LER-1981-057, /03L-0:on 810716,emergency Diesel Generator 1J Declared Inoperable.Caused by Small Fire Resulting from Oil Leak in Exhaust Manifold.Procedures Will Be Changed to Prevent Oil Accumulations in Exhaust |
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m U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT CONTROL BLOCK / / / / / / / (1)
(PLEASE PRINT OR T7PE ALL REQUIRED INFORMATION)
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LICENSEE CODE LICENSE NUMBER LICENSE TYPE CAT
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DOCKET NUMBER EVENT DATE REPORT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES (10)
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/ On July 16, 1981, with Unit I at 100 percent power, a small oil fire on IJ
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/ emergency diesel generator developed aad it was declared inoperable. This event /
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/ reportable pursuant to T.S. 6.9.1.9.b.
The action statement of the LCO (T.S.
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/ 3.8.1.1) was met. 1H emergency diesel generator and off-site power sources were
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IJ emergency diesel generator was returned to operable
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/, status on July 18, 1981. The public health and safety were not affected.
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SYSTEM
CAUSE
CAUSE COMP.
VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE
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SEQUENTIAL OCCURRENCE REPORT REVISION LER/R0 EVENT YEAR REPORT NO.
CODE TYPE NO.
(17) REPORT NUMBER
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ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRD-4 PRIME COMP.
COMPONENT TAKEN ACTION ON PLANT METHOD HOURS SUBMITTED FORM SUB. SUPPLIER MANUFACTURER
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CAUSE DESCRIPTION AND CORRECTIVE ACTIONS (27)
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/ An oil leak in the exhaust manifold caused the fire. Oil accumulations above the/
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/ upper piston after stopping the engine drained to the exhaust manifold causing
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Leaking exhaust manifold gaskets allowed oil to /
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Procedures will be changed to prevent oil accumlations in /
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/ the exhaust and gaskets will be replaced.
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FACILITY METHOD OF STATUS
% POWER OTHER STATUS DISCOVERY DESCRIPTION (32)
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OPERATOR OBSERVATION
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ACTIVITY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITY (35)
LOCATION OF RELEASE (36)
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PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION (39)
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PERSONNEL INJURIES NUMBER DESCRIPTION (41)
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LOSS OF OR DAMAGE TO FACILITY (43)
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PUBLICITY ISSUED DESCRIPTION (45)
NRC USE ONLY
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810:200331 810814*"E OF PREPARER W. R. CARTWRIGHT PHONE (703) 894-5151 PDR ADOCK O$000338 0
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'. Virginia Electric andTPowee Company.
. Attachment: Page 1 of 5 4
'Northi Anna Power Station,' Jnit #1 -
- Docket No.'.50-338'
- Report No. LER 81-057/03L-0 Description of Event'
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Onj July 16,l1981,'with Unit I at 100 percent power, a small oil
' fire developed on.the exhaust manifold of the IJ es.ergency diesel generator.17 minutes.after it had been started for periodic testing.
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The.1J. emergency diesel generator was secured immediately and declared-inoperable..This event is reportable pursuant to.T.S.'6.9.1.9.b.
Probable Consequences of Occurrence
- The operability of off-site power sour'ces and,1H emergency diesel.
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were demonstrated.every 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> until the IJ> ersergency diesel generator was declared operable on July 18, 1981. The action statemeM of the LCO (T.S. 3.8.1.1) was met.
The public health and safety n ni not affected.
Cause of Event-Oil lickage from exhaust flange points _in the turbocharger regian caused a small oil fire. A representative from the Fairbanks Horse Engine Division of Colt' Industries was contracted to trouble shoot
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the problem. After examining the engine, he. stated-that excessive-oil accumulations in the exhaust was caused by' a failure to bar" the engine after shutdown.
The emergency diesel fs a 12 cylinder vertically opposed piston engine. During operation cooling ichrication oil flova through a 4
channel in the connecting rod to an area between the piston skirt and insert and out a hole in the insert. As the, piston moves from the inner dead center to the outer dead center position any. oil above the upper.
piston is thrown' eut into the upper crankcase compartment around' the upper ends of the cylinders.
This oil then drains either toward the blower or control end of the upper crankcase compartment and down to the oil pan. When the diesel'is stopped a substantial-amount of: oil accumulates above the upper pistons which stop near the inner dead center
. position..This oil eventually drains down the cylinder wall past the piston rings, into the combustion space, past the lower piston rings, into the exhaust ports, and into the~ exhaust manifolds. When the engine starts exhaust back pressure is initially high until the turbocharger turbine reaches terminal speed. The accumulated oil is forced out of any leaks in the exhaust manifold. To verify'that-the above condition was occurring, several therac. couples were removed. from
- - the IJ diesel exhaust ports after it had been shutdown for 14 days. Oil was found.in the exhaust system. During the last run the diesel-had been loaded greater than 75 percent for 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />;
- - thus, any oil in the exhaust at that time would have vaporized and wg
- - been exhausted.
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Immediate Corrective Action
An operator reported smoking oil on the exhaust manifold shortly i-before the fire broke out.
The Unit 2 SRO responded immediately.
Upon arriving in the IJ emergency diesel generator room moments after the initial report of smoke, the Unit 2 SRO found that a fire had developed. The diesel was stopped and the fire announced over the plant intercom system. Before the fire. brigade arrived, the Unit 2 SRO 5ad extinguished the fire with a portable dry chemical extinguisher.
The diesel was not damaged by the fire.
One-half hour after the fire the IJ diesel was started.
It ran normally in the loaded condition for five hours.
The diesel generator was returned to auto start, but was not declared operable until July 18, 1981, after a minor coolant leak (unrelated to the fire) was repaired.
Scheduled Corrective Action Procedures will bc changed to require cranking the engine over at least one full revolution 15 minutes after the engine has been stopped. This action will return any oil accumulated above the upper piston to the oil pan and prevent it from draining into the exhaust manifold.
During Unit shutdown of sufficient duration, leaking exhaust manifold gaskets will be replaced. Presently these leaks are minor and only a problem when oil accumulates in the exhaust manifold. With the actions taken to prevent exhaust manifold oil accumulation (see Actions to Prevent Recurrence) the present minor exhaust gasket leaks should not be a problem.
Actions Taken to Prevent Recurrence The same problem occurred on April 21, 1981 (LER 81-027/03L-0).
Two sources of_the exhaust manifold oil were suspect. One source could be prelubrication oil which can leak past the upper piston rings into the combustion region during the prelubrication oeriod (2 minutes at North Anna). The other source can be small amounts of lubrication oil normally found in exhaust gases. Normally oil from these sources would not be a problem rince they would be vaporized and exhausted to the atmosphere. When the diesels are run at light loads, exhaust flow and temperatures are substantially lower than during full lead operation. Exhaust temperatures and flows under light load conditions can be insufficient for complete vaporization and exhaust of oil from the two sources described above.
If many successive light load runs are made it is possible to accumulate oil in the exhsust manifold.
Based on the above analysis of the problem, operation practices were changed to load the diesels to at least 75 percent load for two hours whenever the diesel generators were started except when starts are expected every 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />. During operability checks conducted on a once every 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> schedule, the diesels are loaded -
to at least 75 percent load for two hours every other run.
Operation of the diesels as described above should prevent accumulations of oi,1 in the exhaust manifold due to the phenomenon described above.
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1 To ~ prevent oil accumulations above the ; upper pist'ons lfrom draining
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to the exhaust manifold after the engine has'been stopped, the. engine will be turned'over at least one complete. revolution 15 minutes.
'af ter the engine has-been stopped.
Turning the diesel engine over after it has been stopped and -
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i running the engine, loaded as described above should prevent recurrence.
l Oil leakage points will be cleaned of oil ' accumulations so any additional leakage can be detected and the success of the above corrective actions judged.
G_ene_ric Implications L.
Diesel en, tines similar in design to the emergency diesel engines used at No rth Anna can be expected to have similar problems. ;The
- - problem may not' appear until the exhaust system gaskets start to age, have beer thermally tycled many times, and develop leaks.
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| 05000339/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000339/LER-1981-001-03, /03L-0:on 810101,average RCS Temp Outside Tech Specs on Two Occasions.First Caused by Vol Control Tank Being Overborated;Second by Overcooling Primary.Steam Generator Blowdown Secured,Rods Withdrawn & RCS Diluted | /03L-0:on 810101,average RCS Temp Outside Tech Specs on Two Occasions.First Caused by Vol Control Tank Being Overborated;Second by Overcooling Primary.Steam Generator Blowdown Secured,Rods Withdrawn & RCS Diluted | | | 05000338/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000338/LER-1981-001-03, /03L:on 810318 & 19,nitrogen Supply Tank Pressure for Associated Pressure Operated Relief Valves Dropped Below Min Required to Operate Valves for Low Temp RCS Overpressurization Protection.Caused by Leaks in Tanks | /03L:on 810318 & 19,nitrogen Supply Tank Pressure for Associated Pressure Operated Relief Valves Dropped Below Min Required to Operate Valves for Low Temp RCS Overpressurization Protection.Caused by Leaks in Tanks | | | 05000338/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000338/LER-1981-002-03, /03L-0:on 801231,pressurizer Power Operated Relief Valve Declared Inoperable Because of Low Nitrogen Gas Supply Tank Pressure in 1-GN-TK-1A.Caused by Excessive Usage of Nitrogen to Cycle Relief Valves to Reduce RCS Pressure | /03L-0:on 801231,pressurizer Power Operated Relief Valve Declared Inoperable Because of Low Nitrogen Gas Supply Tank Pressure in 1-GN-TK-1A.Caused by Excessive Usage of Nitrogen to Cycle Relief Valves to Reduce RCS Pressure | | | 05000339/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000339/LER-1981-002-03, /03L-0:on 801230,w/unit in Mode 1,steam Flow Channel III Became Erratic W/O Any Annunciators or Computer Alarms.Cause Unknown.Channel Placed in Trip Condition, Calibr & Returned to Svc | /03L-0:on 801230,w/unit in Mode 1,steam Flow Channel III Became Erratic W/O Any Annunciators or Computer Alarms.Cause Unknown.Channel Placed in Trip Condition, Calibr & Returned to Svc | | | 05000338/LER-1981-003-03, /03L-0:on 810104,loop 3 Reactor Coolant Flow Protection Channel II,F-1435,found Out of Tolerance High. Caused by Voltage Drift in Flow Transmitter Serving Loop. Channel Recalibr | /03L-0:on 810104,loop 3 Reactor Coolant Flow Protection Channel II,F-1435,found Out of Tolerance High. Caused by Voltage Drift in Flow Transmitter Serving Loop. Channel Recalibr | | | 05000338/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000339/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000339/LER-1981-003-03, /03L-0:on 810104,casing Cool Tank Level Indication LI-RS-203B Failed High.Caused by Frozen Transmitter Due to Heat Tracing Failure.Transmitter Was Thawed Out & Redundant Heat Tracing Turned on | /03L-0:on 810104,casing Cool Tank Level Indication LI-RS-203B Failed High.Caused by Frozen Transmitter Due to Heat Tracing Failure.Transmitter Was Thawed Out & Redundant Heat Tracing Turned on | | | 05000338/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000338/LER-1981-004-03, /03L-0:on 801229,three Motor Operated Valves Failed to Actuate During Containment Depressurization Actuation Functional Test.Caused by Loose Lead on Breaker/ Controller & Water in Motor.Valves Repaired | /03L-0:on 801229,three Motor Operated Valves Failed to Actuate During Containment Depressurization Actuation Functional Test.Caused by Loose Lead on Breaker/ Controller & Water in Motor.Valves Repaired | | | 05000339/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000339/LER-1981-004-03, /03L-0:on 810104,during Mode 1 Operation,Flux Penalty Summing Amplifier Found Failed During Loop Calibr Check.Caused by Faulty NSA Card.Card Replaced & Calibr | /03L-0:on 810104,during Mode 1 Operation,Flux Penalty Summing Amplifier Found Failed During Loop Calibr Check.Caused by Faulty NSA Card.Card Replaced & Calibr | | | 05000338/LER-1981-005-03, /03L-0:on 810105,discovered That Control Room Floor Sleeve 1FC00108 Was Never Resealed After Being Previously Breached for Cable Installation.Caused by Failure of Personnel to Follow Procedures.Sleeve Resealed | /03L-0:on 810105,discovered That Control Room Floor Sleeve 1FC00108 Was Never Resealed After Being Previously Breached for Cable Installation.Caused by Failure of Personnel to Follow Procedures.Sleeve Resealed | | | 05000338/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000339/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000339/LER-1981-005-03, /03L-0:on 810106,greater than 12-step Disagreement Noted Between Individual Rod Position for Rod B08 in Control Bank D & Group Demand Position.Caused by Voltage Drift in Signal Conditioning Card.Indicator Channel Recalibr | /03L-0:on 810106,greater than 12-step Disagreement Noted Between Individual Rod Position for Rod B08 in Control Bank D & Group Demand Position.Caused by Voltage Drift in Signal Conditioning Card.Indicator Channel Recalibr | | | 05000338/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000338/LER-1981-006-03, /03L-0:on 810113,pressurizer Pressure Transmitter PT 1457 Found Out of Calibr.Caused by Instrument Drift. Channel Recalibr | /03L-0:on 810113,pressurizer Pressure Transmitter PT 1457 Found Out of Calibr.Caused by Instrument Drift. Channel Recalibr | | | 05000339/LER-1981-006-03, /03L-0:on 810107,w/unit at 1% Power,Average RCS Temp Less than 541 F on Two Occasions.Caused by Overfeeding Steam Generators Due to Feedwater Control Problems.Condenser Steam Dumps Closed & Reactor Temp Increased | /03L-0:on 810107,w/unit at 1% Power,Average RCS Temp Less than 541 F on Two Occasions.Caused by Overfeeding Steam Generators Due to Feedwater Control Problems.Condenser Steam Dumps Closed & Reactor Temp Increased | | | 05000338/LER-1981-007-99, Plug Found Missing from Tube at Row 1,column 12.On 810202,two More Plugs Found Missing.Caused by Bad Seals.One Tube Was Replugged on 810124.Other Two Tubes Replugged on 810303 | Plug Found Missing from Tube at Row 1,column 12.On 810202,two More Plugs Found Missing.Caused by Bad Seals.One Tube Was Replugged on 810124.Other Two Tubes Replugged on 810303 | | | 05000339/LER-1981-007, Forwards LER 81-007/03L-0 | Forwards LER 81-007/03L-0 | | | 05000339/LER-1981-007-03, /03L-0:on 801230,boron Concentration in Boron Acid Storage Tank C & Boron Injection Tank Below Tech Spec. Probably Caused by Inleakage of Unknown Source.Boric Acid Transferred to Tank C.Investigation of Leak Underway | /03L-0:on 801230,boron Concentration in Boron Acid Storage Tank C & Boron Injection Tank Below Tech Spec. Probably Caused by Inleakage of Unknown Source.Boric Acid Transferred to Tank C.Investigation of Leak Underway | | | 05000338/LER-1981-007, Forwards Updated LER 81-007/99X-1 | Forwards Updated LER 81-007/99X-1 | | | 05000339/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000338/LER-1981-008-03, /03L-0:on 810117,steam Generator a Protection Channel 2 Narrow Range Level Transmitter LT-1475 Found Out of Calibr.Caused by Voltage Drift in Level Transmitter Serving Instrument Loop.Recalibr & Returned to Svc | /03L-0:on 810117,steam Generator a Protection Channel 2 Narrow Range Level Transmitter LT-1475 Found Out of Calibr.Caused by Voltage Drift in Level Transmitter Serving Instrument Loop.Recalibr & Returned to Svc | | | 05000338/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000339/LER-1981-008-03, /03L-0:on 810107,primary Coolant Iodine Isotopic Analysis Not Made within 2-6 Hour Per Tech Spec Re Power Changes Exceeding 15% Per Hour.Caused by Failure of Operations Personnel to Follow Procedures.Sample Analyzed | /03L-0:on 810107,primary Coolant Iodine Isotopic Analysis Not Made within 2-6 Hour Per Tech Spec Re Power Changes Exceeding 15% Per Hour.Caused by Failure of Operations Personnel to Follow Procedures.Sample Analyzed | | | 05000339/LER-1981-009, Forwards LER 81-009/03L-0 | Forwards LER 81-009/03L-0 | | | 05000339/LER-1981-009-03, /03L-0:on 810107,during Leak Test Containment Personnel Hatch Outer Door Leaked Air Past Seals.Caused by Improper Fitup of Door Seals to Frame.Door Adjusted | /03L-0:on 810107,during Leak Test Containment Personnel Hatch Outer Door Leaked Air Past Seals.Caused by Improper Fitup of Door Seals to Frame.Door Adjusted | | | 05000338/LER-1981-009-03, Combined Leakage in Excess of Allowable Limits Noted from 14 Electrical Penetrations & 23 Valves.Valve Leakage Caused by Valve Seat Deterioration or Limit Switch Drift | Combined Leakage in Excess of Allowable Limits Noted from 14 Electrical Penetrations & 23 Valves.Valve Leakage Caused by Valve Seat Deterioration or Limit Switch Drift | | | 05000338/LER-1981-009, Forwards Updated LER 81-009/03X-1 | Forwards Updated LER 81-009/03X-1 | | | 05000338/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000338/LER-1981-010-03, /03L-0:on 810211,w/unit in Mode 6,containment Purge & Exhaust Isolation Sys Was Rendered Inoperable When Power to MOV-HV-100B,D Was Lost.Caused by Fault on High Resistance Connection.Defective Parts Replaced | /03L-0:on 810211,w/unit in Mode 6,containment Purge & Exhaust Isolation Sys Was Rendered Inoperable When Power to MOV-HV-100B,D Was Lost.Caused by Fault on High Resistance Connection.Defective Parts Replaced | | | 05000339/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000339/LER-1981-010-03, /03L-0:on 810113,w/unit at 100% Power,Overspeed Trip of Turbine Driven Auxiliary Feedwater Pump Occurred During Surveillance Testing.Caused by Failure of Turbine Governor to Control Speed.Governor Was Replaced | /03L-0:on 810113,w/unit at 100% Power,Overspeed Trip of Turbine Driven Auxiliary Feedwater Pump Occurred During Surveillance Testing.Caused by Failure of Turbine Governor to Control Speed.Governor Was Replaced | | | 05000338/LER-1981-011-03, /03L-0:on 810117,w/unit in Mode 6,loss of Power to Radiation Monitor Common Alarms Panel Was Experienced for Less than 5 Minutes.Caused by Failure of Electrician to Switch Power to Unit 2 During Unit 1 Trip | /03L-0:on 810117,w/unit in Mode 6,loss of Power to Radiation Monitor Common Alarms Panel Was Experienced for Less than 5 Minutes.Caused by Failure of Electrician to Switch Power to Unit 2 During Unit 1 Trip | | | 05000338/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000339/LER-1981-011-03, /03L-0:on 810114,w/unit at 100% Power,Breaker for 2-QS-P-1A Spray Pump Racked Out & Suction Valve MOV-QS-200A Closed & de-energized.Caused by Dirty Seat on Vent Valve. Valve Seat Cleaned & Disc Lapped | /03L-0:on 810114,w/unit at 100% Power,Breaker for 2-QS-P-1A Spray Pump Racked Out & Suction Valve MOV-QS-200A Closed & de-energized.Caused by Dirty Seat on Vent Valve. Valve Seat Cleaned & Disc Lapped | | | 05000339/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000338/LER-1981-012-03, /03L-0:on 810118,fuel Bldg Supply & Exhaust Fan Suction Dampers Switched to Failed Position,Bypassing Iodine Filter Bank When Control Bank Was Isolated.Caused by Low Outdoor Temp.Dampers Positioned to Exhaust Through Filter | /03L-0:on 810118,fuel Bldg Supply & Exhaust Fan Suction Dampers Switched to Failed Position,Bypassing Iodine Filter Bank When Control Bank Was Isolated.Caused by Low Outdoor Temp.Dampers Positioned to Exhaust Through Filter | | | 05000338/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000339/LER-1981-012-03, /03L-0:on 810121,containment Pressure Protection Channel 3 Failed Low.Caused by Blown Transistor on Loop Power Supply Card,Resulting in Power Loss to Each Comparator in Loop.Failed Card Replaced W/Calibr Card | /03L-0:on 810121,containment Pressure Protection Channel 3 Failed Low.Caused by Blown Transistor on Loop Power Supply Card,Resulting in Power Loss to Each Comparator in Loop.Failed Card Replaced W/Calibr Card | | | 05000339/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000339/LER-1981-013-03, /03L-0:on 810126,containment Hi & hi-hi Pressure Channel III Annunciator Energized.Caused by Instrument Drift in Nonisolated Power Supply Card S/N 5088,increasing Output Voltage.Card Replaced & Channel Calibr | /03L-0:on 810126,containment Hi & hi-hi Pressure Channel III Annunciator Energized.Caused by Instrument Drift in Nonisolated Power Supply Card S/N 5088,increasing Output Voltage.Card Replaced & Channel Calibr | | | 05000338/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | | | 05000339/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | |
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