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Category:TECHNICAL SPECIFICATIONS & TEST REPORTS
MONTHYEARML20210H2901999-07-30030 July 1999 Proposed Tech Specs Pages,Extending Operation of RBS from Current Licensed Power Level of 2894 Mwt to Uprated Power Level 3039 Mwt ML20205P8701999-04-15015 April 1999 Proposed Tech Specs,Implementing Bwrog/Ge Enhanced Option I-A (EI-A) Reactor Stability long-term Solution ML20205L7321999-04-0808 April 1999 Proposed Tech Specs,Removing Notes That Refer to Specific Cycles,Per LAR 1998-15 Re Change to TS 2.1.1.2, Reactor Core Safety Limits ML20206R9351999-01-12012 January 1999 Proposed Tech Specs Re Refueling Equipment Interlocks Required Actions ML20199C1881999-01-0808 January 1999 Revised Page 7 to Rev 13 of RBS Security Training & Qualification Plan ML20198E8091998-12-16016 December 1998 Proposed Tech Specs Pages Re Change to TS Safety Limit 2.1.1.2,changing Two Recirculation Loop MCPR Limit from 1.13 to 1.12 & Single Recirculation Loop MCPR Limit from 1.14 to 1.13 ML20196A1401998-11-20020 November 1998 Proposed Tech Specs Adding 3.10.9, Control Rod Pattern - Cycle 8, to Support Startup from Outage Planned for Early Dec 1998 ML20154H3691998-10-0808 October 1998 Proposed Tech Specs Implementing BWROG Enhanced Option I-A Reactor Stability Long Term Solution as Documented in NEDO-32339,Rev 1, Reactor Stability Long-Term Solution, Enhanced Option I-A ML20153H0311998-09-23023 September 1998 Proposed Tech Specs Changing Specific Gravity Acceptance Criteria for Div III Battery ML20153E8111998-09-22022 September 1998 Proposed Tech Specs Deleting License Conditions Associated with Transamerica Delaval,Inc EDGs ML20217J0951998-04-21021 April 1998 Proposed Tech Specs Bases Update Package for Revs Implemented Since Last Submittal Through Refuel Outage 7 ML20216F1941998-04-0909 April 1998 Proposed Tech Specs License Condition 2.C(13) Re Partial Feedwater Heating & Final Feedwater Temp Reduction RBG-44355, Cycle 8 Startup Physics Test Summary1998-01-19019 January 1998 Cycle 8 Startup Physics Test Summary ML20202F0361997-11-26026 November 1997 Rev 0 to IST Plan for Pumps & Valves Second Ten-Yr Interval ML20216E4861997-09-0505 September 1997 Proposed Tech Specs Re APRM Setpoints,Reactivity Anomalies & RPS Instrumentation ML20210K2131997-08-15015 August 1997 Proposed Administrative Changes to TS 2.1.1.2 W/Note to Indicate Operating Cycle for Which SLMCPR Value Has Been Approved & TS 5.6.5 W/Note Providing Link to Specific GE Documents Used in Approving SLMCPR Changes for Given Cycle ML20217J0481997-08-0505 August 1997 Proposed Tech Specs 2.1.1.2, Reactor Core (Safety Limits), Increasing Two Recirculation Loop MCPR Limit to 1.13 & Single Recirculation Loop MCPR Limit to 1.14 ML20151L6041997-07-31031 July 1997 Proposed Tech Specs,Requesting Approval of Change to TS 3.6.1.8, Penetration Valve Leakage Control Sys, for Upcoming Outage ML20196J7741997-07-30030 July 1997 Proposed Tech Specs Clarifying Surveillance Requirements 3.6.4.2.1 & 3.6.4.2.2 to Match Corresponding Changes to NUREG-1434 ML20134A7021997-01-20020 January 1997 Proposed Tech Specs to License NPF-47,enhancing Operation of Plant to Allow Operation at 100% Power W/Lower Core Flows & Use of Flow Control Spectral Shift Strategies to Increase Cycle Energy ML20133M0451997-01-10010 January 1997 Proposed Tech Specs 3.4.11 Re RCS Pressure & Temp Limits ML20140F0151996-12-26026 December 1996 Rev 6 to RSP-0008, ODCM Procedure ML20134M2271996-11-15015 November 1996 Proposed Tech Specs,Changing TS SL 2.1.1.2, Reactor Core (Sl), Which Increases Two Recirculation Loop MCPR Limit from 1.07 to 1.10 & Single Recirculation Loop MCPR from 1.08 to 1.12 ML20134M0151996-11-15015 November 1996 Proposed Tech Specs 3.8.1 Re AC Sources Operating ML20134M2061996-11-0606 November 1996 Proposed Tech Specs,Permitting Increase in Allowable Leak Rate for MSIVs & Deleting Penetration Valve Leakage Control Sys & Ms Positive Leakage Control Sys Requirements ML20129J4231996-10-24024 October 1996 Proposed Tech Specs 3.8.1 Re A.C. Sources - Operating ML20117K1071996-08-29029 August 1996 Proposed Tech Specs Re Reactor Vessel Matl Surveillance Program Capsule Withdrawal Schedule ML20117G7401996-08-29029 August 1996 Proposed Tech Specs 3.1 Re Reactivity Control Systems ML20116P1341996-08-0808 August 1996 Technical Requirements Manual ML20116J3151996-08-0707 August 1996 Proposed Tech Specs,Submitting TS Bases Pages for Revs Performed Since 951001 Approval of TS Bases ML20116L6321996-08-0101 August 1996 Proposed Tech Specs Re Primary Containment/Drywell Hydrogen Mixing Sys & Drywell Isolation Valves ML20113F2271996-06-12012 June 1996 Rev 0 to Calculation PI-0103-00203.002-101, Ampacity Derating Evaluation ML20117L2581996-06-0404 June 1996 Proposed Tech Specs Re Replacement Page for Ltr RBG-42764, Proposed Tech Specs 3.9.1 Re Refueling Equipment Interlocks1996-05-31031 May 1996 Proposed Tech Specs 3.9.1 Re Refueling Equipment Interlocks ML20112E7831996-05-30030 May 1996 Proposed Tech Spec 3.8.3 Re Incorporation of 5-start Air Pressure Design Criterion for Div III DG ML20117H3271996-05-20020 May 1996 Proposed Tech Specs Re Change in Co Name from Gulf States Utils Co to Entergy Gulf States,Inc B130180, Surveillance Specimen Program Evaluation for River Bend Station1996-04-30030 April 1996 Surveillance Specimen Program Evaluation for River Bend Station ML20107E4681996-04-18018 April 1996 Proposed Tech Specs Re Fuel Loading W/Control Rods Withdrawn or Removed from Defueled Core Cells ML20094N7741995-11-22022 November 1995 Proposed Tech Specs,Clarifying Info Contained in License Amend Request (LAR) 95-21 ML20094M8001995-11-20020 November 1995 Proposed Tech Specs Re Drywell Leak Rate Testing Requirements ML20094N0091995-11-20020 November 1995 Proposed Tech Specs Eliminating Selected Response Time Testing Requirements ML20094B0001995-10-26026 October 1995 Proposed Tech Specs,Consisting of Change Request 95-10, Deleting TS 5.5.12, Biofouling Prevention & Detection, & Various Editorial Corrections ML20093L7361995-10-24024 October 1995 Proposed Tech Specs 3.6.1.1 Through 3.6.1.3 Re Containment Sys ML20108B5941995-10-0101 October 1995 Rev 5A to River Bend Station Offsite Dose Calculation Manual Procedure ML20087J5451995-08-17017 August 1995 Proposed Tech Specs Re Engineered Safety Sys Which Responds to Fuel Handling Accident Conditions ML20084L5001995-05-30030 May 1995 Proposed Tech Specs,Allowing TS 3/4.6.2.2, Drywell Bypass Leakage, Tests to Be Performed at Intervals as Long as Five Yrs Based on Demonstrated Performance of Drywell Structure ML20084L4541995-05-30030 May 1995 Proposed Tech Specs Re Request for Exemption from App J, Primary Reactor Containment Leakage Testing for Water- Cooled Power Reactors ML20078M1171995-02-0808 February 1995 Proposed Tech Specs Page Re Secondary Containment Automatic Isolation Dampers ML20077S4401995-01-18018 January 1995 Revised Pages of Proposed Tech Specs Re Conversion to TS Based on NUREG-1434, Improved TS Rev 0 ML20078H0881994-11-10010 November 1994 Proposed Tech Specs Reflecting Clarifications to LAR 91-11 1999-07-30
[Table view] Category:TEST REPORT
MONTHYEARRBG-44355, Cycle 8 Startup Physics Test Summary1998-01-19019 January 1998 Cycle 8 Startup Physics Test Summary ML20116M8051992-08-31031 August 1992 Reactor Containment Building Integrated Leak Rate Test for River Bend Station ML20043D4611990-05-30030 May 1990 Suppl 16 to Startup Test Rept, for Period Through 900530. W/900601 Ltr ML20042E9891990-04-27027 April 1990 Suppl 15 to Startup Test Rept. W/900430 Ltr ML20006C5581990-01-27027 January 1990 Unit 1 Startup Test Rept (Suppl 14). W/900131 Ltr ML19354D4471989-10-31031 October 1989 Startup Test Rept (Suppl 13), for Period Through 891027. W/891031 Ltr RBG-31323, Unit 1 Startup Test Rept (Suppl 12), Covering Period Through 8907271989-08-0404 August 1989 Unit 1 Startup Test Rept (Suppl 12), Covering Period Through 890727 ML20246M6951989-05-31031 May 1989 Reactor Containment Bldg Integrated Leakage Rate Test Types A,B & C Periodic Test RBG-30602, Unit 1 Startup Test Rept (Suppl 11)1989-04-27027 April 1989 Unit 1 Startup Test Rept (Suppl 11) RBG-29153, Suppl 9 to River Bend Station Unit 1 Startup Test Rept1988-10-13013 October 1988 Suppl 9 to River Bend Station Unit 1 Startup Test Rept RBG-28346, Startup Test Rept (Suppl 8) for Unit 11988-07-18018 July 1988 Startup Test Rept (Suppl 8) for Unit 1 ML20043A9081988-05-25025 May 1988 Determination of Fast Neutron Flux Density & Fluence:River Bend Station. RBG-27778, Suppl 7 to River Bend Station Unit 1 Startup Test Rept1988-04-15015 April 1988 Suppl 7 to River Bend Station Unit 1 Startup Test Rept RBG-27434, Suppl 6 to River Bend Station-Unit 1 Startup Test Rept1988-01-27027 January 1988 Suppl 6 to River Bend Station-Unit 1 Startup Test Rept RBG-26875, Gulf States Utils Co,River Bend Station-Unit 1 Startup Test Rept (Suppl 5)1987-10-27027 October 1987 Gulf States Utils Co,River Bend Station-Unit 1 Startup Test Rept (Suppl 5) RBG-26366, Suppl 4 to Gulf States Utils Co River Bend Station Unit 1 Startup Test Rept1987-07-28028 July 1987 Suppl 4 to Gulf States Utils Co River Bend Station Unit 1 Startup Test Rept ML20210B2831987-04-23023 April 1987 Suppl 3 to Startup Test Rept ML20212C8861987-01-30030 January 1987 Suppl 2 to Startup Test Rept ML20214P2001986-11-18018 November 1986 Suppl 1 to Startup Test Rept RBG-24132, Startup Test Rept,River Bend Unit 11986-07-31031 July 1986 Startup Test Rept,River Bend Unit 1 ML20132B2801985-08-31031 August 1985 Evaluation of CLASIX-3 Conservatisms & Quarter-Scale Tests ML20134H2151985-06-30030 June 1985 Ani/Maerp Std Method of Fire Tests of Cable & Pipe Penetration Fire Stops:Internal & External Seal of Aluminum Conduits,B&B/Promatec CTP-1092,A Issue & CTP-1093,A Issue, Final Rept ML20134G8601985-04-30030 April 1985 Reactor Containment Bldg Integrated Leakage Rate Test, Types A,B & C,Preoperational Test ML20094N7891984-01-13013 January 1984 GE Plant Piping Analysis Ii,Design Memo 150-96 ML19305E7131980-03-20020 March 1980 Rept of Potential Alkali Reactivity ASTM C227. ML19305E6841980-03-11011 March 1980 Rept on Potential Alkali Reactivity ASTM C227 & C-289. ML19322E9601980-02-20020 February 1980 Rept of Potential Alkali:Reactivity,Astm C227. ML19322E9631980-02-20020 February 1980 Rept of Potential Alkali:Reactivity,Astm C227. ML19322E9521980-02-12012 February 1980 Rept of Potential Alkali:Reactivity,Astm C227 & C289. ML19322E9531980-02-12012 February 1980 Rept of Potential Alkali:Reactivity,Astm C227 & C289. ML19322E9471980-01-23023 January 1980 Rept of Potential Alkali:Reactivity,Astm C227. ML19322E9461980-01-23023 January 1980 Rept of Potential Alkali:Reactivity,Astm C227. ML19322E9341980-01-15015 January 1980 Rept of Potential Alkali:Reactivity,Astm C227 & C-289. ML19322E9381980-01-15015 January 1980 Rept of Potential Alkai:Reactivity,Astm C227 & C-289. ML19294B2821979-12-20020 December 1979 Rept of Potential Alkali Reactivity ASTM C-227 & C-289 for Gulf States Utils Co - S&W Agent, for Fine Aggregate ML19294B2871979-12-20020 December 1979 Rept of Potential Alkali Reactivity ASTM C-227 & C-289 for Gulf States Utils Co - S&W,Agent for Number 57 Coarse Aggregate 1998-01-19
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GL/LF STATES . UTELITIES COMPANY n,e mau.w. .w n, . a e m m n i.msa a u, .ee,m ADIA(G51I>N OW WM 346 fWi1 January 31,1990 RBG-32234 File Nos. G9.5, G9.25.1.5 U. S. Nuclear Regulatory Commission Document Control Desk WLshington, D.C. 20555 Gentlemen:
River Bend Station - Unit 1 Docket No. 50-458 Enclosed is Supplement 14 to the.Startup Test Report for River Bend Station - Unit 1. This report covers the period through January 27, 1989. This information is provided pursuant to Technical Specifications 6.9.1.2 and 6.9.1.3 and Regulatory Guides 1.16 and 1.68. An additional report will follow within three months pursuant to Technical Specification 6.9.1.3.
Sincerely, J..F.Aix/p J E. Booker Manager-River Bend Oversight River Bend Nuclear Group JEB/ SF/ch ONL/p%
Enclosure
.cc: U. S. Nuclear Regulatory Commission Region IV 611 Ryan Plaza Drive, Suite 1000 Arlington, TX 76011 NRC Resident Inspector P.O. Box 1051 St. Francisv111e, LA 70775 Mr. Walt A. Paulson Project Manager, River Bend Station Document Control Desk Washington. 0.C. 20555 h 1 90020e0226 900127 #
- gDR ..ADOCK 05000458 PDC (l
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GULF STATES UTILITIES COMPANY i RIVER BEND STATION-UNIT 1 >
i STARTUPTESTREPORT(SUPPLEMENT 14) l t
t 27 JANUARY 1990 r
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STARTUP. TEST REPORT (SUPPLEMENT 14) i
- 1. The River Bend - Unit 1 Startup Test Program was concluded on June 16, 1986. This supplemental report provides the current status of open test exceptions from the October 27, 1989 supplement of the Gulf States Utilities Company, River Bend Station - Unit 1. Startup Test Report. Since the October 27, 1989 report, six test exceptions heve been closed and three open test exceptions remain.
- 2. All open test exceptions are categorized as affecting level 2 i criteria or lower. Any level I criteria failures referenced ;
in previous supplements were downgraded to level 2 criteria .
- as a result of appropriate engineering analysis and are ;
considered level 2 criteria in this report. This is j consistent with the treatment of all test criteria referenced d in the initial Startup Test Report. All open test exceptions were evaluated and approved by the on-site review committee for continued, safe, full power operation of River Bend Station - Unit 1.
- 3. Currently, the test exceptions are assigned to the individual system engineers to which the exceptions are most applicable.
It is believed that each engineer's knowledge of the system will aid in expediting the closure of the test exceptions.
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- ST-13 Process Computer r
TE-12: Status: Closed Temperature calibration problems were discovered as a result of balance of plant testing. These problems are still in the process of being corrected. This test exception involves balance of plant performance calculations and has no impact on any safety-related portion of the plant. Correction of the problem is still being pursued. However the calculations by the plant process computer are merely a convenience, not a necessity. At this time the calculations are being done en a personal _ computer with the data entered manually. This level 2 exception was evaluated as not impacting safe, full power operation. This test excoption has been reviewed by the Facility Review Committee (FRC) and recommended for closure.
ST-22 Pressure Regulator TE-22: Status: Open The main turbine pressure regulator failed the level 2 criteria for incremental regulation. Operation of the system through actual plant transients, including recirculation system flow control valve runbacks, single loop operation, power changes at various rates and numerous startups and shutdowns since initial criticality, has demonstrated that this system performs satisfactorily. Engineering is evaluating data collected during plant power maneuvers to evaluate the closure of this test exception. This exception has been determined not to impact safe, full power operation.
ST-23A Water Level Setpoint, Manual Feedwater Flow Changes TE-19: Status: Closed Based on the operating history of the feedwater system through normal operating transients, it has been determined that retesting is not necessary and that the feedwater level control system has been proven to be reliable and responsive. Although testing of individual valves was not possible, sufficient data exists to show that the system does respond in a linear fashion.
This exception dealt with system reliability and did not concern plant safety. This level 2 exception was evaluated as not impacting safe, full power ope' ration. The FRC has reviewed this test exception and recommended it for closure.
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ST-25C/D Main Steam Line riow Instroentation TE-3: Status: Open The elbow tap flow versus delta P curves are not within + 5% of the design curves. Elbow tap flow data were taken during power '
ascension following the first refueling outage. Engineering is evaluating field data to determine required main steam line flow instrumentation calibration changes. General Electric (GE) has evaluated this data and has agreed with GSU that this level 2 ;
test exception does not impact safe, full power operation. '
ST-30C Recirculation System Performance 1
TE-3: Status: Open The recirculation system flow control valve mismatch that existed was reduced from 14% to 7% and the core and drive flow shortfalls have been resolved. Evaluation is continuing to resolve the below design acceptance of the M ratio for the loop b problem.
Retest may be required to adequately disposition the M ratio problem due to the reduced flow control valve mismatch. A retest procedure has been drafted by on-site GE personnel. Evaluation of data obtained during plant power maneuvers continues. This .
level 2 test exception does not impact safe, full power operation.
ST-95 Emergency Response Infomation System TE-3: Status: Closed ,
Module S0-10 of the emergency response information system (ERIS) which performs scram timing, failed. This module addressed the set am time of only one rod. Work requests for correcting the problem were completed. However, this module failed again during retest. Plant maintenance and engineering personnel are ,
evaluating the cause of the second failure. This test exception is being closed because the rod's scram time is obtainable by attaching a strip-chart recorder to a permanent GE panel in the main control room. Scram times are then calculated manually.
The FRC has concurred with this evaluation. This level 2 exception does not impact safe, full power operation. .
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ST-100 Piping Vibration i
TE-16: Status: Closed Vibration data for MSS Points T42 and T220 was not available due
- to the failure of the ERIS data collection panel 113. Both of these points are located on non-safety related main steam piping. .
Data were obtained for one of these points during transients, I which were more severe than those called for in the test. The
, data were found acceptable. No data were available for the second point. However, the plant has experienced the most severe
- s. transient postulated for these pipes several times. A- detailed inspection of this piping and its associated supports during the last refueling outage revealed no abnormalities. Therefore, this piping is considered acceptable. This level 2 test exception does not impact safe, full power operation. This Test Exception has been evaluated by the FRC as accept-as-is based on a review of available data, operating history, and field inspection.
TE-20: Status: Closed ,
During generator load rejection (ST-27) points, MSS T-42Z, T235X, Y & Z, and FWS T-144X failed Level I criteria. MSS T-42X and FWS T-144& and Z failed level 2 criteria. No data was available for condensate test point T/S-525 since CNN-A0V 119 failed to open.
The data that exceeded the level 1 and 2 criteria were evaluated l prior to the closure of the start-up test program and determined to be acceptable. The remaining portion of the exception (T/S-525) involves only a portion of non-safety related condensate piping. This piping has been subjected to several load rejections during and since initial plant start-up. A detailed inspection of this piping and its associated supports '
during the last refueling outage revealed no abnormalities.
Therefore, this piping is considered acceptable. This Test Exception has been evaluated by the FRC as accept-as-is based on a review of available data, plant operating history and field inspection, i
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TE-21: Status: Closed Test points MSS- T-200, FWS T-39, SVV T-39 and T-85 were not operable during generator load rejection. Point MSS T-200 is on '
i nonsafety-related piping, points FWS T-39, SVV T-39 and SVV T-85 are on safety related piping. Point MSS T-200 is considered '
acceptable based on detailed field inspection of the piping and supports, and on comparison with other MSS points. Point FWS ,
T-39 is acceptable based on ASME XI Inservice Inspections of '
piping and supports..and on comparison with other FWS points.
Points SVV T-39 and SVV T-85 are acceptable based on ASME XI ISI ;
Inspections and on comparison with data. for these points' from ,
other transients. The only significant transient these points i experience is the lifting of a main steam safety relief valve ;
(the points are on an SRV tailpipe). Data for relief valve -l
. actuation were collected during other tests and were found to be satisfactory. This Test Exception has been evaluated by the FRC l as accept-as-is based on a review of available data, plant l
operating history, and field inspections. j i
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