ML20006A321

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Forwards TMI Resident Ofc Monthly Status Rept for 891128- 1218
ML20006A321
Person / Time
Site: Crane  Constellation icon.png
Issue date: 01/09/1990
From: Cowgill C
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To: Wenzinger E
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
References
NUDOCS 9001260121
Download: ML20006A321 (5)


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-Docket'Nos.'50-289' l

50-320 l

' MEMORANDUM FOR: Edward C. Wenzinger, Chief Projects Branch No'. 4 Division of Reactor Projects

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J FROM:

Curtis J. Cowgill, Chief Reactor Projects Section 4B 1

Division of Reactor Projects SUBJECf:

TMI' STATUS REPORT FOR THE-PERIOD NOVEMBER 28, -

DECEMBER 18, 1989 q

Enclosed is the last TMI Resident Office monthly status report, which covers both TMI-1 and TMI-2.

This report is to provide NRC management and the public twith highlights of significant events at TMI-1 and TMI-2 from an NRC regulatory

. perspective. The monthly status report for the' period May 16 - June 18, 1989 stated that the TMI status report would be discontinued when TMI-2 Defueling

_ as completed. With:the completion of bulk defueling-the defueling process is w

-essentially complete.' Based on this information the NRC sees no further value 4

.in' continuing these' reports.

Original Signed 4

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.beddNx Curtis J. Cowgill, Chief O Reactor Projects-Section 4B

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Division-of Reactor Projects-1

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Enclosure:

As Stated I

l OFFICIAL RECORD COPY TMI STATUS RPT 11/28-12/18/89 - 0001.0.0 01/08/90

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EdwardLC.'Wenzinger 2

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cc w/ enclosure:

- S. Varga, NRR J. Stolz, NRR-

.R. Hernan, NRR:

-M. Masnik,.NRR.

T. Martin, EDO-J. Partlow, NRR

,s J. Roe, NRR L. Whitney, NRR

'l T. Gerusky, BRP/ DER, Commonwealth of Pennsylvania Governor's Office of Policy, Commonwealth of Pennsylvania E

TMI Alert Susquehanna Valley Alliance Friends & Family of TMI l

D. Davenport L. Drey -

E.'Harzier t

A. Herman H.iHucker.

-J.:Johnsrud1

'P. Smith

-H.. Spinelli:

C. Wolfe Concerned Mothers and Women Public Document Room 2Loca11 Public Document Room

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K., Abraham,.RI.(2 copies)

M. Miller, RI.

W. Kane,!RI LW. Baunack, RI l

C. Cowgill, RI.

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J. Bell', NRR i

Region I Docket Room (w/ concurrences)

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D. Johnson

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'T.EMoslak L. Thonus R. Brady.

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0FFICIAL RECORD COPY TMI STATUS RPT 11/28-12/18/89 - 0002.0.0 01/08/90

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ENCLOSURE TMI-1 AND TMI-2 STATUS REPORT FOR THE PERIOD NOVEMBER 28 - DECEMBER 18, 1989 1.

TMI-I a.

Facility Operations Summary' During this reporting period, TMI-1 operated at full power until.

November 29, 1989. On _ that date, a reactor trip occurred as a result of an electrical problem experienced in the Turbine Electro Hydraulic Control System. This was the first automatic shutdown of the TMI-1 reactor in 13 months. Upon diagnosing the cause of the. reactor trip, the reactor was restarted achieving criticality at 3:00 am on December 1, 1989.

Following restart, the plant achieved full power and remained at 100% power until December 16, 1989. On December 16, 1989, a planned reduction to 95% power

- occurred as a result of normal fuel burn-up. An additional 5% reduction in power will occur every three or four days until it is operating at about 70% by January 5, 1990. At that time, the plant will be taken off line until March 4, 1989 to conduct refueling / maintenance activities.

2.

TMI-2 a,

Facility Activities Summary

.The licensee temporarily halted Defueling on November 28, 1989, after a

. worker received an unplanned exposure during the removal of a piece of equipment from-the Unit 2 reactor vessel.

The exposure occurred to the skin-on.the palm of-the workers hand and is estimated to be less than one rem. The regulatory limit for this type of exposure is 18.75. rem per j

calendar quarter.

l Radiological work practices were reviewed to preclude a reoccurrence, Following an investigation into the causes of the event and the implemen-tation of corrective actions, defueling was resumed on December 7, 1989.

On Saturday, December 16, 1989, the licensee completed bulk defueling of the TMI-2 reactor vessel. Approximately 300,000 lbs of core debris and intermixed materials were removed.

Several hundred pounds of finely divided fuel debris remain, principally as a dust layer on horizontal

surfaces, i

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E Defueling crews will remove this remaining fuel by vacuuming brushing and

. water flushing.

These activities should be completed by early January 1990.. After two weeks of video verification of defueling completion, the reactor vessel will be turned over to an international research group for reactor vessel lower head sampling. The one month long research effort will obtain metallurgical samples from instrument penetrations and the reactor-vessel lower head.

3.

NRC Staff Activities i

The NRC staff assigned on site during this period consisted of a senior resident-inspector, three resident-inspectors and a project manager for j

TMI-2.

4 a.

Enforcement Conference j

i I

On November 22, 1989, an Enforcement Conference was held between NRC and GPU Nuclear Management at the NRC Region I offices in King of Prussia, PA.

The purpose-of the conference was to discuss the nature of the events that resulted in the overexposure of two workers on September 25, 1989 and licensee's actions taken to preclude a reoccurrence.

l On Monday, December 4, 1989, the enforcement conference was reconvened in l

t'he NRC Region I office with the licensee. The purpose of the enforcement conference.was to review the potential for commonalities between the l

September 25 extremity overexposure and the event which occurred cn i

November 28, 1989. The' November 28 event did not result in an over-

' i exposure, but the high dose rates involved (greater than 300 Rad /hr beta) b

. created a hazard.

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L The licensee informed the NRC of their analysis of the principal causes, i

contributing factors, and planned corrective actions. Although some.

contributing factors were common, the events were largely separate and distinct. The licensee's corrective actions included upgraded training, procedure review and upgrade, personnel skills and qualification review,

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and positive communication methods.

b.

Regional Management Site Visit On November 30, 1989, NRC Region I management visited the site to evaluate l

the causes and plant conditions that resulted in a worker receiving an unanticipated exposure while removing a piece of equipment from the reactor vessel.

The results of this evaluation will be documented in

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report no.-50-320/89-13.

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3 c.

Inspection Reports.

During this period, Region I issued the-following inspection reports.

--TMI-1 Inspection Report 50-289/89-81 addressing routine safety inspection activities for the emergency preparedness exercise.

--TMI-1 and TMI-2 Inspection Reports 50_-289/89-22 and 50-320/89-10 addressing routine safeguards inspection. One violation was issued concerning security personnel qualifications.

---TMI-2 Inspection Report 50-320/89-08 addressing a routine safety inspection.

l

d. NRR Licensing Actions On November 27, 1989, the NRC office of Nuclear Reactor Regulation (NRR) issued a safety evaluation (SE) and approval letter for GPUN tc use the polar crane auxiliary hook over the seal table. This allows the licensee to use the crane to partially withdraw incore instrument strings from the-reactor vessel. Withdrawal of the instrument strings is a preliminary u

activity in the reactor vessel lower head sampling program.

On November 28, 1989, the:NRR staff issued a SE and approval letter for the reactor vessel lower head sampling program.

This program is part of B-an international researc:1 effort in core melt-reactor vessel interactions.

Samples from the reactor vessel lower head, including instrument penetrations will be cut out using a metal disintegration machine.

This

-activity will take place after the completion of defueling the TMI-2 reactor vessel, p.

Organization plan change Number 21 was issued on November 8, 1989. This change approves a corporate level realignment of GPU Nuclear.

4.

Public-Meeting The next meeting of the Advisory Panel for the Oecontamination of TMI-2' has been postponed until spring of 1990.

The meeting will be scheduled after the panel members and NRC staff receive the final Defueling Completion Report from GPU Nuclear. The time, date and location will be announced via press releases.

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