|
---|
Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARML20217K4701999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for TMI-1.With ML20211Q3551999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Tmi,Unit 1.With ML20210U4791999-07-31031 July 1999 Monthly Operating Rept for July 1999 for TMI-1.With ML20209H1421999-06-30030 June 1999 Monthly Operating Rept for June 1999 for TMI-1.With ML20195H9261999-05-31031 May 1999 Monthly Operating Rept for May 1999 for TMI-1.With ML20206R0571999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Tmi,Unit 1.With ML20205K6851999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Tmi,Unit 1.With ML20207M8461999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for TMI-1.With ML20198B8641998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for TMI-1.With ML20196B7191998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for TMI-1.With ML20154L5541998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for TMI Unit 1.With ML20151V2811998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Tmi,Unit 1.With ML20237C6411998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Tmi,Unit 1 ML20236R2201998-06-30030 June 1998 Monthly Operating Rept for June 1998 for TMI-1 ML20249A1061998-05-31031 May 1998 Monthly Operating Rept for May 1998 for TMI-1 ML20247G0761998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Three Mile Island Nuclear Station,Unit 1 ML20216K1061998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Three Mile Island Nuclear Station,Unit 1 ML20216F0981998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Three Mile Island Nuclear Station,Unit 1 ML20202F8121998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for TMI Nuclear Station, Unit 1 ML20199J3251997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Three Mile Island Nuclear Station,Unit 1 ML20203K4081997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for TMI-1 ML20199E3401997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for TMI-1 ML20198J8121997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for TMI-1 ML20217A8761997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for TMI-1 ML20210K0331997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Three Mile Island, Unit 1 ML20196G8401997-06-30030 June 1997 Monthly Operating Rept for June 1997 for TMI-1 ML20210K0401997-06-30030 June 1997 Revised App B of Monthly Operating Rept for June 1997 for Three Mile Island,Unit 1 Correcting Calculational Error in Shutdown Duration Hours Value ML20141C6521997-05-31031 May 1997 Monthly Operating Rept for May 1997 for TMI-1 ML20141G2801997-04-30030 April 1997 Monthly Operating Rept for Apr 1997 for TMI-1 ML20140D6601997-03-31031 March 1997 Monthly Operating Rept for Mar 1997 for Three Mile Island, Unit 1 ML20136G3891997-02-28028 February 1997 Monthly Operating Rept for Feb 1997 for Three Mile Island Nuclear Station,Unit 1 ML20134Q2071997-01-31031 January 1997 Monthly Operating Rept for Jan 1997 for TMI-1 ML20133G8231996-12-31031 December 1996 Monthly Operating Rept for Dec 1996 for TMI-1 ML20132D5431996-11-30030 November 1996 Monthly Operating Rept for Nov 1996 for Three Mile Island Nuclear Station,Unit 1 (TMI-1) ML20135A8291996-10-31031 October 1996 Monthly Operating Rept for Oct 1996 for TMI-1 ML20129B6621996-09-30030 September 1996 Monthly Operating Rept for Sept 1996 for Three Mile Island Nuclear Station Unit 1 (TMI-1) ML20129C2661996-08-31031 August 1996 Monthly Operating Rept for Aug 1996 for Three Mile Island Nuclear Station,Unit 1 ML20116N6571996-07-31031 July 1996 Monthly Operating Rept for July 1996 for Three Mile Island Nuclear Station,Unit 1 ML20115E2071996-06-30030 June 1996 Monthly Operating Rept for June 1996 for TMI-1 ML20117M1581996-05-31031 May 1996 Monthly Operating Rept for May 1996 for Three Mile Island Unit 1 ML20112A2171996-04-30030 April 1996 Monthly Operating Rept for Apr 1996 for Three Mile Island Nuclear Station Unit 1 ML20117D3691996-03-31031 March 1996 Monthly Operating Rept for March 1996 for TMI-1 ML20101C6811996-02-29029 February 1996 Monthly Operating Rept for Feb 1996 for Three Mile Island Nuclear Station,Unit I ML20149K7551996-01-31031 January 1996 Monthly Operating Rept for Jan 1996 for TMI-1 ML20096D5781995-12-31031 December 1995 Monthly Operating Rept for Dec 1995 for TMI Nuclear Station ML20095E0521995-11-30030 November 1995 Monthly Operating Rept for Nov 1995 for TMI-1 ML20094L7651995-10-31031 October 1995 Monthly Operating Rept for Oct 1995 for TMI-1 ML20093E6731995-09-30030 September 1995 Monthly Operating Rept for Sept 1995 for TMI-1 ML20092F4401995-08-31031 August 1995 Monthly Operating Rept for Aug 1995 for TMI-1 ML20086F5021995-06-30030 June 1995 Monthly Operating Rept for June 1995 for TMI Unit 1 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G1001999-10-14014 October 1999 Errata to Safety Evaluation Supporting Amend 215 to FOL DPR-50.Credit Given for Delay in ECCS Leakage ML20217K4701999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for TMI-1.With ML20216F9231999-09-22022 September 1999 Safety Evaluation Supporting Amend 216 to License DPR-50 05000289/LER-1999-010, :on 990830,discovery of Condition Outside UFSAR Design Basis for Flood Protection Was Noted.Caused Because Original Problem Was Not Corrected by Design Change.Flood Procedure Was Immediately Revised.With1999-09-21021 September 1999
- on 990830,discovery of Condition Outside UFSAR Design Basis for Flood Protection Was Noted.Caused Because Original Problem Was Not Corrected by Design Change.Flood Procedure Was Immediately Revised.With
ML20211H5111999-08-31031 August 1999 Non-proprietary Rev 1 to MPR-1820(NP), TMI Nuclear Generating Station OTSG Kinetic Expansion Insp Criteria Analysis ML20211Q3551999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Tmi,Unit 1.With ML20211E8731999-08-24024 August 1999 Safety Evaluation Supporting Amend 215 to License DPR-50 ML20211B1931999-08-19019 August 1999 Safety Evaluation Supporting Amend 214 to License DPR-50 ML20210R4791999-08-13013 August 1999 Update 3 to Post-Defueling Monitored Storage SAR, for TMI-2 ML20210U4791999-07-31031 July 1999 Monthly Operating Rept for July 1999 for TMI-1.With 05000289/LER-1999-009, :on 990626,automatic Start of EDG 1A Occurred. Caused by Failure of Fault Pressure Relay on Auxiliary Transformer 1B.Failed Pressure Relay Has Been Replaced1999-07-22022 July 1999
- on 990626,automatic Start of EDG 1A Occurred. Caused by Failure of Fault Pressure Relay on Auxiliary Transformer 1B.Failed Pressure Relay Has Been Replaced
ML20210K7651999-07-0909 July 1999 Rev 2 to 86-5002073-02, Summary Rept for Bwog 20% Tp Loca ML20209G0011999-07-0909 July 1999 Staff Evaluation of Individual Plant Exam of External Events Submittal on Plant,Unit 1 ML20209H8251999-07-0101 July 1999 Provides Commission with Evaluation of & Recommendations for Improvement in Processes Used in Staff Review & Approval of Applications for Transfer of Operating Licenses of TMI-1 & Pilgrim Station ML20209H1421999-06-30030 June 1999 Monthly Operating Rept for June 1999 for TMI-1.With ML20212H9101999-06-21021 June 1999 Safety Evaluation Supporting Amend 212 to License DPR-50 05000289/LER-1999-007, :on 990528,increasing Failure Rate of ESAS Relays Characterized by Coil Overheating & Failing to Fully re-close After Being de-energized Was Discovered.Cause Indeterminate.Relay Check Procedure Has Been Changed1999-06-18018 June 1999
- on 990528,increasing Failure Rate of ESAS Relays Characterized by Coil Overheating & Failing to Fully re-close After Being de-energized Was Discovered.Cause Indeterminate.Relay Check Procedure Has Been Changed
ML20195J9401999-06-15015 June 1999 Safety Evaluation Supporting Amend 211 to License DPR-50 05000289/LER-1999-005, :on 990514,open Flood Path Between Turbine Bldg & Control Bldg Was Noted.Caused by Failure to Recognize That Mods Affected Flood Protection.Revised Flood Procedures.With1999-06-14014 June 1999
- on 990514,open Flood Path Between Turbine Bldg & Control Bldg Was Noted.Caused by Failure to Recognize That Mods Affected Flood Protection.Revised Flood Procedures.With
ML20195H0751999-06-0808 June 1999 Drill 9904, 1999 Biennial Exercise for Three Mile Island ML20195H9261999-05-31031 May 1999 Monthly Operating Rept for May 1999 for TMI-1.With ML20209G0351999-05-31031 May 1999 TER on Review of TMI-1 IPEEE Submittal on High Winds,Floods & Other External Events (Hfo) ML20207B6621999-05-27027 May 1999 SER Finding That Licensee Established Acceptable Program to Periodically Verify design-basis Capability of safety-related MOVs at TMI-1 & That Util Adequately Addressed Actions Required in GL 96-05 05000289/LER-1999-003-01, :on 990310,discovered Failure of Manual Balancing Damper in Supply Duct of Control Bldg Evs.Caused by Failure to Adequately Review Risk & Consequences of Change.Failed Damper Was Clamped Open1999-05-0707 May 1999
- on 990310,discovered Failure of Manual Balancing Damper in Supply Duct of Control Bldg Evs.Caused by Failure to Adequately Review Risk & Consequences of Change.Failed Damper Was Clamped Open
ML20206R0571999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Tmi,Unit 1.With ML20206D4201999-04-20020 April 1999 Safety Evaluation Granting Exemption from Technical Requirements of 10CFR50,App R,Section III.G.2.c for Fire Areas/Zones AB-FZ-4,CB-FA-1,FH-FZ-1,FH-FZ-6,FH-FZ-6, IPSH-FZ-1,IPSH-FZ-2,AB-FZ-3,AB-FZ-5,AB-FZ-7 & FH-FZ-2 ML20205Q6111999-04-15015 April 1999 Safety Evaluation Supporting Amend 210 to License DPR-50 ML20205Q5981999-04-13013 April 1999 Safety Evaluation Supporting Amend 209 to License DPR-50 ML20206P2841999-04-12012 April 1999 SER Approving Transfer of License for Tmi,Unit 1,held by Gpu Nuclear,Inc to Amergen Energy Co,Llc & Conforming Amend, Per 10CFR50.80 & 50.90 ML20209G0071999-03-31031 March 1999 Submittal-Only Screening Review of Three Mile Island,Unit 1 Individual Plant Exam for External Events (Seismic Portion) ML20205K6851999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Tmi,Unit 1.With 05000289/LER-1999-002, :on 990212,potential Failure of Multiple Containment Monitoring Sys CIV (CM-V-1,2,3 & 4) Was Noted. Caused by Inappropriate Use of Vendor Info.Personnel Will Be Trained on Mgt Expectations.With1999-03-14014 March 1999
- on 990212,potential Failure of Multiple Containment Monitoring Sys CIV (CM-V-1,2,3 & 4) Was Noted. Caused by Inappropriate Use of Vendor Info.Personnel Will Be Trained on Mgt Expectations.With
ML20210C0161999-03-0101 March 1999 Forwards Corrected Pp 3 of SECY-98-252.Correction Makes Changes to Footnote 3 as Directed by SRM on SECY-98-246 ML20207M8461999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for TMI-1.With 05000289/LER-1999-001-01, :on 990122,short Sections of Piping Caused by Misplacement of Sensing Elements & Insulation.Caused by Failure to Adhere to Vendor instruction.Re-installed Heat Trace Sys1999-02-19019 February 1999
- on 990122,short Sections of Piping Caused by Misplacement of Sensing Elements & Insulation.Caused by Failure to Adhere to Vendor instruction.Re-installed Heat Trace Sys
ML20196K3561999-01-22022 January 1999 Safety Evaluation Concluding That Although Original Licensee Thermal Model Was Unacceptable for Ampacity Derating Assessments Revised Model Identified in 970624 Submittal Acceptable for Installed Electrical Raceway Ampacity Limits 05000289/LER-1998-014-01, :on 981210,missed TS Surveillance Was Noted. Caused by Human Error.Absolute & Relative Control Rod Positions Were Obtained Immediately & Verified to Agree within Required Range.With1999-01-11011 January 1999
- on 981210,missed TS Surveillance Was Noted. Caused by Human Error.Absolute & Relative Control Rod Positions Were Obtained Immediately & Verified to Agree within Required Range.With
ML20196G4661998-12-31031 December 1998 British Energy Annual Rept & Accounts 1997/98. Prospectus of British Energy Share Offer Encl ML20207A9291998-12-31031 December 1998 1998 Annual Rept for TMI-1 & TMI-2 ML20196F6861998-12-0202 December 1998 Safety Evaluation Accepting Licensee Second 10-yr Interval ISI Program Plan Request for Alternative to ASME B&PV Code Section XI Requirements Re Actions to Be Taken Upon Detecting Leakage at Bolted Connection ML20198B8641998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for TMI-1.With ML20195C6921998-11-12012 November 1998 Safety Evaluation Supporting Amend 52 to License DPR-73 ML20195J8591998-11-12012 November 1998 Rev 11 to 1000-PLN-7200.01, Gpu Nuclear Operational QA Plan ML20196B7191998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for TMI-1.With ML20203G1211998-10-30030 October 1998 Informs Commission About Staff Preliminary Views Concerning Whether Proposed Purchase of TMI-1,by Amergen,Inc,Would Cause Commission to Know or Have Reason to Believe That License for TMI-1 Would Be Controlled by Foreign Govt 05000289/LER-1998-013, :on 980916,failure to Perform Fire Protection Program Surveillances at Required Frequency Was Noted.Caused by Changes Not Being Made to Surveillance Schedule.Performed Missed Insp Surveillance1998-10-15015 October 1998
- on 980916,failure to Perform Fire Protection Program Surveillances at Required Frequency Was Noted.Caused by Changes Not Being Made to Surveillance Schedule.Performed Missed Insp Surveillance
ML20155E7511998-10-15015 October 1998 Rev 1 to Form NIS-1 Owners Data Rept for Isi,Rept on 1997 Outage 12R EC Exams of TMI-1 OTSG Tubing 05000289/LER-1998-010-01, :on 980825,potential Violation of Design Criteria During Single Auxiliary Transformer Operation Occurred.Caused by Failure to Adequately Define Job Performance Stds.Temporary Change Notice Issued1998-10-0909 October 1998
- on 980825,potential Violation of Design Criteria During Single Auxiliary Transformer Operation Occurred.Caused by Failure to Adequately Define Job Performance Stds.Temporary Change Notice Issued
ML20154L5541998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for TMI Unit 1.With 05000289/LER-1998-011, :on 980825,Thermo-Lag Fire Barrier Was Found Installed Outside Approved Joint Design Arrangement.Caused by Personnel Error.Initiated Continuous Fire Watch & Installed Trowel Grade Thermo-Lag in Void & on Outer Edge1998-09-23023 September 1998
- on 980825,Thermo-Lag Fire Barrier Was Found Installed Outside Approved Joint Design Arrangement.Caused by Personnel Error.Initiated Continuous Fire Watch & Installed Trowel Grade Thermo-Lag in Void & on Outer Edge
1999-09-30
[Table view] |
Text
{{#Wiki_filter:_
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i GPU Nuclear Corporat6on NggIg{
Post Office Box 480 j
Route 441 South i
Middletown, Pennsylvania 17057 0191 717 944 7621 TELEX 84 2386 Writer's Direct Dial Number:
Febnnry 15, 1990 C311-90-2014 l
j U. S. Nuclear Regulatory Commission Attn:
Document Control Desk Washington, D.C.-
20555
Dear-Sir:
j Three Mile Island Nuclear Station, Unit I (TM1-1)
Operating License No. DPR-50 Docket No. 50-289 Monthly Operating Report January 1990
' Enclosed are two copies of the January 1990 Monthly Operating Report for Three Mile Island Nuclear Station, Unit 1.
Sincerely,
. D.
u ill i
Vice President & Director, TMI I HDH/WGH:2014 cc: W.; Russell, USNRC F. Young, USNRC Attachments
{
I /
P 900222046790gs;1g9 ADOCK 05
{DR GPU Nuclear Corporation is a subsidiary of the General Public Utilities Corporation
OPERATIONS SUtHARY
[
JANUARY 1990 i
It was previously reported that the plant was in a slow power reduction since December 15th, coasting down for the BR refueling outage. The plant was operated at reduced power until approximately 2200 hours on January 5th, when 1
the main generator was taken off line and the BR outage comenced.
Refueling of the reactor commenced on January 26, 1990 with control rod shuffle and continued into February.
MAJOR SAFETY RELATED MAINTENANCE During January, the following major safety related maintenance activities were performed:
Integrated Leak Rate Testing (ILRT)
With the plant in cold shutdown, preparations for the Integrated Leak Rate Test were performed. The preparation activities included calibration and installation of test instruments, inspection and test of the six air compressors to be used to pressurize the Reactor Building, and performance of local leak rate testing of the Reactor Building purge valves (AH-V-1A/B/C/D).
Repairs were required for AH-V-1C to eliminate a gasket leak before satisfactory local leak rate test results were obtained for the valve.
Bonnet leaks on'four Feedwater valves (FW-V-55A, 80A, 81A, and 82B) were sealed by injection of Furmanite compound.
The Leak Rate system was aligned for pressurization on completion of the preparations and the Reactor Building pressurized to 50.6 psi.
After a four hour stabilization period, the first twenty-four hour test was begun. This initial-ILRT was declared invalid due to leakage into the OTSGs.
Several valves on the secondary plant outside of the ILRT valve lineup were found to be open and were closed.
No significant leakage was identified as a result of inspection of the containment isolation valves and boundaries.
Unstable Reactor Building temperature conditions caused a second ILRT to be declared invalid at approximately the ten hour mark. A third test was started after securing the Reactor Building Industrial Cooler system. This third ILRT and a six hour superimposed test were completed and their results declared satisfactory. The Reactor Building was depressurized and systems returned to normal.
Fuel Handling Systems Repair and modification to the Fuel Handing equipment was performed in preparation for its use in fuel handling activities. Maintenance and repairs included repairing the telescopic cylinder down light and hose replacement on the control rod-mast of the spent fuel bridge, replacing a ten amp breaker on the Reactor Building auxiliary bridge, and replacing hoses with stainless steel tubing on the Reactor Building upenders.
The modification involved installation of pointers to aid the operators in positioning both the Spent Fuel Pool and Reactor Building Fuel Transfer Canal fuel upenders to ensure a full vertical position.
Divers installed the pointers on the Fuel-Pool fuel upenders.
E I
I l
Reactor Vessel (RC-T-1)
In preparation for refueling the reactor vessel, the following work items were accomplished. The reactor head micsile shields were removed and the Fuel Transfer Canal stairway installed. The reactor vessel head insulation was removed and the RV studs detensioned. The RV studs were parked and the guide j
studs installed.
A modification to install permanent reactor vessel head lifting pendants was started with the attachment of the pendants to support head lift. The remainder of the modification work will be completed with the head on the head stand. The Reactor Coolant Inventory Tracking system lines were disconnected and the head fans removed. The "A" to "B" cables, "P!" tube l
cables and thermocouple cables were disconnected from the head and all CRDM position indicators were then removed. The CRDM cooling water lines were disconnected and the APSR/CRDMs were uncoupled and the lead screws parked. The flood line cover plate and the fuel transfer tube flanges were removed. The head was removed from the vessel and transferred to the head stand. The indexing fixture was installed and the plenum removed from the vecsel and stored in the deep end of the canal. The stud holes were sealed and the vessel i
seal plate installed and sealed. The reactor dosimetry was replaced and the "NI" cover plate reinstalled and sealed. The reactor vessel internal vent valves were exercised and the vessel incore detectors parked.
And finally the fuel canal was flooded in preparation for fuel movement.
Control Rod Drive Mechanisms (CRDM)
During preparations for lifting and moving the reactor vessel head, leakage from several of the CRDM nozzle flanges was identified.
After investigation, fourteen leaking CRDMs were repaired. The stators from the leaking CRDMs were removed while the head was on the head stand. A shielded platform was constructed at the head to facilitate removal of the CRDM hold down bolts. The CRDM motor tubes were removed to a vertical storage rack.
Drilling of the CRDM split nut rings and additional repair work will continue into February.
Once Through Steam Generators (RC-H-1A/B)
Once Through Steam Gerrator (OTSG) work completed in January included opening of the upper primary m9nways and handboles on both "A" and "B" OTSGs and ventilating both units through the handholes.
Bubble test rigs were installed and the bubble tests performed. Though two tubes were rolled as a result of the bubble tests in the "A" OTSG, the tests were deemed inconclusive and the OTSGs drained. The lower primary mant:ays were removed in preparation for Installation of the Cold 1.eg Dams.
Main Steam Safety Valves The Main Steam Safety Valve work performed during January resulted in seven valves being repaired. The following is a summary of that work:
- 1. MS-V-17B, MS-V-17D, and MS-V-20D had seats lapped,
- 2. MS-V-20B, MS-V-21A, and MS-V-21B had discs replaced and seats lapped,
- 3. and MS-V-18A had the disc and stem replaced and seats lapped The valves were reassembled and prepared for testing when the plant achieves a hot shutdown condition.
2
Pr'essurizer Code Safety Valve (RC-RV-1A1 Pressurizer Code Safety valve RC-RV-1A was replaced with a rebuilt / tested valve. The valve removed was packaged and shipped to Wyle Laboratories for inspection and testing. Results of the tests are due in February.
l Miscellaneous Work Items Following is a summary / status of various other work items being performed j
during the BR outage:
1.
Valve repacks - 307 of 427 2.
Valve replacements - 66 of 175 3.
Large valve seat repairs - 2 of 13 4.
Local leak rate tests - 102 of 115 l
S.
MOVATS valve operator tests - 9 of 52
~
6.
Conex wire inspections - 53 of 53 7.
Molded case breaker tests - 65 of 154 8.
4160V breaker tests - 8 of 8 9.
480V breaker tests - 40 of 44
- 10. Tech Spec snubber seal replacements - 28 of 37
- 11. Tech Spec snubber functional tests - 20 of 20 12.
Non-Tech Spec snubber functional tests - 1 of 38 Note: snubber numbers reflect completed testing and not reinsta11ation.
pr "
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4 OPERATING DATA REPORT DOCKET NO.
50-209 DATE 01/31/90 COMPLETED BY C.W. Smyth TELEPHONE (717 F948-8551._
OPERATING STATUS l
l NOTES le UNIT NAME:
THREE MILE ISLAND UNIT 1 1 I
2; REPORTING PERIOD:
JANUARY
,1990. I I
3.; LICENSED THERMAL POWER (MWT):
2560. I I
& NAMEPLATE RATING (GROSS MWE):
871. I I
52 DESIGN ELECTRICAL RATING (NET MWE):
819. 1 I
MAXIMUM DEPENDABLE CAPACITY (GROSS MWE):
05G. 1 I
-7; MAXIMUM DEPENDADLE CAPACITY (NET MWE):
800. l
.I i
i Oc IF. CHANGES OCCUR IN (ITEMS 3-7) SINCE LAST REPORT, GIVE REASONS:
9 POWER LEVEL TO WHICH RESTRICTED, IF ANY (NET MWE)
- 10. CEASONS FOR RESTRICTIONS, IF ANY:
a d
THIS MONTH YR-TO-DATE CUMMULATIVE 11, HOURS IN REPORTING PERIOD 744.-
744.
135145.
-12 NUMBER OF= HOURS REACTOR WAS CRITICAL 118.1 118.1 62116.7 13 -REACTOR RESERVE SHUTDOWN HOURS 0.0 0.0 2002.8.
14 -HOURS GENERATOR ON-LINE 117.1 117.1 61113.3 2
[ 15. UNIT RESERVE SHUTDOWN HOURS 0.0 0.0 0.0:
1 ;. GROSS THERMAL ENERGY GENERATED (MWH) 235434.
235434.
149607329.
[171_ GROSS ELECTRICAL ENERGY GENERATED (MWH) 82799.
82799.
50389468.
" 104 NET ELECTRICAL ENERGY GENERATED (MWH) 72500.
72508.
47258997.
103 -UNIT SERVICE FACTOR 15.7 15.7 45.2
- 20. UNIT AVAILABILITY. FACTOR
~15.7 15.7 45.2 21e UNIT CAPACITYLFACTOR (USING'MDC NET) 12.1 12.1 44.G
- 22. UNIT CAPACITY FACTOR (USING DER NET) 11.9 11.9 42.7 23e UNIT FORCED OUTAGE RATE O.0 0.0 49.7 i:
h 24, SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE, DATE. AND DURATION OF EACH-Presently shutdown for 8R Outage.
fll~25.. IF SHUT DOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP:
2/25/90 4
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L Actiselly emed Exhibitm l
F & H NUREC 016I
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a' e
i REFUELING INFORMATION REQUEST i
l 1.
Name of Facility:
Three Mile Island Nuclear Station, Unit 1 l
2.
Scheduled date for next refueling shutdown:
October 4,1991(9R) 3.
Scheduled date for restart following current refueling: February 25, 1990 (8R) l 4.
Will refueling or resumption of operation thereafter require a technical specification change or other license amendment?
No If answer is yes, in general, what will these be?
If answer is no, has the reload fuel design and core configuration been reviewed by your Plant Safety Review Committee to determine whether any unreviewed safety questions are associated with the core reload (Ref. 10 CFR Seccion 50.59)? No If no such review has taken place, when is it scheduled?
t February 22, 1990 5.
Scheduled date(s) for submitting proposed licensing action and supporting information: None Planned 6.
Important licensing considerations associsted with refueling, e.g. new or i
different fuel design or supplier, unreviewed design or performance analysis methods, significant changes in fuel design, new operating i
l_
procedures:
None 7.
The number of fuel assemblies (a) in the core, and (b) in the spent fuel storage pool:
(a) 177 (b)440 8.
The present licensed spent fuel pool storage capacity and the size of any increase in licensed storage capacity that has been requested or is planned, in number of fuel assemblies:
The present licensed capacity is 752.
Planning to increase licensed capacity through fuel pool reracking is in process.
I 9.
The projacted date of the last refueling that can be discharged to the spent fuel pool assuming the present licensed capacity:
1991 is the last refueling discharge which allows full core off-load capacity (177 fuel assemblies).
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