ML20012F592

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Monthly Operating Repts for Mar 1990 for Prairie Island Nuclear Generating Plant
ML20012F592
Person / Time
Site: Prairie Island  Xcel Energy icon.png
Issue date: 03/31/1990
From: Dugstad D, Parker T
NORTHERN STATES POWER CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NUDOCS 9004160255
Download: ML20012F592 (9)


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f April 10, 1990 Prairie Island Technical Specification Section 6.7.A.3 U S Nuclear Regulatory Commission I

Attn: Document Control Desk Washington, DC 20$$$

PRAIRIP, ISLAND NUCLF).R GCNTMTING PLANT O

boektt No. SCA S?

Licente N(, DPR44't

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1 Konthly operr. ting. keport Mm. h b999 Attacitt'. is the Monthly Operstieg Peport for March,1990 for the Prairie j

Inland 11uclear Generating Plant..

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W Thomas M Parker Manager Nuclear Support Services

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Director Office of Resource Management Regional Administrator III, NRC i

NRR Project Manager, NRC NRC Resident Inspector MPCA Attn: J V Perman l

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J, DDCKET NO.,50-282 4

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h@,< l.ON11HC' 20TH. R.0857 POWER WAS REDUCED TO ABOU

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b UPERTURBAT10N TEST 4T HICH. REACTOR POWER. ALL WENT WELL.'

$ $ yONJYllE 3.1ST.9 0001 1HE UNIT' LDAD FOLLOWED PER SYSTEN.DISPATf'H UNTfL 0620s

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DOCNET'NO.59-202 UNIT' PRAIRIE ISLAND WQ.i_

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DATE, APRIL 4,~1990 COMPLETED BY DALE DUGSTAD.

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2.~ REPORTING. PERIOD: N&ECH... 1270..

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^7 C0 3.1 LICENSED' THERMAL POWER (MWT)i 1650 l

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4C NAMEPLATE RATING (GROSS MWE):

593 l

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.I if' J76 M4XIMUM DEPENDABLE CA!'ACITY a' NET' MI6)1 S03 1.,

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.YB:10:D61E, CUbuLeIIVEe i1; HOURS-IN REPORTING PERIOD 744 2160 142900' Ql12. NUMBER.0F HOURS REACTOR WAS CRITICAL:

'744.0 1260.2

-120379.7

13.n REACTOR RESERVE: SHUTDOWN HOURS 0.0 0.0-5571.1<.'

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'L14.THOURS GENERATOR ON-LINE 744.0 1188.3

T118836.6' "

l i150 UNIT RESERVE SHUTDOWN' HOURS 0.0 0.0 0.01 6144:. GROSS THERMAL ENERGY' GENERATED (MWH)

~1204506

.1586225 186947679i Gki7e GROSS ELECTRICAL ENERGY GENERATED-(MWH) L405570 529700

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118. NET ELECTRICALLENERGY GENERATED (MWH)-

385730 495594

57548928 s

19'JUNITTSERVICE FACTOR 100.0 55.0 83.2

20.< UNIT AVAILABILITY ~ FACTOR 100.0 55.0 83.26

( 211 UNITLCAPACITY~ FACTOR (USING MDC NET)

'103.1 45.6'

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L.g22.1 UNIT CAPACITY, FACTOR (USING DER NET)

'97.8 43.3

'76.01

$23.' UNIT FORCED OUTAGE RATE 0.0 2.8 5.9:

f 24d FORCED OUTAGE HOURS-0.0 33.9:

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COMPLETED BY DALL DUGSIeD______

TELLEPHONE 61?-300-1101-6376 MONIUllMBEU..__

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IYLE BE650ti dCIURD SYSIEb CODE F-FORCED A-EQUIPMENT FAILURE 1 MANUAL.

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C-REFUELING 3-AUTO TRIP D-REGULATORY RESTRICTION 4-CONTINUED E-OPERATOR TRAINING &

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DATE' APRIL'.4,.1990

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THE' UNIT WAS DASE LOADED THIS HONTH.

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ON THE'8TH'O 1142 THE UNIT TRIPPED DUE TO A FAULTY RELAY ASSOCIATED lWITH.THE GENERATOR BUS DUCT COOLING SYSTEH. DURING THE STARTUP THE REACTOR-

. ENT CRITICAL 9 2208 BUT. TRIPPED G 0120 0F THE 9TH DUE TO A BLOWN FUSE F

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IN THE REACTOR PROTECTION SYSTEM. ON THE'iOTH & 0215 THE REACTOR'WENT 1: CRITICAL AND THE GENERATOR WAS PLACED ON-LINE 9 0928.'THE FIRST TRIP CAUSED SOME SECONDARY SIDE RELEIFS TO LIFT AND ONE FLANGE LEAK..THESE.

PROBLEMS WERE ADDRESSED.-

ON THE 16TH THE UNIT TRIPPED & 0921 DUE TO IMPROPERLY ATTACHING TEST-

' EQUIPMENT TO THE. ROD CONTROL SYSTEM'S ON-LINE~ MONITORING EQUIPMENT. THIS

'CAUSEDiA GROUND IN THE SYSTEM AND A TRIP WHEN THE URGENT ALARM WAS RESET.

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THE REACTOR'WENT CRITICAL 0 2233.AND'THE GENERATOR WAS PLACED ON-LINE 9:

'~0120 0F THE 1.7TH. NO-PROBLEMS WERE ENCOUNTERED DURING THIS~ TRIP OR.STARTUP.

0Nl.THE 20TH. 9 'i M 5 THE UNIT'S POWER WAS REDUCED TO APPROXIMATELY 500 MWE 4 -(REACTOR POWER:9 9S%) DUE TO'A TUBE' LEAK IN 2iA FEEDWATER HEATER.THE UNIT l REMAINED AT'THISJPOWER LEVEL.UNTIL THE'31ST-@ 1900 WHEN THE' REACTOR'WAS iRETURNED'TO 100% POWER. THE UNITS ELECTRICAL OUTPUT IS STILL-LOW DUE'TO THE FEEDWATER HEATERS OUT OF SERVICE AND THE SPRING. BLOWDOWN RESTRICTION.

~21A'FEEDWATER HEATER IS SCHEDULED FOR REPAIR ON THE WEEKEND OF APRIL 7TH.

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OEEBoIING Dolo _BCE0BI DOCKET NO. 50-306 UNIT PRAIRIE ISLAND N0.2_

DATE APRIL 4, 1990 COMPLETED BY DALE DUGSTAD TELEPHONE 612-368-1121-4376 OEERoIING_II6IUS

i. UNIT NAME:

E801BIE_ISLOND_NO._2

2. REPORTING PERIOD:_doECU______1220___

l NOTES:

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3. LICENSED THERMAL POWER (MWT):

1650 l

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NAMEPLATE RATING (GROSS MWE).

593 l

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5. DESIGN ELECTRICAL RATING (NET MWE):

530 l

l

6. MAXIMUM DEPENDABLE CAPACITY (GROSS MWE)t 534 l

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7. MAXIMUM DEPENDADLE CAPACITY (NET MWE):

500 1_ _ _.. _ _ _ _ _ _ _ _

_ _ _. 1 8.

IF. CHANGES OCCUR IN CAPACITY RATINGS (ITEMS NUMBER 3 THROUGH 7)

SINCE LAST REPORT GIVE REASON:__NONE______________________________

9. POWER LEVEL TO WHICH RESTRICTED, IF ANY (NET MWE):__NONE_..___,____

,10. REASONS FOR RESTRICTIONS, IF ANY:__NONE_______________________________

IHIS_MONIU YB:IO:D6IE

.CUduLGIIVE ii. HOURS IN REPORTING PERIOD 744 2160 133918

12. NUMDER OF HOURS REACTOR WAS CRITICAL 695.6 1894.2 117795.9

,13. REACTOR RESERVE SHUTDOWN HOURS 0.0 0.0 1516.1

14. HOURS GENERATOR ON-LINE 682.1 1865.8 116633.8
15. UNIT RESERVE SHUTDOWN HOURS 0.0 0.0 0.0-
16. GROSS THERMAL ENERGY GENERATED (MWH) 1089263 3014737

'd4242984

17. GROSS ELECTRICAL ENERGY GENERATED (MWH) 358840 1005980 39748900 10 NET ELECTRICAL ENERGY GENERATED (MWH) 339919 951400 56509193

'19. UNIT SERVICE FACTOR 91.7 86.4 87.1

20. UNIT AVAILABILITY FACTOR 91.7 86.4 87.1
21. UNIT CAPACITY FACTOR (USING MDC NET) 91.4 80.1 84.4 72.-UNIT CAPACITY FACTOR (USING DER NET) 86.2 83.1 79.6
23. UNIT FORCED OUTAGE RATE 8.3 13.6 3.2
24. FORCED OUTAGE HOURS 61.9 294.2 3840.0
25. SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE, DATE & DURATION OF EACH)

________REEUELING_6HD_MoINIEN6NCE_IN_6UGUSI__1220 ___________.._________

26.-IF CURRENTLY SHUTDOWN ESTIMATED STARTUP DATEl_.___._H_o_______

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90/03/00 F,

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90/03/i6 F;

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90-003 AA N/A; C

~ TEST EQUIPMENT CAUSED GROUND IN ROD CONTROL SYSTEM.

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C-REFUELING 3-AUTO TRIP D-REGULATORY RESTRICTION 4-CONTINUED E-OPERATOR TRAINING &

5-REDUCED LOAD C0dEONENI_ CODE LICENSE EXAMINATION 9-0THER F-ADMINISTRATIVE IEEE STD 003A-1903 G-OPERATIONAL ERROR H-0THER

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