LER-1981-020, /03L-0:on 810506,during Diesel Generator Redundant Start Test (EMI-3),D Engine Left Bank Air Start Motors Would Not Develop Min Rotational Speed.Caused by Broken Vane.Air Starting Motors Replaced |
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| 2591981020R03 - NRC Website |
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O rennewe Valley Authority Form IlF-17 Mrowns Ferry Nuclear Plant BF 15.2 3/24/M1 LER SUPPLEMENTAL INFORMATION BFRO 259 / 81020 Technical Specification involved
- 3. 9. B. 2 -
Reported Under Technical Specification _
6.7.2.b(2)
Date of Occurrenc 5/6/81 Time of Occurrence 0115 Unit l' & 2 D/G I41entification and Description of.Occurrencc:
"C" diesel generator air start motors would not develop minimum rpm te p.iss test criteria.
Cono2 ion. Prior to occurrence:
1: nit i refueling outage.
L' nit 2 at 98.2%.
Unit 3 at 99%.
Action specified in the Technical Specification Surveillance Requircaents met due to inoperable equipment. Describe.
Nt requirements of T.S. 3.9.B.2.
tg.arent Cause of Occurrence:
\\
necken vane due to normal wear.
Analvg of Cccurrence:
There was no danger to the health or safety of the public, no release of activity, no damage to the plant or equipment, and no resulting significant chain of events.
f gugect ve Action:
Feplaced air start motors.
Recurrence control: Program to monitor performance of motors and evaluate present preventive maintenance will be established.
Fadure Data-BIP5 50-259/74004, 74013W, 74021W, and 75008W.
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" Retention : Period Lifetime; Responsibility - Document Control Supervisor
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| 05000260/LER-1981-001, Forwards LER 81-001/01T-0 | Forwards LER 81-001/01T-0 | | | 05000260/LER-1981-001-01, /01T-0:on 810102,scram Discharge Vol Level Switch 2-LS-85-45A Found Inoperable & -C & -D Found Offscale.Caused by One Robert Shaw Switch Model SL-305-EI-X Sticking & Setpoint Drift.Stuck Switches Float Chamber Back Flushed | /01T-0:on 810102,scram Discharge Vol Level Switch 2-LS-85-45A Found Inoperable & -C & -D Found Offscale.Caused by One Robert Shaw Switch Model SL-305-EI-X Sticking & Setpoint Drift.Stuck Switches Float Chamber Back Flushed | | | 05000259/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000296/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000296/LER-1981-001-03, /03L-0:on 810106,both Smoke Detectors in Reactor Bldg Fixed Spray Zone Were Inoperable.Caused by Loose Screw in Terminal Block.Screw Replaced | /03L-0:on 810106,both Smoke Detectors in Reactor Bldg Fixed Spray Zone Were Inoperable.Caused by Loose Screw in Terminal Block.Screw Replaced | | | 05000259/LER-1981-001-03, /03L-0:on 810105,core Spray Sparger to Reactor Pressure Vessel D/P Switch 1-PDIS-75-28 Found Set Above Tech Spec Limit.Caused by Barton Model 288 Setpoint Drift.Switch Replaced W/New Switch on 810115 | /03L-0:on 810105,core Spray Sparger to Reactor Pressure Vessel D/P Switch 1-PDIS-75-28 Found Set Above Tech Spec Limit.Caused by Barton Model 288 Setpoint Drift.Switch Replaced W/New Switch on 810115 | | | 05000260/LER-1981-002-03, /03L-0:on 810102,scram Discharge Instrument Vol Rod Block Level Switch 2-LS-85-45E Found Set at 27 Gallons. 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