ML20011A347

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QA Program Insp Rept 99900086/81-01 on 810326,27 & 30.No Noncompliance Noted.Major Areas Inspected:Mfg Status Review, Action on Previous Insp Findings,Liquid Penetrant Exam & QA Records
ML20011A347
Person / Time
Issue date: 04/28/1981
From: Barnes I, Ellershaw L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20011A341 List:
References
REF-QA-99900086 NUDOCS 8110090339
Download: ML20011A347 (5)


Text

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U.S. NUCLEAR REGULATORY COMMISSION 0FFICE OF INSPECTION AND ENFORCEMENT REGION IV Report No. 99900086/81-01 Program No. S1300 Company:

Hopkinsons Ltd.

Britannia Works P.O. Box B27 Huddersfield, ENGLAND Inspection Conduc 'ed: ' March 26, 27, and 30, 1981 f.

Inspector:

Lt.,s Ah Y 47

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hE.Ellersnaw,ContractorInspector

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Oste Rhactive Inspection Section Vendor Inspection Branch Approved'by:

/w 4 Ar/TI I. Barnes, Chief Date Reactive Inspection Section Vendor Inspection Branch Summary Inspection conducted March 26, 27, and 30, 1981 (99900086/81-01)

Areas Insoected:

Implementation of 10 CFR Part 50 Appendix B criteria and applicable coces and standards including:

manufacturing status review; action on previous inspection findings; liquid penetrant examination, and quality assurance records.

The inspection involved a total of 24 inspector hours on site by one NRC inspector.

Results:

In the four areas inspected, no nonconformances or unresolved items were identified.

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V 8110090339 810430 PDR GA999 EMVHOPK i

99900086 PDR

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. DETAILS SECTION (Prepared by L. E. Ellershaw)

. A.

Persons-Contacted

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A. Barker - QA Engineer R. Barrow - Manager, QA U. K. Clayton - Sr. Designer D. Croft - Works Manager

.R. Darroch'- NDE Level II Examiner G. Evans - Sr. QA Assistant' P. E. Holt - QA Executive H. Robinson - Chief Inspector C. Smith - Design Engineer D. Waterworth - QA Engineer R. Watson'- Engineerino Director B.

' Manufacturing Status Review

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The following information pertaining to the manufacturing status of valves being supplied to WPPSS

  • WNP 3 and 5 was obtained during this inspection.

There are 120 valves on order of which 27 for WNP 3 and 1 for WNP 5 have been shipped.

All carbon steel valves are complete.

The stainless steel valve bodies are procured from Breda Fuchine in a fully certificated condition.

Approxi-mately 50 valve bodies remain to be shipped from Breda.

Nearly all manu-facturing of valve internals is complete, with these items being stored prior to assembly.

The final shipping schedule could not be ascertained.

C.

Action on Previous Inspection Findings 1.

(Closed) Deviation, Item A (Inspection Report No. 80-02):

This item dealt with certain Manufacturing Orders (MO) not providing all infof,-

mation to enable the gompany to satisfactorily control shop production; e.g., use of design concessions not specified on M0s, incorrect drawing revisions listed on M0s, and certain drawings not specifying radii dimensions.

Hopkinsons Ltd. (HL) has implemented their cnmmitted corrective actions, in that a review of M0s and applicable drawings showed the correct revision numbers, and, all drawings not specifying radii dimen-sions have been corrected.

In addition, there was no evidence to show further use of design concessions in a manner for which they were not intended.

2.

(Closed) Deviation, Item ho. B (Inspection Report No. 80-02):

This item dealt with certain nonconforming items not being identified as nonconforming through the use of Hold Tags or other means.

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HL implemented their committed corrective action, in that a review of open and closed nonconformance reports showed, that parts for which disposition had not been completed were tagged as nonconforming and, that the documentation for parts on which disposition was com-pleted, identified the nonconformance report numbers.

3.

(Closed) Deviation, Item C (Inspection Report No. 80-02):

This item dealt with items being moved to the next operation without the preceding operation being signed off.

HL implemented their committed corrective action, in that?a review of manufacturing orders for parts in the manufacturing area revealed that all preceding operations had been signed off.

4.

(Closed) Follow-up Inspection Item, Details Section, paragraph B.7 (Inspection Report 80-02):

This item dealt with lack of documented evidence to support that an analytical avfi" Scion is being made of quality trends or the reasons for nonconformances.

HL has conductcd meetings of the Quality Corrective Action Committee and a review of nonconformances has taken place, with the results being documented to reflect the frequency and categories of the nonconfor-mances.

5.

(Closed) Follow-up Inspection Item, Details Section, paragraph B.10 (Inspection Report 80-02):

This item dealt with formalizing a system for monitoring foundry repair welding activities.

Procedure N6.-1, " Welding Quality Assurance," addresses the requirements for monitoring repair welding activities.

The effectiveness relative to the implementation of the procedure could not be asc'ertained, in that welding activity, since January,1981, has been at a.'irtual standstill.

The 24 carbon steel valve bodies for WPPSS-WNP 3 and WNP 5, which are cast by HL, have been completed.

The 96 stainless steel valve. bodies for WPPSS 3 and 5 are procured by HL from Breda Fuchine in a fully certificated condition.

There are approximate 1f 50 valve body castings remaining to be shipped from Breda Fucnine.

In addition, with very few exceptions, all components requirec for valve assembly have been completed and are in stores.

D.

Liquid Penetrant Examination (PT)

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1.

Objectives The objectives of tr's area of the inspection were to verify that HL had implemented the requirements for conducting liquid penetrant examination in accordance with the QA Manual and,applicacie NRC and ASME Code requirements.

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Method'of Accomplishment The preceding objectives were accomplished by:

a.

Review of QA Manual Section 7, "Non-Destructive Examination "

b.

Observation of PT being performed on the following items:

(1) Disc - 47/SM 5633, (2) Valve Body - 12/SM 6095, and (3) Lids (3) - 20/SM 5630, 19/SM 5630, and 27/SM 5630 c.

Review of Manufacturing Orders for the above items to assure the PT proced re to be used was specified.

d.

Review of PT Procedure No. N 7-5, revision 6.

e.

Review of the certified material-test reports associated with the cleaner, penetrant, and developer used during these exam-inations.

f.

Review of the qualification records of the Level II Examiner performing the PT.

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Discussions with cognizant personnel.

3.

Findings a.

Nonconformance None.-

b.

Unresolved Items

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None.

E.

Quality Assurance' Records 1.

Objective; The objectives of this area of the inspection were to verify that HL had implemented the requirements for generating, collecting, and storing requireo QA records in accordance with the QA Manual and applicable NRC and ASME Code requirements.

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2.

Method of Accomplishment The preceding objectives were accomplished by:

a.

Review of QA Manual Section 10. " Documentation."

b.

. Review of final QA Documentation package for the following valves; and all of their components:

(1) Auxiliary Feed Water Valve, Mark No. 3AFVH011SA.

(2) Auxiliary Feed > Water Valve, Mark No. 3AFVH045SB.

Both of these valves are SA 216 material, so particular emphasis-was placed on weld repairs and postweld heat treatnent (PWHT).

Review of the weld material certified material test reports.

c.

d.

Review of PWHT records.

Re iew of component part identification records by cross refer-e.

encing the final records with the original material test report records.

~f.

Discussions with cognizant personnel.

3.

Findings a.

Nonconformances d

None.

b.

Unresolved Items None.

F.

Exit Meeting An exit meeting was held at the conclusion of this inspection on March 30, 1981, with the followir.g management representativas:

t R. Barrow - Manager, QA P. E. Holt - QA Executive R. Watson - Engineering Director The NRC inspector summarized the scope and findings of the inspection.

Management acknowledged the statements as presented to them.

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