ML20010C212

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Monthly Operating Rept for Jul 1981
ML20010C212
Person / Time
Site: Salem 
Issue date: 08/11/1981
From: Miller L
Public Service Enterprise Group
To:
Shared Package
ML20010C211 List:
References
NUDOCS 8108190249
Download: ML20010C212 (25)


Text

{{#Wiki_filter:. ..i AVERAGE DAILY UNIT PCh7.R LST.L N DOCKET NO. 50-311 UNIT Salem #2 DATE August. 11, 1981 CGIPLETED BY L.K. Miller TELEPHONE-609-365-7000X507 9 M0!GI July 1981 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY P0hER LEVEL (hWe-NET) (hME-NET) 1 205 17 336 2 211 18 409 '3 222 19 414 4 169 20 41s 5 211 21 393 6 133 22 406 7 94 23 91 8 0 24 380 9 0 25 277 10 0 26 195 11 0 27 380 12 0 28 511 13 29 29 449 l 14 229 30 139 87 415 15 31 16 208 p, 2 'of 26 g 8.1-7.R1 8108190249 810011' PDR ADOCK 05000311 R PDR

GWUGG CAM REPORT cocxET ro.: 50-311 cmz : August 11, 1981 m sy: L.K. Miller TJ2%NE: 609-365-7000 X507 enunc sTucs 1. Unit Name: Salem #2 noe, 2. ampartirq Period: July 1981 3. Licensed ".2===1 Power cett): 3411 4 Newsolate Rating (Gross fede): 1162 5. Design Electrical Rating (Not me): 1115 6. 14=w4m-Deparvishla Capacity 1 Gross fede): 1149 7. !*=v4== Dependable CWty (Not rese): 1104 8. If C2=9== Oo:ur in Capacity Ratings (Itase Nuzter 3 ' hrough 7) Since Last aspo-t, Give anastma N/A 9. Power Iavel M knich Best:1c::ad, If Any (Not feit.,: NONE

10. Roneces For Bestricticms, If Any:

N/A "his btinth Year to Date o m lative 744 5,087 11,256

12. nw=r of axrs Reactor was Critical 605.2 1,063.1

?,331.3

13. anactor asserve Shut 2wn sours 0.0 0.0 0.0
14. Hours Generator On-Line 541.3 619.9 619.9
15. Unit anserve Shut & wn Hours 0,0 0.0 0.0
16. Gross 2===1 niergy Generatadoes) 737,059 815,157 815,157
17. Gross Electrical Energy Generated 0es) 191.510 203.600 203.600
13. Not 5*1
  • ml Energy Generated 0es) 165,738 165,738 165,738
19. Unit Servim Factor 0.0 0.0 0.0
20. thit Av=41 *414_ty Factor 0.0 0.0 0.0
21. thit Capacity Factor (Using ftlC Net) 0.0 0.0 0.0
22. thit Capacity Fac. tor (Usirq DER Net) 0.0 0.0 0.0
23. Unit k road Outage Rate 0.0 0.0 0.0
24. 9=% Sc%1=a Over Next 6 btmths (Type, Date, and Duraticm of Each):

NONE

25. If East Dawn At Dui of Report Period, Estimated Date of Startig:

N/A

26. thits In hst Status (Prior to Ccasercial Opetion):

Forecast Achieved INITIAI, CRITICALITY 06/30/80 08/02/80 IN m aI, E m. w d 09/01/80 06/03/81 b l-7.R2 Pg.3 of 26 coecac:AI. craveICN 09/24/81 N/A

tNIT SIIL3KMNS ND ItME34 IU1CTI0tG DOCKET No.: 50-311 Salem #2 susurr turn July 1981 un1TiHAME: DATE: August 11, 1981 COMPLETED BY L.K. Miller 609-365-7000 X507 TELEPilONE: ft31tD OF 11mATI(N P"TINrl LI Q2EE SYSTEM (DRM2fr CAUSE NO (DRNCTIVE 10. DATE M (IK11RS) REASON DOWN EVENT GEE 4 01E5 ACTION TO IEACIOR I6urt i EMM RIEURIEN3 I N/A V. I 1 I i h I I I I t k i 1 2 3 4 5 F Forced Reason lethod Exhibit G - Instructione g t 1-Same Si schedalal A-Rpl[nent Failure (Explain) 1-Manual for Preparation of Data Entry Sheets for Lloemose B-ttsintenance or Test 2-Manual Scram. Event > port (tat) rite c-w rueling IFRegulatory Restriction 3-Automatic Scram. (NURIG-0161) [ 4 E-Operator Training & License Examination 4-Continuation of r-h hinistrative Previous Outage 5 G-Operational Error (Explain) n-other (Explain) 5-Load Reduction 9-Other 4 of 26 p.g. 8-1-7.R1 I'

DOCKET NO: 50-311 MAJOR PLANT-MODIFICATIONS UNIT NAME: Salem 2 REPORT MONTH July 1981 DATE: Auguct 11, 1981 COMPLETED BY: L.K. Miller ~ TELEPHONE: 609-365-7000 X507' o

  • DCR NO.

PRINCIPLZ SYSTEM SUBJECT 2EC-0759-RHR Shielding Addition Installation of shielding Around an Exposed 14' RHR Line 2ET-0780A Relay Room Ventilation Perform Tests 2EC-0784 Annunciators Add New Acknowledge Button to Existing Circuit 2EC-0808 Condensate Polishing Add Support to Gage Glasses for the CI 50 Tank 2EC-0836 Radiation Monitoring Diodes were added across various Relay Coils 2EC-0853 Main Steam Rework the Main Steam Flow Feeler ines to Provide a Takeoff in the Horizontal Plane for the High Pressure Connection 2EC-1224 Fire Protection Add Smoke Detectors 2EC-1268 Containment Level Addition of, Containment Licuid Level Recorders in the Control Room 2SC-0592 Main Steam Change Material of Part on 21 & 23MS46 l

  • DESIGN CHANGE REOUEST 8-1-7.R1 Page 5 of 26

DOCKET NO. 50-311 ' MAJOR PLANT MODIFICATIONS UNIT NAME: Salem #2 REPORT MONTH July 1981 DATE: August 11. 1981 COMPLETED BY: L.K. Miller TELEPHONE: 60c-365-7000 X507

  • DCR NO.

10CFR50.59 SAFETY EVALUATION 2EC-0759 The new shielding for the R.H.R. lines at El. 55' in the auxiliary build-ing is designed for the D.B.E., therefore an unreviewed safety question is not involved. 2ET-0780A This test will be conducted when #2 Unit is not running, temperature sen-sitive equipment will be monitored during the test and, if during the test, the te mperatures should approach the allowable limits stated in the test procedure. The test will be suspended and ventilation will be restored. 2EC-0784 This is not a safety related change and does not affect safety related equipment. 2EC-0808 This change will reduce the chance of a Pentron CI-50 spill, therefore this will not involve a USQ. 2EC-0836 The change only allows the original design to function as it was intended by preventing reverse current flow through the relay coils. This is not a safety related change and does not affect any safety related equipment. 2EC-0853 The change involves repositioning of the instrument lines to improve performance of the flow transmitters. No existing analyses are affected and no new concerns arise because of the change. 2EC-1224 This change extends the exist; ag fire detection eystem to cover additional areas of the plant. In doing so, it does not affect any safety related equipment. 2EC-1268 Addition of the recorder does not affect any environmentally related system so no USQ is involved. 2SC-0592 The replacement of the existing valve disc, MTRL A-105, does not alter the original design concept of the piping system in any way. Also, this change does not alter the Ibchnical spec. or the S.A.R. Page 6 of 26 o.

., _J. M _ . r._, ~ g 4 ~ _ _,. _ Q i' (; o _ SultTED BY... ..S#LEM. GENERATING STATION _.___ DATE 08/06/81 _._.._b OEPARTMENT, WODW DDnFR P;n. SAFFTY DEL ATF D rou l Pur te t nOdx HDOFN lng = IlNIT P PAGE 0601 l g lno::n 4 0:nED q j' NUMBER DEPT E 00 i P'4EN T IDENTIFTCATTON EMPLANATION nF nnWK PERFORMED y# (* Q# Nf 92R104 M SAFFGitARD EQHTP CnNTROL M ,4 Y, DESCpipTION nF PROBLFM, TRnURLE SHOOT Fit.E CARD MHICM WAS REMOVED

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$y' 7* FROM NO.18 SEC AND INSTALL NO.PR SEC n d CnWDECTIVF ACTInN, SEC CAR nPERATED IN PH WITHOUT A PRORLEM ' r Q r< 1.'- M P LS I M_ GEN R_ HI R_ LVL_ CN T R L._ 3 '~137610.

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DE9CRIPTf04 nF PDnRLEM, LEVEL DEVIATION ALARM !$ LTT ON MAIN CNTRL f PANEL HITH_. CORRECT _STM.GENR LIVEL. ._~ _ _ _ _.. ._h? I CnRRECTIVE ACTION, REPLACFD COMPARATOR s ?, C37612 M 24 SERVICE WTR PMP STRNR - l$ ( .P N _2_ _.. _ ,h . DESCRIPTION OF PRORLFM,__....w0N?T OPERATE,1N AUTO.OR.. MANUAL EVEN WHEN _,N RESET ?d( ' 7' _CORDECTIVE_.AtTIDN, R EPLA C E D. CDN T R OL_T R A N SF ORME R _____ _ __ ____ _ _ _._ l -nt ( l?1 937671 M 2A SERVICF WTA PMP GLND INJ '4 pd i f."i nESColpif0N nF PDORLFM, LINE LEAKING AT FLROM, DnMNSTREAM OF 76Snlo h(

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_ _ _... _ _ _.CnRRECTIVF ACTinN, RETHREADFD PIPF PUT DN TEFLON TAPE ___ d ?' 15 N ,%.._937709._._ M. _ .24 SERVTCE WATER PUuP ____._.M ';9 DESCRIPTIOP4 nF PROPLFM, PUMP MnTnR WAS SPWAYED WITH WATER. Ll C N .c l 'i CnRRECTIVF ACTION, PHYSICALLY DRIEn MOTnR HnHSING WITH R A(,3 MEGGERED MOTnu, WINDINGS, READ 1RO OHMS [J $ . sanuNo.. _ _ _. ____ _f; - y! w% a

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~ n-c - a = -. --_z a-5 g 4 j c1 e p t ..._ SD2 T E D 8 Y....~ -._.... SALEM GFNERATING STATION DATE.08/06/8L -}' DEPARTMENT, WORK UpDN Nn. SAFFTY REIATEn EQUIP *FNT >0RM ORDFR lng - UNIT 2 PAGE 0002 l* f tr 1 DRr - j', 02 DER - i,, j NUusER DEPT EQUIPMENT IDENTTFTCETTON EXPLANAff0N OF nqRK PERFORMED ' {' IN' 937777 M 2C O!FSFL ALARM 6 ,1 lj DESCRIPTION OF PRDRLFM, HIGH LEVFL ALARM ON OIL DAY TANK WILL NOT Fj, "M CLEAR WHFN THE TANK 15 AT NORMAL LEVEL Qh i CnRRECTIVF ACTION, REC ALIBR A TFD LFVL d b 937119 M 4_SER VICE_.NTR PMP._.S T RNR _b

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!h ' d nESCRIPTION OF P R f1R L F M, MOTOR DOESN'T RUN ___N lq CnWRECTIVE ACTInN, PHYSICALLY ORIEn ALL ELECTRICAL CONNECTION W i DRAINED WATER OUT OF CONDUIT THROUGH ( ,_CONDUI.I_COV ER S w as -A f 937771 M 2CV241, VALVE I nESCRIPTION OF P R T)R L F M, FOUND PLUG RLOWN OUT OF VALVE RODY c 4 CORRECTIVE _ ACTION, CHANGED _D' RING _T0_OPPOSIT_ SIDE,_ CLEANED ____ _ W ALL PARTS AND ASSEMRLED F l h( l 't$C37790.__-. M - .._21_ SERVICE WIR T R VL4G St.1N..-._ _ - -..~._.__ __.__ _ _. _ _. _ _ _ _. _ _ _ -d w nESCRIPTTON nF PRDALFM, HEAD SHAFT REARING GREASE CONNFCTION [U ( [, fWDKEN CORRECTTVF ACTION, REPLACEO GREASE rITTING

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n d .h"i 937791 O< M 74 9EUVICE WTR TWVLNG SCHN . DESCRIPTION _OF_ PROBLEM, HE.AD._SHAF.I._BEARI E LUBE CONNECTION LINE _ h RRDKEN P M ,t . - _. ~. .CORRECTfvF ACTION. . INSTALLED NEW.GHEASE FITTING.BECAUSE LINE. _.y COULO NOT RF REPAIRED F" l'i ( .p __g !h d ( _ _, _ _,4 )i 10( b g - ~ Y Page 8 of 26 ] L l

i h. . [j 0. i-0' h'[aSO21Fosv--.. S AL FM GrNFRATING STATION._.__.- _._.__ DaTE 08/06/81__.. u J' DEPARTMENT, wGPM 000EW wn, saFrty R E t A T F. O FQUIPaFNi a09m OWDFW LOG = UNIT 2 PAGF 0n03 p 1! (*' M ORv __l *' ll ORnE# NUMBER DEPT E001P"ENT IDENitF1 CATION FXPLANATION OF wnRw PERFORMED gi 7% [1 ['1 437742 M 27 9FRVICE wie TRVLNG St e 5 h _[j d .;5 OESCRIpif0N OF P909LFM, TNSTALL TURE ASSFMRLY 'M i -jd CORRECTIVF ACTION,-. _.. ..PUTa teEW GREASE FITTING.INTQ_ HEAD SHAFT __._ _ _ _ H ]f ' l"' REARING .n .hS37&48 a4 2WL99,_ VALVE jf .,9 i.a ' (j nESCOIPTTON OF PRORLFM, WILL NOT CLOSE FROM CONSOLE PUSHRuTTnN . rrj _.PEZEL-_. ..___.___._M ja 1 . h CORRECTIVE ACTION, REPATRFD REZFL SWITCH ) ( '( ,_, _p

,1 937857 M

2C EMFRG OIESFL in C tb.._.____.._____.._ DESCRIPTION 0F PRORLEM,._ _.._ PRE-LUME DIL PUMP FAILURE ALARM.WILL NOT _

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_ _____ _ __--__...._ CORRECTIVE ACTION, PEPAIRED FLON_3NIICH j! fN i" h( f' 937901 M 29 OlFSEL P _.._L__ .M Q( DE9CDIPTION OF P90RLFM, FAST AND WEST Top AIR STARTER APPEAR in RE 9 DRAGGING AND NOT HELPING TO START DIESEL ,d h.i w CORRECTTVF ACTION, LORRTCATED RACMS AND EXERCISED LINMAGE d ) M 2? SEDVICE WATER PUMP __ __. _.fd .L,_ 937903.. !h nESCRIATTON OF PRORLFM, DIL SIGHT GLASS LEAMS h

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';) CORRECTIVE ACTION, VENT CAP DN SIGHT GLASS Lon5E g 937953. M 21SW77,. VALVE. ~ ______] Q b H DEMCRIPTION nF PenRLFM, VALVE DnFSN'T SEAT DOMING RACMFLOW TEST

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g.... _.. = C A M pt f 302TEO.4Y-_.__.._._ SALFM GENFRATING STATION _ __._. _ _ _. _ - - - - DaTE 08/06/81 _ ___ DEPa#TMENT, WOQK nonEN V), S AF FT Y OCLATED F 0H I PwF ee f *0RM 000ER LOG = UNIT 7 PAGE 0004 l j ---~ _. t NU*RER DEPT EQUTPSENT IDENTIFTCATION FEPLANaTION OF hnRM PERFOR*ED []# . _. _. _ _.._ q3 p, ij h,# COROFCTIVE ACTION, INSTALLED NEW SPINF VALVE [%jj {; 03A152 M 27 SERVICE WTR TRVLNG ScivN ib _DESCRIFTION.0F PROMLFM,___ _.. SCREEN. WILL NOT _ w0RK _IN AUT0_DR_M ANU AL _. _ _.. _.._____._.._.._.j l. CORRECTIVE ACTInN, REPLACED PRESSURE DEVICE !il [ ,l.i fl 933155 M 27 SERVICE WATER PMP STONFR r f hfu __ _ ___.._ 0ESCRIPTION.0F PP08LEM,._ MHEN STRAINE8t.IS.IN_ MANUAL IT_ WON'T_8ACK. u 5 WASH DHE TO P2ShP4 NOT UPENING P1 ( f*if COR R EC T I V E._ A CT ION, RECONNECTED _AIRLINF fu 11 3 f ( f 932653 M 21 AUW RLOG 9HPPLY FAN i n 7' j" l FESCRIPTION OF PpqRLFM, CAN'T ST Al.T TRIPS nN OVERLnAD h b CORRECTIVE ACTION, REPL A CED _DVE RLD A D_S EI_ C( b 93R669. M 24 DE91DUE HEAT WEMOVAL SkP PMP k h M 'h*..__..-___..._..._ nESCOIPTION OF PWORLFM, PUMP RUNNING CONT]NUOMSLY h ]t _.._._._. CORRECTIVE. ACTION, REPAIRED _LD7755_AND_RECALIBHATED__ id ' . b'. 934894 M 27 CHILL WATER P H$8 P f"j .._.____.3-f oESCRIPTION nF PROPLEM, PUMP SEAL LEANING [a> l{n ____ _..__ COR R EC T I V E__A CT I ON, TNSTALLED NEW_ BEARING ___ ] 934648 M 29nP6.23Sw20,249W70, VALVFS 9 nESCRIPTION OF POORLFM, CHFCM LIMITORuuE DRIVES FnR WATER % ( '] i ____.___ ___ ___.__._ __ _ _ CORRECTIVE. ACTION, OPEN_AND. DRIED.0UT_THE DRIVE _ MOTORS._._ _ ______. _ _ _ _ _ g3,9a5 u 21991ft, VAlvF g"Q .,,4 b )

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'f f ,t. DATE.08/06/81 - $ .__. SO2 T ED A Y._.._ __. SAtEM GFNFRATING STATION. ~ l', (n j'l DEPARTMENT, WORM OROFR Nn. SAFriY REL 4Tt o FQllipvF4T NORM ORDFW lng = ttNIT 2 PAGE 0009 {. e M__ worn + P OInEO l', l* NUMRER DEPT E00TPMENT IDENTTFICATION EMPLANATTJN OF nnRM PERFORMED { i f DESCRIPif0N OF PRORLFM, VALVF LEAMS THRU j" A CnRRECTIVF ACTION, REPATRFD CUTS AND ADDED SPACE RING L. M.- _22CV1 % -. VALVE ~

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DESCRIPTTON OF PRORLEM, REPLACE nIAPHRAM ~1 CHANGE 0 ntAPHRAM ~ ] CORRECTTVF ACTIny, i'A t1 (c } Scoc72_ _ M.____ ___2R_01ESEL_GENERATDR k DESCRIPTION OF PRORLFM, DIESEL WILL NnT COME UP TO 900 RPM IN 10 I k f*' MEr m CnRRECTivE ACTION, REWIRED TURen SOLENOID VALVE 6 2 P 440473 M DIE 9EL GENER ARFA SMP POMP d P [ DESCRIP T ION _OF_Pm '8LEM, S UMP _ PUMP __DDE3_NOLDPER AIF p M f M CORRECTTVF.ACTinN, REPLACED FLOAT S W l'l8:H ASSEMBLY [ ( p i9 940476 M 2? Aur FEFD PHMR M. i, ( _. _._..._ D ESCR I P T ION. 0F _ PROB LEM,- DUTBDARD..PUMR_ BEARING lAN_OFF_THE_SHAET__ _ ___ 4 CORRECTIVE ACTInN, PUT EXTRA SET SCRE4 IN F AN, AND REPLACFD ( . GEAR. _ _.. _ Q( l"! 940592 M Ha-2372 HT TRACF CONTROLLFR ~ ~ ~ ~ 1 ESCRIPTION OF PRORLFN, PRTMARY SYS NOT MATNT61NING TEMP ,n m CORRECTIVE ACTInm, . RESET PRIMARY SETPOINi$ n L p. l"! 94060s M VITAL HEAT TRACING l, (. l* q Q( DESCRIPTION OF PRORLFM, AMMETER READING Lah { H L 'T .. _ _. _. y [> : L.' ( v( y Page 11 of 26

r - -aj D* p p 1 3 f8k 'Y j ':. SO2TFD RY-. .SALFM GFNFRATING STATION DATE 08/06/81 _l N DEPARi"ENT, WORK ORDFW W1 S AFFT Y REIATEn FuulPpFNT >Opn ORnF4 LOG - tlNIT 2 PAGE 0006 k f@ MORd f ORDER ,'f NUwaER DEPT EOUTPwENT 10ENTfF1 CATION FIPLANATION OF nnRN PERFDNMED [.) I __J I 00RRECTivF ACTION, REPATRFD BRONEN MPLICE {.. 4., fi 94063I M 22 SAFETv INJECTION POMP [ n d I ? __ __.____DESCR PTION OF PRORLFM,_._. _ DUTBOARD BEARING LOOSING OIL a i a i i: M CnNRECTIVF ACTION, TAPED DRAIN PLilG AND REPAIRED END COVER !gd GASKET. x f ,W 9 M 23 CHARGING PilMP fi-40635---- 3 ? DESCRIPTION OF PRnRLFM, DIL SIGHT CLASS LEAMS P b' CORRECTIVE ACTION, ADJUSTED _ GLASS _AND IIGHTEhED_NU13.. H f? b'940669 .______,..._h .M 21 FAN COTL UNIT F OESCRIPTION OF PRnALEM, UNIT TRIPPING 10 SECS AFTER STARTING IT F N $( - _ CORRECTIVE. A CT IDN, GREASED _ BEARINGS. W I" M '1 941482 M 2C SEC, INSTRU kl @ n m DESrRTPTION OF PROALFM, SEC iS IN ALARM M f ._)[j C -. _.. _. CORRECTIVE ACTION, REf. ACED _ CIRCUIT 80ARD_ CARD H 941557 M 23 SERVICE WATFC PuuP U( h _. ~ _. _. _ _.. _ _ji L 'l q 9 nESCRIPTTON OF PRn%FM, PUMP PACKING IS LEAKING __ _ _ _ _...__ _ __ _... __ _ C O R R EC T I V E.. A C T 10 N, TIGHTENED _ PAC. KING ~ [d h f.1 945469 M 24 9ERVICE WATER STRNR r' DESCRIPTION OF PDonLEM, L AD NkRE SHnRTEn ~ ' ~ ']L a n U f* .CONRECTIVE ACTION,..____RErf! RED _ MOTOR LEADS _ __ n f P 945434 W 24 9ERVTCE WATER PUwP Q Q-- -q H

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3p 1t. F t '... 30DTED 8f - _. - -_ _. .,aLEM Gr rnF R A T ING STATION.._ __ __ __ _ D A T E ' 0 8 / 06 / 8 L. _.._... DEPARTwENT, w0DK 000FW Nn. S AF F TY RELATFD FQUIPpFNT >URA DRDFR lng - UNIT 2 PAGE 0007 l p J i . _ _ _ _ _ _ _.. _. ~.. _.. [ f DEPT EQUTPMENT IDENTIFTCaTIn* FXPLANATION OF wnRM PERFnRMEn ' _.. NUM7;E R..---__ OESCRIP110N nF PRORLFM, PACKING LFAKS N 1 CnRRECTTVF ACTION, REPACKED STRAINER f g. _.4454R8_ _._ M 24 SERVICE _WIR_PMP_STRNR _. ~ _ _ _. _ _ _. ] f 'i DESCRIPTION OF PRnRLFM, 230V ACB TRIPS, STDAINER WILL NOT STAY IN 3ERVICE_ 4 'd CORRECTTVF ACTION, REPLACED SOLEN 0in COIL ~ ,h E i, ~ _ _ {' 4 27 COMPnNFNT CnGLTNG PUuP d'" 945572 g., D ES CR I P.T ION _DF_ P R OB LE M, 1NBOARn_. PUMP _ BEARING.LDOSE _I4_ HOUSING N 21 CORRECTTVE ACTION, ADDEO SHIM TO REARING TO RFMOVE EXCESS l C ^ F CLEARANCE.___ = C b 946715 M 21CV163, valve J'1" DESCRIPTION OF PROBLEM, REPAIR LEANS ON VALVE Ei ( t" CORRECTIVE ACTION,... _._. REPLACED.DIAPHRAM___ _... _. _ ___ _. _, _ __ _. _. _ _ _ _, [j h 9469R1 M 2FT-571, INSIDU w OESCRIPTION OF PRnRLFM, SENSING LINE HAS A LEAK DN WELDED P EL h FITTING $ ( d.J CDRRECTIVF ACTInN, INSTALLED NEW COHPLING Q M gC 4 947203 M 2TO-7322,_INSTHU . {h si 7' DESCRIPTION nF PDORLFM, REPLACF 2A DIESEL LURE NIL TEMP INDICATOR .00T.0F.DRYWELL. CORRECTIVE ACTION, PUSHED OFVICF INTO nRYWELL AND TIGHTENED k' f-SET _ SCREW o L l 6 C y h j ( s Page 13 of 26 t__.

y y f Ik w e d.. 303 FED RY_ _ SALEM GENERATING STATION _ _ _ _ _ _ _ _. _ _ _ DATE 08/06/81.. .J.# h DEPARTMENT, WORK ORDFR NO. SAFFTY RELATFn EQIflPurNT PORK ORDFR LOG - UNIT P PAGE 000R + v ED%K l'I O 0E0 DEPT EcufPuENT IDENTIFICATION EMPLANATION OF HORM PERFnRMED f lf NuwBER ('t.____..~_..__-.____._._-- _._ ~ 1 I N 947234 M POP 9, I N S T Rtl f,

1 PESCRIPTION OF PRORLFu, POPa IS OFF YET ON CONSOLE 2PR47 INDIC ATES f*.

OPFN ji CnetRECTivF ACTION, RFPLACED 2PR4T Cnll AND COIL MOUSING f 3 y G M _ 94254.9 M MP.Ai'LSERVICE _W4TER PUMP N W s 'E ' 6 f'_ DESCRIPTTON OF PRnRLEM, RERUILD PUMP FRO *e P3' bay s" M CORRECTTVF ACTION, RERUILT PUMP i F" 5 f*_ _926537 P c M AMN C L_.l e _IN S T R u 11 , 21 DESCRIPTTON OF PRnRLFM, TNDICATES HICH d k 9' Q P1 CORRECT!vF ACTION, RECALIRRATED INDICATOR _. _ _ _ _ _, _. _. _ _ - _. _ _.. _ _ _ _ -... _a LG H* _926541 P DN44,._INSTRU _. j . p) h N DESCRIPTTON OF PROPLFMe ISOLATION AMPLIF TER DUTPili OUT OF SPFC j. ._.____,.h j'j_...__.__.__._._____._.._. . _.. _ _ _.. _. ADJUSTED 10N CURRENT TO 2.500 VDC AND 5" p CORRECTIVF ACTION, h( q OUTPilf TO 10.0n0 VDC iw g. P' 226543 P 2RIac TNSTRU (* (A & [" DESCPIPTION OF.PR9RLFM. NO. DETECTOR RESPONSL j N MJ pk CORRECTivF ACTION, RECALIRRATED DISCRIMINATOR VOLTAGE {'; T26545 P 23 STM CENER FD WATFR Ch TROL h lid DESCRIPTION OF. PROBLEM,. . INVESTIGATE.CAUSE.OF. REACTOR. TRIP. __ __ ______.) N [

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. _ _ _ -. - p E s' t' ) .f U, A 3k.SODTEDBY.._. _ _. RELAftn Fuulp"FNi h0RK URDFR LOG - UNIT 2 PAbt 0009 .5ALEM GF'.FR A TING STATION __.... _ _ DATE 0n/06/s! ____ _ p. DEPARTMENT, WORM ORDFW W1 SafFTY .l, f FON b f DRDED Qj DEPT ' EQUIPMENT IDEP'T IF IC A T IOM EXPLANATION OF MORir PERFORFED Q j' _.NUuBE R ] nESCRIPTTON OF PRORLFM, RESET P0nER RANGF HIGH LFvFL TRIP SETPOINT F ____JO,.2C1_AND_P0nEH RANGL RDD.TO.651_.__. _ !1 pj" CORRFCTIVE ACTION, ADOUSTED NC307, Nc306 n y . 931852 P TARGET A r i ke FLlix DiFF RECORDER ]

1 a i f'

DES C R I P IION._ DF_ P R OB LEM, RESELDELT A. !_ RECORDER ' i f h' CORRECTIVF ACTION, REPLACED AUCTIONFER 4 h 932672 P 2PI-5?t, TNSTRH '..u 7, ?i" __ DES CR I P T 10N. 0F_.PR09 LE W, SENSING _LINLEIITINGS _LE AKING INSIDE P ANEL___ i CORRECTivF ACTION, REPAIRED SENSING LINF FITT1hSS $( 'f. ._.-._-J 'N-934614 P 29 S T *4 GENER FD FLOW CHP 'd .( '? DESCRIPTION.0F. PROBLEM, . FAILED _ LOW W y y h CORRECTIVE ACTION, REPLACED FORCF MOTnR. ( W m __]i j", 937549 P 27 FCCS ACCH 4 PRESS Al&#M ,g p F _...__ ____ DESCRIPTION _OF_ PROBLEM, _._ ALARM _IS_UP_.WHEN_ PRESSURE IS_IN_PRDPER__.._._.- _ _ __ _, d d' RAND .d CORRECTIVE ACTION, .RECALIRR4TED.. _ _ $q .+ ( (';937600 P 29 FCCS ACCOM PRESS ALARM 4 y ]( .M nFSCRIPTION OF PR0RLFM, ALARM TS tlP WHEN PRESSURF IS IN PROPER f* BAND q ' [1 _M CDRRECTTVE AcTInN, RECAL1RR4TED ('j ] ., ( ,i j i( L 937607 _P _.__IEMP DEVIAIION ALARM.__ f1 C ( e O q' ( 'M L

w L _..

Page 15 of 26 i

. ~... m. -) ( [,1 ld/ e SALEM GENERATINC. STATION- _ _. DATE OR/06/81..-.--- . L SO2TED BY ___...._ - _.___..- DEPARI"ENI, hnRK ORUF4 NO. SArFTY RELATED FQUIPmFNT WOEM URDER LOG - UNIT P PAGE 0010 l,' j w -- N - - '_ JDRF ORDED Q, DEPT EQUIP IDENTIFICAIION EXPLANATION OF knRW P E R Fn'1ME D .q ____"ENT. _ ~. ...- } 8 NUu8ER '6___ b DESCRIPTION nF PRORLFM, IN ALARM j CORRECTIvf ACTInN, REPLACED SIGNAL ISOLATne d H g',_ 937h30 P 243F40a_VALVF ~ 7p s "l DESCRIPTION nF PRnRLFM, NO OPEN INDICATInN ..s CORRECTIVE ACTION, ADJUSTED LIMIT Sw!TCH_ p h._._937 631 P 238F.4 0,_V ALVE_. _ f)l

fn DESCRIPTTON nF PDORLFM, NO CLOSED INDICATInN h

h4 N C0dRECTIVF ACTInN, ADJUSTFD MICROSnITCH 11 hI f 937t;48 P !_ LOOP _ LOW FLDn ALARM -. _ _ _ nESCRIPTION OF PRORLFM, LOW FLnu OID NOT COME IN WITH TNF RCR

M ha i"

i ~ CORRECTIVF ACTION, REPLACED COMPARATOR ![ 1 ' q .___.__..) 't _937658 _ _~P._.__ 21 CVCS. HOLDUP TANK LEVEL.IND... nESCRIPTION OF PRORLFM, LEVEL 20-301 0FF W W 7 CORRECTIVF ACT!nN, CALIRRATFD ALARM AND INDICATOR - I a _.937691.__ _ P _._ _21 STM GENER FD Flow CH2 'U I 1 DE*tCRIPTION nF PRnRLFM, CHANNEL FAILED Low bA _ ___ ? CnRRECTTVF ACTInN, RECALIRRATED SQUARE ROOT EXTRACTOR Qw . 937702 _ P. .2R178,-INSTRU. _ _.g d ( I DESCRIPTION OF PRORLFM, PUMP HAS LOW FluW, AND MnNITne FAILEn ed CARRECTIVF ACTION, REPLACED MC4800 CHIP, DEVICE SELECTS [ ( INTERNAL AND EWiFRNAL NATA LINE RUFFERS r, a P j . _ _,l V be )b M' r _ _.m Page 16 of 26

_~,2 h_ [ b y ' r c k 9i__ S03 T F D B Y. _._ _ ~ __ SALEM GENERATING STATION._ DATE 04/06/81 T F nEPARTMENT, 40pK 090FR NO. S4Friv REL ATED Fotfl PwF r.T PORK ORDFR LOG - UNIT 2 PAGF 0011 I en;;g b l' OKDED F' NUM3FR DEPT ECOTPMENT IDENTTFTCATTON FXPLANATION OF nnRM PERFORMED + n q$ b h "i 937809 P 28 STM GENER FLOW CH4 ,r DESCRIPTION OF PRORLFM, CHANNEL IS SPIKING q 'd CORRECTIVF A C T ION,_ ____._. _ T IGHTEN FIT T f fags, _RLENDOWN SEleSING LINES .. y h E M 937810 P A tl X FD PMR CLAMP! TRON w [ DESCRIPTION OF P R O M L E **, 7ERO CLAMPITRON f _ ___ _ ___ CORRECTIVE ACTION..__ ZERDED.CLAMPITRON- _ q'a 'p E 937612 P 24 REACTOR ConLANT LOOP CH2 r [6 F DESCRIPTION OF PR09LFM, CHANNEL INDICATES HIAMER FLOW THAN CM1 4 f AND CH3 M J'._ __ CORRECTIVF ACTION, RLFhDOWN TRANSMITTFR SFNSING LINES j h dC 937841. P. 22AF21,_ VALVE. y g., f nEMCRIPTTON OF PRORLFM, DEMAND INDICATION WILL NOT EXCEEn R52 i,4 1_._--____-__.. }d M ]*._937854 _ ___P 24GP8,... VALVE ___...___ _ __ _ _ _ __.__ _. j DESCRIPTTON OF PRORLFM, NO CLD9ED INDICATION h,j ; r 4( p , _ 937868 P 2 R 1 R B e._IN S T R O ___. j1 DESCDIPTION OF PRnRLEM, MONITOR ALARMING ERRONEOUSLY .q b 5" n__ j" CORRECTIVE ACTION, REPROGRAMMED AND AnJUSTED MONITOR [ f ). ( ( L 937869 P 2 R 19 C,,. I N S T R U ____ .y nE9CRIPTION OF PRORLFM, MONITOR ALARMING ERR 0NEntlSLY ( "L._.__._._. ..t w t N [h q Nf y Page 17 of 26

I ^

g f.)

[; s ' 6 q! >s 'L _ S O2 T E D B Y -___ _.. _ __ _ _- -_ _.. _. SALFM. GENERATING STATION.____ DATE 08/06/81 _ _i

  • 0RM 000FN Nn.

S A F f" T Y DELATEn FOUIPwFNT h00R ODOFR LOG - UNIT 2 PAGE 0017 .'q' DEP ARIMENT, j *,.C rnen P OODER DEP EQUTP IDENTTFICAff0N EXPLANATION OF knRM PERFORWED {?qI j' .NUwSER.- _ _ _'___,_ _"ENT_ _ _ _. ._.____r< ,i %. i I kl" CORRECitVE ACTION, ADJUSTED SETPOINTS AND REPAIRE0 P/S j 937831 P 2?SW122, VALVE

h..

-.__._ DESCRIPTION 0F. PROBLEM __._ _ VALVE.DNLYIOPENINfn PARTIALLY _ _. 2 _. h m CDRRECTTWE ACTION, FOUND VALVE nN HaNnJACM k b* 1 q?r l" 937884 P 21 FAN COOLER UNIT w ___ DESCRIPTION OF PROBLEM,. _.____UNARLE_.TO. EXCEED 2100.GP'4 IN Low SPEED .__._...___u._h ,h,_ q h CORRECT 1vF ACTION, ADJUSTED SETPOINTS ON HIf;H FLOW CONTROL C ,) N 937916 P 218F19 CNTRL, INSTRO P DESCRIPTION OF PRORLFN,. -_ _ NOISE ON CONTROLLER.1LC-500E w

'd F'

CORRECTTVF ACTION, REPLACED SIGNAL TSOLATOR 2LM-505C w!TH IC A NOTHER_ BENCH _C ALIBR A T ED_ UNIT j r H C di P PPS1, VALVE f 939491,. DESC#IPTION nF PRORLFMe CANNni GET OFMAND SIGNAL TO READ LESS THAN _.y]C 9 F 40 p. P CORRECTTVF ACTinN, REPLACED OP-AMP P4jC M i.".. _9 3 3 619._. -._ P. .2CV7, VALVE d., al DEMCRIPTION OF PRORLFM, VALVE CLOSED FOR NO APPARENT RFASON M y n [B CnRRECTivF ACTInN, ADJUSTED LIMIT SMITCH h). 938651 P DELTA I RECORDER [ m H nESC#IPTTON DF PRaPLFM, DELTA I PEN ON RFCORDER HAS FAILED Lnw [ 6 _ _ _ _. _ _ _ ~ _ _ -..... 4 C G A LL_ _. - _ .._.3 m M N G ?,.l ,s4 g. b A Page 18 of 26

m.. g. _. _. __ _ ~ I 11 ^ L

j'._ SORTF0 BY SALEM.GFNFRATThG STATION..__. _.. _.

DATE 08/06/81._ [ nEPARTMENT, MORN OOOFW Nn. 9AFFTY #6 LATED FQUIPwFNT WOQK HOOFR LOG - UNIT 2 PAGE 001'l l 1 rnin 0%DE9 i]# Y l'. NUMBER DEPT EcuTPMENT IDENTIFICATION FxPLANATION OF nnRx PERFORME0 h j 940449 P 21 FAN COTL UNIT Q DESCRIRTION OF PRORLFM, SERVICE n4TER Flow LOST p, w d W bs ._. -._. CORRECTIVE ACTIDN,.__ BLEW.ROTH. LEGS.DonN. _ _..__ _... [h# h 940531 P 22 MTEAM GENERATOR w 'h. -D r DESCRIPTION OF PROPLEM, NOT SMUTOOWN PANFL IMOICATES HIGHER THAN CONTRUL ROOM INDICATION $f ] _.__.._..__.._._a f,.. P CORRECTIVF ACTION, REPLACFD INDICATnR $ ( l'j N ? _9'10596 R REACIDR_.MTER._STOR AGE I ANK l" m h DESCRIPTION OF PRORLFM, LEVEL CHANNEL D HAS FAILFD )( L jr 9 CORRECTIVF ACTIDN, REPLACED METER MnVFMENT ?, ( p 930597 P >R 128. INS T R11 f nESCRIPTION OF PRORLEM, TNSTRUMENT FAILED w CORDECTIVF ACTION, CLEARED RAMS AND PUT IN SETPOINTS P A ? _ 940303 P 2R198,_INSTRU nESCRIRTION OF PR0RLEM, INSTRUMENT FAILED i} V j i"', CnRRECTIVF ACTION, CLEARF0 RAMS, PUT IN SETPOINTS AND [ 40 JUSTED UNIT f] F _1 ,]( 440608 P ROD POSITTON INDICATION o( f'j'i... _ DESCRIPTION OF PROBLEM,_ _ _. BEZEL. INDICATION L0ut.nITH RESPECT _TO __ ._________m_.m DEMAND POSITION h (* ____ CORRECTIVE.. ACTION, CALIBRATED _ INDICATOR y f.'.; 1 .d h i ._ ___ _[.; u h.,_ U Page 19 of 26

_ _.. _ _ _ _ _ _ _ ~ ~. _.. _. _ _ ~ _ 1 k r 5 SO2TED 8v _._. ~ _ _-_... _. S ALb'M GENERAf!NC STATION.._ DATE 0 8 / 06 / 81. __. __. ; ' DEPAoTMENT, WORK ORDER No. Sarriv RELATEn FQUIPMFNT *0RN ORDER LOG = tJNIT 2 PAGF 00I4

j a.

k ORDER

l. #

NUM3ER DEPT EQUIP"ENT IDENTIFICATION EMPLANATION DF n0RW PERFOR"ED 's__.___ f-940639 P 21 STM GCNER FD FLOW CHP c 1 jI 1 DESP (ION OF PRORLFM, OUT OF CALIBRATION h 1 CORRECT ! vE ACT 10N.-___ REPL ACED. ISOL ATOR __ - - _g p' 940643 P 2RIPR, INSTRU whj DESCRIPTION OF PRORLFM, INSTRugENT FAILED H _ _._._ CORRECTIVE ACTION, _ REPLACED ALL.2101 AND_.5101_MEMORT.IC'S _._. _ __ __ i_g REPROGRAMMED MEMnRY _910*,88 8 9PNI_F11EL PII_.HE_DuTLET_ FLDu 1, DESCRIPTION OF PRORLFM, INDICATES 1000 GPM w!TH MEAT EXCHANGER F- _ _2 ... ISOLATED __ _ __ uMM k CO R R E C T I v,-

ACTION, FOUND SLIGHT RESISTANCE IN LINNAGE i$(

.as .h [I I C41414 P 2RI6, INSTRU ',1

  • 1 DESCRIPTION OF PROPLEM, __ _.._ND_ SCAN ______ _

..,__.____.H w i CORRECTIVF ACTION, REPLACED SCALOR 3 i

V]I 945463 P

245W24, VALVE Q1 DESCRIPTION OF PRnRLFM,._ __SDLENGID BURNED UP.~ __.~- 7 kd a. 3 '! CnRRECTIVE aCTInN, REPLACED COIL (c m y( fi 9458R5 P 24G48, VALVE W ,- ] DESCRIPTION OF PRORLFM, 05 LIGHT WILL NOT.LIGH1 nHEN. VALVE _IS.. _. ( n il _ __.. CORRECTIVE. ACTION, ADJUSIED_ LIMIT _. SWITCH _ __._ t' e ?( @k.__ _. - _- .__.-__._..JF . 9 d( ph ..___ ] y k Page 20 of 26

' ~ ' ' ' L O 4 k r .S AI FM GFNFRATTNG STATION-_ -__ --... DATE 08/06/81_ _..__, iL 903TFD RY_ - 9 AF Fiv RFL ATF D 00lflPaeFNT #04n ORDER LOG - HNIV P PAGE 0015 g g nEPARTMENT, WORK 000FW Nf). V, Qp l' I.l O 0% DER NU"8ER DEPT E00iP*ENT 10ENTTFICATION FRPLANATTON nF nDRM PERFOR"En b di., O 'l 94%527 P 22MSIO CNTALLER, IN9TRU {,' O DESC#]PTION OF P P O R L F **, THE VALVE DEMAND PEGS LOW WHEN ADJUSTING L THE SETPOINT 3 ) 1 9 CORRECTIVE ACTInn, REPLACEO MANUAL /AUTH STATION A O -_tt 55p .F 2a._5IEAM. GENERATOR ,t C " O DEMCRIPTION OF pp0RLEu, thDICATES 121 HICHFR THAN THE CHANNELS ON _ _ _. _. ~. _ _ _.. .. _ _ __ _. A LL D T H E R. G E N E R A T OR S _-. _ _.__...._. ]fC CnRRECTIVE ACTInN, CALIRRAfED THE BEZEL INDICATOR N j f{' >{ E5577 P 21 REACTOR COOLANT PUMP C .DESCRIPTf0N OF PRORLFMe.._..._ _ ND _INDIC A TION _IN C0r4 TROL. R00M ON THE. LOWER _ _._.__,________.id MCALE 9 C 1* -_ CORRECTIVE _ ACTION, REPLACED._IRANSMITTER 'L !. C P 2R178, TN9TRU _445601-.. ~ -__-_..q n yCo "t ~ CORRECTIVE ACTION, _ _ REPAIRED BROMEN_NIRE _ REPLACED _865T_AND_____. M862CD MC _94%%5._ .P. __.. 2?MSI A, VALVE )C '1 nESCRIPTION OF PRnRLFM, DEMAND INDICATION SH0h3 tot OPFN, VALVE fS_CLUSED .]

1. $(

CnRoECTTVr ACTION, REPLACED METER MnVEMENT ,4 t"% Ily [. oo'inet P 214910, VALVE L (6 7 _ _ __ _ _ Qd M 4 (t 9 q N F .ie y

  • ~ y-Page 21 of 26 4

k

'7 a f SORTED SY. _ _ _ _ _. - - _ _. - _ . SALEM GENERATING. STATION DATE 0A/06/81 -

  • l DEPARi"ENT, WORM ORDFW NO.

SAFriv pELATED FOUIP*FNT h0Rn ORUFR LOG - UNIT 2 PAGE 0036 E .nw 0:0E0- [ Huur.ER DEPT EQUIP"ENT IDENTIFICATION DPLANATION OF wnRK PERFORMEn DESCRIPTION nF PRORLFM, VALVE CONTROL FATLFD TO MANUAL AND OPENED q VALVE TD_1201_DE"AND. CORRECTIVF ACTION, RRPLACED AUT0/ MANUAL STATION-3 _ _. _ _ _ _ _ ~ 1 f,4 9C%r,54 P 23MS10, VALVE [- G nESCRIPTIDM_DF PRGBLEM, VI.LVE_ CON T ROLLER _HO TJOR KINr. i N 4 f* CORRECTTVE ACTION, REPLACED CAPACTTOR 'f' [47 r s [G 946965 P 27 Siw GE*fER FD Flow TRANS _DESCRIPT_IOM_ DF _. PROBLEM. T NS TR U"EN T._PIRING_LE AKING. 0VER_0THER .d ' FEEDWATER TRANSMTTTERS t '. ;. - y . ; (o h,1 CORRECTIVE ACTION,..___ _ REPLACE _ MELDED. FITTING,.ALSO REPLACED._. __d + SENSING LINES q b 97.4972 N42,_ CHANNEL 2_nIS 5 h,) y l" nESCRIPTTON OF PROBLFM, DELTA FLOW INDICATOR NEEns AnJUSTING p f CORRECTtvF ACTION, ADJUSTED DELTA INDICATOW i"._ 947019 P 2R418,__INSTRU M y 1 N DESCRIPTION OF PRORLFM, INVESTTGATE NO SCAN TO COMPUTER CPH ? ?C m _d F CORRECTIVF ACTION, READJUSTED COMPONENT AND CLEARED NO SCAN M i V@ 94703& P DR418,_.INSTRU DESCRIPTTON OF PRORLEM, NO SCAN b lF_ 2 ? CnWRECTivF ACTION, REPLACED 8661 MODULE G P 2R11A,_INSTRU d h937039. H

e Q._ __ -._.. _.--. _. _ _

s G [, h 4e _. _. ___ _ _2 b Page 22 of 26

7 m. .[ b O ] f a.- SALEM.GFNFRATING. STATION._ DATE 08/0 Met _. ) . SDDTED 87.. _. nEPagyuggy, popg opDFk AO. S AF8 TV #FL ATEn FullIRwFNT PORN UDDFR LOG - IINIT 2 PAGE 0017 Cg h. f' IADRm }.} p 0;DED' ' 'i NUMT*F R DEPT EnUTP"ENT IDENTTFTCATION FMPLANATTON OF p nR et PFRFORMED q l'l.. -, - - m C DESCRTPTTON OF PROPLEM, LOW VALUES, NUT OF SPEC ? ADJUSTED DETECTOR PLACFMFNT AND VOLTAGE ,qp CORRECTtvF ACTION, { b m i P_ STM DUMP.TURa_ TRIP _AND.LO RFJT_ _ _ _ ___g

".1_C17101 a

DESCRIPTION OF PROPLFM, CHANNEL 00T OF CALTHRATION h f j'1 m A REPLACFD LEAD LAC [ Ti CnRRECTTVF ACTIDN, .i, f .C37123-P 2P128.. VALVE _ ( !N nESCRIPTION OF PRORLFM, CHANNEL FAILFD ..a x F H: C3 RECTive ACTiaN, REPLACE ICao-PRnCE==0R AND

  • Ra=

M (z m N _C37126 _ P._ 2Ne3._PDWEN_NANGE. ._j a* DESCRIPTTON OF PRARLFN, DELTA FLUlt NFTER UN CONTROL CONSOLE NUT OF $( h" S P EC_. M( s US CDRRECTTVF ACTION, ADJUSTED INDICATOR [ ( J h. _ _._ __._.. _ _ _ _. _ _ _. _ VFNT RECORDFR f< 947127 P PLANT m Y __ _ DESCRIPTION _OF_PROBLEH. CHARI. DRIVE NOI_WDRKING _- ? N,

'i" COPRECTTvF ACTION, REPLACED CHART DRIVE 40 TOR i

u M F 947129 P 2049, INSTPil &( I j"' 4 D ES CRI P ilD*LOF_.P ROB LE M. REMOVE _EILTERSJROM_2R11 A_ANQ_2R12BJOR_.._._ k~ COUNTING RY HP hf M._..____...._._..-. . CORRECTIVE ACTION..___.___TNSTALLEn NEW.FILTFRS .J C I I. P TAVC TNDICT ON L0nPS 21-22-23-24 m 947151 n /H - DESCRIPTION OF PRnRLFM, CHECK CALIRRATION T'r 5 "I__.___..._-.._-. _ _ __. 4' w t )d 0( .H 'M --Page-23-of 26 l-

A. _.. _ _ _... _ _. _ _ _. _ ~ __ _ _ _. _ _ _ _ _ _.. _ _. _ _ _ _ _ _. _ _ __.. - _. _ _ ~ _. _ - -. C r i ll A O DATE._08/06/81 .._ P SALEM GENFR& TING STATION ___ PAGF 00tR I '....__ 3 02 T E D. 8 Y. --_ _. __. _ __... _. REL A TF n F fJIIIRwt NT *0R4 HWDEN LOG - IINIT 2 O 3l DEPART *ENT, WORM OODER No. SAFFiv i '} _ J.* 9 un.w >d6 8j nRDED ENPLANATION OF MORK PERFORMED NUNCER DEPT FQUIP"ENT IDENTIFICATTON 'L__..._____.____.... b 1 CnRRECTIVE ACTInN, RECALIBRATED '.h "i {' 'CG7152 P TavG nEVIATION ALARM 11 6 DESCRIPTION OF PROBLEH, _ _ _ AL ARM _t S. UP.. ON _ CONSOLE. h .a 7J k + CORRECTIVF ACTION, REPLACED SIGNAL isnLATOR y d 'C47154 P REF TAVG RECnROFR ]6 j) _ -. - _ _ _ _ _ _ _. _.. _ __. DESCRIPTION OF.PROBLFM,_. RECORDER IS. READING _ LOW _ ...__ __. _ -. _ _ _-_ _ _.... _ _. ___ q .;j 6 p M CORRECTTVF ACTION, RECALIRRATED in P (g w } C'J7155 P TURR TRIP AtfTO STOP OTL SWTCH

d_

DESCRIPTION OF.PRORLFM,_-_ _.FOUND OUT_OF SPEC. -. _l w x CnRRECTIVF ACTinN, ADJU9 FED PD-455 AND 826 [k M CQ7156 P REACTnR WTR STRG TANK LFVEL

-{._.___._.._.____-

DESCRIPTION OF PRORLEM,_____-_ CHANNEL..FOUND_00T_OF_ CAL 18 RATION . _. 4 3 k CORRECTIVF ACTION, REPLACED SIGNAL C0wPARATDR M Q [*i ~M.__._____.__ DESCRIPTION OF PRORLEMe.._._.FL0n READING HIGH_..._ _ _. _ _ _ ___. _. _ _ _. _ h C47157 P 24 ST4 GENER FLOM CH{ M M)4

  • n CnRRECTivF ACTIDN, ADJUSTED PFM-5429 y

M 447158 P 22 STM GENER FLnd CH2 '.I % 'b DESCRIPTION DF PROPLFM, RESET FOUND OUT OF. SPEC _.. _ _ _ J h" N( '1 .i hb C f'R R E C T I VF ACTION, CALIRRATED BISTARLE W [

("'

CnLn LEG LOOP 24 - 6, ( ' {' 907159 P L _ _ _.. nESCRIPTION OF PRORLFMe._ LOOP.FOUND.0UT OF CALIRRATION_ __ ____ _ _.dj L s h ( h g D y

F As b

W _ ~ Page 24 of 26 i

--.. _ _ - ~ I: . ~. e _3ORTED BY. SALE *4 GFhf4ATif.G STATTON DATE 0 A / 06 / 41.. PAGE 0019 'j DEP API'8tNI, WHQ% UROF 6e Ain.

  • L A F F i f QEt ATEn F RHIPwF Ni 90pd (JWpFW lng = UNIT 7 r.

s. 1 h i__EDRK lC ntDER FxPLANATION DF WORK PFRFORMED ) MuuqER nEPT. EcutPwENT InENifFTCATION Dl .2__ 3A CORRECTIVE ACTinN, MADE ZERO AND SPAN ADJUSTMENTS y '{ '1 A n

i. 447140 P.

TRATN Re INSTRU DESCRIPTION OF. PROBLEM __. LOGIC _A.. SERVICE WATER _.POSITIDnER.1. CHECKS-._ _ ____... s. RAD l b CORRECTIVE _ACJION, _REPLACEILUNIVERS AL_BD ARD - mH 3 s p> - G 1 m .a J I _TDTALLLINES_ s.000385._ _. ) O TOTAL A-RECS = 0n0111 '.i - l v j ASI__uPnAIF .y e O '" il @ 810806 = l- ? t13754 ' [ _ E*JTER COMMANDS O q END OF RUN h y Jg n

seIRPT PRINTS r

t"1g x p 3( p = - - c .i u 3 44 ,, q H f. ti 4 i: ~ ? 6 M , w F4 S C 4 g i , n y l[ Page 25 of 26

REFUELING INFORMATION DOCKET NO.: 50-311 UNIT: Salem #2 DATE: August 11, 1981 COMPLETED BY: L.K. Miller TELEPHONE: 609-365-7000X507 i MONTH: July 1981 1. Refueling information has changed from last month: _O X YES N 1 1 2. Scheduled date of next refueling: January 8, 1983 1 3. S:neduled date for restart following refueling: April 3, 1983 4. A. Will Technical Specli'ication changes or other license amendments be required? YES NO NOT DETERMINED TO-DATE, July 1981 B. Has the reload fuel design been reviewed by the O ation Operating Review Committee? YES NO ( If no, when is it scheduled? December 1982 5. Scheduled date(s) for submitting proposed licensing action: December 1982 (TF nonnirna) 6. Important licensing considarations associated with refueling: NONE =- 7. Number of Fuel Assemblies: A. In-Core 193 B. In Spent Fuel Storage 0 8. Present licensed spent fuel storage capacity: 1170 Future spent fuel storage capacity: 1170 9. Date of last refueling that can be discharged to the spent fuel pool assuming the present licensed capacity: March 2000 Page 26 of 26 8-1-7.R4 .}}