ML20024B305

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Questions Availability Record of Plants
ML20024B305
Person / Time
Site: Crane  Constellation icon.png
Issue date: 10/05/1978
From: Vannoy W
BABCOCK & WILCOX CO.
To: Favret L
BABCOCK & WILCOX CO.
References
TASK-*, TASK-GB GPU-2442, NUDOCS 8307080340
Download: ML20024B305 (2)


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L. St. FAVRET, VICE PRESIDENT 3

NUCLEAR DIVISIONS

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W W. St. VANN0Y, EXECUTIVE VICE PRESIDENT file No.

- In POWER CENERATION GRCUP e, get,

-M-AVAILABILITY OF Br.W PLANTS 38 CCTOBER 5, 19 7 3 l

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Our availability is the worst in the industry. We continue to have the same problems with reactor coolant pumps, seals, CRD>t's, etc.

We talk of 90% availability for NSS by 1980. We appear to be giving lip service to this objective. What is going to be done -

hard facts?

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4/1x 2 QC. 1978 Volute 6 !:uit.cr 14 September 19, 1978 PL/.'if CPEPATI;;*. EXPERIENCE.

August 1978 10!ch - Gross nss Avail

Unit Capacity 3 Last Last Aucust Total 1

_Aums t _12 Mo.

Cum 2 12 Mo.

Cum 2 Oconee 495,800 _24,630,450 94 76 72

.73 66 60 Oconee-2 367,030 19,c35.S30 66 74 70 54 62 61 Oconce-3 644,400 20,5*3,044 98 7G 77 SS.

63 63 TMI-1 C03,659 22,657,215 100 85 81 97 79 75 98 81 76, 93 67 63 ANO-1 605,755 18.277,932 Rancho seco 600,587 15,030,224 100 76 66 59 57 49 Crystal River-3 0

5,358,397 0

49 61 0

44 47

. Davis-Besse 151.451 2.107,472 52 53' 58*

20 29*

29*

Total !!.'ch 3,550,652 123,601,534 AV9-76 72 67 59 g

wet;ntea Avg.'

73 62 Plant Heat Rate, net (average for St*J units) = 10,712 BTU /kweh 2

Plant Heat Rata:, net (average for all other operating units") = 11,055 BIU/kweh 15ince initial startup i

25tnce cc=ercial operation 3 Based on Maximum Oependable Capacity Net since comercial operation

' Average through SVeighted against total it.leh

  • Last 10 cenths.

AUGUST Op!?>.TIO!:S Ocence-3, 7hree (*!1e Island-1. Arkansas Nuclear One-1 and Rancho Seco all operated at or near maximum capacity for the entire centh.

Oconce-2 was shutd:.n on 4;ust 11 to repair railed RC pump leakage instru:.en again on August 14 due to failed seals on two RC pumps.

0:ence-1 needed replace.eit of a failed stator in cariy August along uith repairs ts 6: ster hea*ers. On *ay: 13 an.; c.v: lair-3 in: recta in th.' --* ured -"-'r:e

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