SER Accepting Licensee Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20211A6561999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 2 B17858, Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 3.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 3.With B17856, Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 1.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 1.With ML20210J0311999-07-21021 July 1999 Rev 20,Change 10 to QAP 1.0, Organization ML20210E5931999-07-19019 July 1999 Revised Page 16 of 21,to App F of Northeast Util QA Program Plan ML20210C5911999-07-15015 July 1999 Revised Rev 20,change 10 to Northeast Util QA Program TR, Replacing Summary of Changes ML20210A0411999-07-15015 July 1999 Rev 20,change 10 to Northeast Util QA Program Tr B17814, Special Rept:On 990612 B Train EDG Failed to Restart within 5 Minutes Following Completion of 18 Month 24 H Endurance Run Required by TS 4.8.1.1.2.g.7.Caused by Procedural inadequacy.Re-performed Hot Restart Via Manual Start1999-07-12012 July 1999 Special Rept:On 990612 B Train EDG Failed to Restart within 5 Minutes Following Completion of 18 Month 24 H Endurance Run Required by TS 4.8.1.1.2.g.7.Caused by Procedural inadequacy.Re-performed Hot Restart Via Manual Start ML20209D1881999-07-0101 July 1999 Rev 20,change 9 to Northeast Util QA Program Tr ML20196J2191999-06-30030 June 1999 SER Concluding That Licensee USI A-46 Implementation Program,In General,Met Purpose & Intent of Criteria in GIP-2 & Staff Sser 2 for Resolution of USI A-46 ML20211A6751999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 2,providing Revised Average Daily Unit Power Level & Operating Data Rept ML20196A8451999-06-30030 June 1999 Post Shutdown Decommissioning Activities Rept ML20209J0541999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Unit 2 B17830, Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 3.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 3.With ML20196K1791999-06-30030 June 1999 Addendum 6 to Millstone Unit 2 Annual Rept, ML20196J1821999-06-30030 June 1999 Rev 21,Change 0 to Northeast Utilities QAP (Nuqap) Tr B17833, Monthly Operating Rept for June 1999 for Millstone Power Station,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Power Station,Unit 1.With ML20195H1011999-06-11011 June 1999 Rev 20,change 8 to Northeast Utilities QAP (Nuqap) TR ML20207G6411999-06-0303 June 1999 Safety Evaluation Supporting Amends 105,235 & 171 to Licenses DPR-21,DPR-65 & NPF-49,respectively ML20211A6631999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 2,providing Revised Average Daily Unit Power Level,Operating Data Rept & Unit Shutdowns & Power Reductions B17808, Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 3.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 3.With ML20211B7351999-05-31031 May 1999 Cycle 7 Colr B17804, Monthly Operating Rept for May 1999 for Mnps,Unit 2.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Mnps,Unit 2.With B17807, Monthly Operating Rept for May 1999 for Mnps,Unit 1.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Mnps,Unit 1.With ML20209J0661999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Millstone Unit 2 ML20206M4631999-05-11011 May 1999 Safety Evaluation Supporting Alternative Proposed by Licensee to Perform Ultrasonic Exam on Inner Surface of Nozzle to safe-end Weld ML20206J8351999-05-0707 May 1999 Rev 20,Change 7 to QAP-1.0, Northeast Utls QA Program (Nuqap) Tr ML20206G6221999-05-0404 May 1999 SER Accepting Util Request to Apply leak-before-break Status to Pressurizer Surge Line Piping for Millstone Nuclear Power Station,Unit 2 B17782, Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station,Unit 1.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station,Unit 1.With ML20205R3531999-04-30030 April 1999 Addendum 4 to Annual Rept, B17775, Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station Unit 3.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station Unit 3.With ML20205K6141999-04-30030 April 1999 Non-proprietary Version of Rev 2 to Holtec Rept HI-971843, Licensing Rept for Reclassification of Discharge in Millstone Unit 3 Spent Fuel Pool ML20206E2971999-04-30030 April 1999 Rev 1 to Millstone Nuclear Power Station,Unit 2 COLR - Cycle 13 B17777, Monthly Operating Rept for Apr 1999 for Millstone Unit 2. with1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Unit 2. with ML20205Q5891999-04-0909 April 1999 Rev 20,change 6 to QAP-1.0,Northeast Utils QA Program TR ML20205R8751999-04-0909 April 1999 Provides Commission with Staff Assessment of Issues Related to Restart of Millstone Unit 2 & Staff Recommendations Re Restart Authorization for Millstone Unit 2 ML20206T3991999-03-31031 March 1999 First Quarter 1999 Performance Rept, Dtd May 1999 B17747, Monthly Operating Rept for Mar 1999 for Millstone Nuclear Power Station,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Millstone Nuclear Power Station,Unit 1.With 1999-09-30
[Table view] |
Text
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lWMrrHI!AST IFFII.FFII!S^ '
P O BOX 270
} , HARTFORD. CONNECTICUT 06101 (203) 666-6911 3 L J Mr. Richard C. DeYoung, Director July 15,1983 Office of Inspection and Enforcement U.S. Nuclear Peguhtory Camission MP-5244 Washington, D. C. 20555
Reference:
Facility Operating License No. DPR-65, Docket No. 50-336
Dear Mr. DeYoung:
This letter forwards the Special Report required to be subnitted within ninety days pursuant to Millstone Unit 2 Appendix A Technical Specifica-tions, Section 6.9.2.e and 3.5.2.b, IOCS Actuation.
Plant Conditions Prior to the Event:
On April 21, 1983 at 1340 hours0.0155 days <br />0.372 hours <br />0.00222 weeks <br />5.0987e-4 months <br />, Unit 2 was operating at 67% power, with 2 charging pumps operating and an 80 gallon per minute continuous dilution in progress. Earlier in the day, a dropped CEA caused a reduction of power to less than 70%. Xenon had not yet peaked, therefore it was still adding
^
strong negative reactivity. An Instrumentation and Controls (I&C) technician had obtained permission to perform surveillance procedure SP 2403J Panual Test Insertion (MII) surveillance on the Engineered Safeguards Actuation Systan (ESAS).
Event Cescription The I&C technician had satisfactorily ccmpleted the preliminary tests of the MII equipnent and had begun to connect the box to the ESAS cabinets.
lie had connected the ccumon ard Vo leads to the Channel A Containnent Pressure bistable and the cmmon lead to the Channel C Containment Pressure bistable. As the Vo lead was connected, all of the actuation module lights cane on. He imrediately rmoved the lead and all lights went out, without having to push any reset buttons. h Containment Pressure bistable had not energized. At the instant the actuation modules energized, both facility I and II SIAS equipnent energized. The operators innediately
, . observed Pressurizer and Containment pressures and found them to be normal.
h Shift Supervisor verified with the technician that it had been an inadwrtent initiation as a result of the testing. 'Ihe Control Operator (CO) secured the Boric Acid punps and shut the Boric Acid Storage Tank gravity feed valves. The charging pump suction was restored to the Volume Contial Tank (VCT) . The Supervising Control Opstor (SCO) reduced turbine load to match reactor power. h sudden reduction of reactor power fran the boration prior to the turbine load reduction resulted in a slight cmldown (approx. 2 F on Tc) and a resultant RCS pressure drcp of c.pproxi-mately 20 PSI. h CO and SCO 1mnediately began restoration of egaipment to normal operating condition. Operating Provh 2394, Inadvertent IICS Initiation, was obtained and equipnent verified to be restored.
G307210342 830715 /
PDR ADOCK 05000336 Id S PDR f
. .\ -
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=
Analysis of Event:
2 During the performance of OP 2394, it was discovered that all pumps and ;
fans responded to the SIAS signal, throttle valves were found to be in a throttled position and scnne valves and dampers had not changed position. ,
h initial determination of the event therefore, was that a random ac- j tuation of SIAS Actuntion bbdules had occurred since not all equignent i respcnded. Subsequent investigation revealed that all valves which were =
found not to be in their accident position wem air operated valves and the 3 actuation modules associated with those valves had in fact fired since i other equipnent had gone to their accident position. Motor operated valves ?
had gone to their accident position. a
==
A test was perfonned on certain valves which were known to not hnve j responded to the SIAS signal. When their associated act21ation rnodule f energized, all valves responded and remained in their required position / 1 mode until reset by the operator. Further checking of air operated valves ]
showed that if the valve does not go full travel before the signal is 2 -
t rmoved the valve will return to its original position. Since the SIAS signal was innediately rmoved, all air operated valves were discovered in their original position. This also explains the "as found" position of the 4 ventilation dampers. !
a A theory which could explain why the actuation occurred is that sten the y test gear was connected to the Containment Pressure bistable, it could have -
loaded or scruehow reduced the 15 volt logic power supply such that the .
actuation roodules associated with Containment Pressure /SIAS signal fired.
As soon as the probe was renoved, the actuation inodules reset since they --
were not " locked-in" through the logic circuitry. h reason for the J
" crowbar circuit" is to short the 24 volt actuation nodule power supply if a voltage dip on the 15 volt logic power supply is sensed. h crcwbar i prevents randcm firing of the actuation modules. In this case the test i prthe was connected downstream of the voltage sensing device, therefore the $
crowbar protection was not available. ;
i h intention of the MrI is to test the various logic conbinations for 11 actuation module response. This signal is of such a short duration (less
than 2 milliseconds) that equipnent acblation does not occur. In this 5 event, the prebe insertion was sufficient to result in equignent actuation. J R
A couplete check was performed on the MPI test equipnent and no inconsis- 2 tencies or abnonnalities were found. A check of the test circuit diagram E also revealed no reason or means of causing the actuation. It should be $
noted that as a precautionarv measure, the MrI box is always powered through an isolation transformer. 'Ihis should have prevented the d grounding / loading of the 15 volt supply as described above. }
i
Consequences of Event:
There were no consequences effecting plant operation as a result of the initiation other than a slight increase in PCS boron concentration (approximately 15 PPM) with its resultant power decrease of 7%. Since letdown flow had not isolated, the heating effect produced by the Pegenera-tive Heat Exchanger was still present, therefore there was no thermal shock to the charging line nozzles or in the reactor coolant systen in general.
Conclusions:
Though the exact cauw of the inadvertent initiation is not known, all equipnent responded as required. In the future, the MPI surveillance will be satisfied whenever possible by the Autcmatic Test Insertion (ATI) device which is in continuous operation and will verjfy proper ESAS operation. If the MrI is required to be performed, operators vill be stationed to mitigate any potential problems or indertent actuation.
Yours truly, NORIHEAST NUCLEAR ENErsTI ANY 6V,'-g at/
E. J. Mroczka Station Superintendent Millstone Nuclear Power Station FJM/JGR:mo cc: Dr. T. E. Murley, Region Administrator, Region I, King of Prussia, PA.19406 Director, Office of Management Information and Preguuu Control, Washington, D. C. 20555 (3)
U. S. Nuclear Regulatory Camission, c/o Document Management Brarch, Washington, D. C. 20555 L _
i