ML20003D629

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Replacement Page for 800428 Rept,Consisting of Ltr Forwarding fifty-seventh Quarterly Rept for Jan-Mar 1980. Rept for Jul-Sept 1980 Encl
ML20003D629
Person / Time
Site: West Valley Demonstration Project
Issue date: 10/29/1980
From: Duckworth J
NUCLEAR FUEL SERVICES, INC.
To:
NRC OFFICE OF NUCLEAR MATERIAL SAFETY & SAFEGUARDS (NMSS)
Shared Package
ML20003D627 List:
References
17773, 800428-01, 800428-1, 9-80-20, NUDOCS 8103270853
Download: ML20003D629 (12)


Text

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/T Nuclear Fuel Services, Inc. P.O. Box 124

  • West Valley, New York 14171 A Subsidiary of Getty Oil Company (716) 942-3235 April 28,1980 9-80-20 (ReplacementPage October 29,1980)

Director Office of Nuclear Material Safety and Safeguards U. S. Nuclear Regulatory Comission Washington, D.C. 20555

Dear Sir:

Enclosed is the fifty-sixth quarterly report for the period January 1, 1980 to March 31, 1980 as required by Paragraph SC(4) of Provisional License CSF-1.

If you have any questions or comments, please contact us.

Very truly yours, NUCLEAR FU L SER/ CES, INC.

J. . Duckworth General Manager CWA /SRG/aa Attachment cc: NYSERDA Chairman 8108270 )

TABLE OF CONTEilTS .

ENVIRONMEllTAL MONITORING LOW LEVEL LIQUID EFFLUENTS ,

GASEOUS EFFLUEllTS SURVEILLAtlCE TESTS LOW LEVEL LIQUID WASTE TREATMENT PLANT PERFORMANCE TABLE 1 LIQUID EFFLUEllTS - 1980 TABLE 2 GASEOUS EFFLUENTS - 1980 TABLE 3 SURVEILLANCE TESTS TABLE 4 FILTER REPLACEMENT' PROCESSING SUfHARY NUCLEAR FUEL SUPP.ARY .

TABLE 5 NUCLEAR PJEL STATUS - SEPTEMBER 30, 1980 RADI0 ACTIVE WASTE -

FACILITY PERFORMANCE AND MODIFICATIONS e

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ENVIRONMENTAL MONITORING 131I was dis-As a result of changes in Technical Specifications, sampling milk for continued on September 21, 1973.

Thirty-nine (39) samples were obtained during the second quarter from the perimeterThe aloh monitoring stations and were analyzed for alpha and beta activity.3.24 (10 15) pCi/ml.

ranged from 1.38 (10-16) to 1.47 (10 15) uCi/ml for an average of The beta activity ranged from 5.33 (10 15) to 6.99 (10 l'+) pCi/mi with an average of 2.10 (10 14) pCi/ml .

' LOW LEVEL LIOUID EFFLUENTS The amounts of radioactivity in liquid discharged from the plant during this period and their relationship to the maximum permissible concentration (MPC) in the Cattaraugus Creek are shown in Table 1.

GASEOUS EFFLUENTS The amount of particulate radioactivity discharged via the plant stack and the relationship to the release limit in the Technical Specifications is shown in Table

2. Change 20 to the Technical Specifications discontinued the recuirements of Krypton-85 and Iodine-131 monitoring while plant operations are suspended.

SURVEILLANCE TESTS During this period, tests were performed in accordance with Section 6 of the Technical Specifications. The completion dates are shown in Tables 3 and 4.

LOW LEVEL LIQUID WASTE TREATMENT PLANT PERFORMANCE 1,097,000 During this period, the LLWT was in operation a total af 10 days and treated Fourty-eight (48) drums of concentrated sludge were removed, each gallons of water.

naving a radiation luel of <10 mr/hr. Decontamination of waste water continues to be good. All water discharged has been below 2.0 x 10 5 pCi Csl37/ml. Average removal factors for this period are shown below.

AVERAGE REMOVAL FACTOR Previous Quarter This'Ouarter Isotope 76.1 80.0 Cs-137 Not Yet Available f Sr-90 99.7 l

Below Detection Limits Below Detection Limits l Ru-Rh-106 -

97.7 Gross Beta 95.3 No significant developments or modifications to the facility have occurred during the past quarter and operation has been routine.

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Table 1

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LIOUID EFFLUENTS--1980 (Curies) 8

% MPC Measured Gro3s s Tritium Sr 90 I 129 In Cattaraucus Creek Month Gross a C 0.33 0.0010 0.00001 NR Jan 0.000001 0.00002 C 0.55 0.0007 0.00001 NR Feb 0.000001 0.00002 C 0.39 0.0006 0.00001 NR Mar 0.000001 0.00002 0.0025 0.00006 0.29 0.00013 0.019 1.37 Apr C 0.49 0.0008 0.00001 NR May 0.000001 0.00003 C 0.88 0.0009 0.00001 NR Jun 0.000001 0.00003 c 0.33 0.0008 0.00001 NR Jul 0.000001 0.00004 b b NA NA 0.018 4.87 NA Aug 0.000007 ,

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' NA NR NA 0.000001 0.00004 0.0005 Sep d

0.0026 - 0.00006 0.46' 0.00021 0.037 6.25 1980 4

. a MPC (s) = 3.0 (10~7) pCi/ml when SrSO analyses are not availableSO ana MPC (s) .= 1.0 (10 s) pCi/ml when Sr - ,

MPC (a) = 5.0 (10~6) uCi/ml .

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b Not yet available cNot required; there were no lagoon 3 effluent releases for the month dRelease through July 1980

'MPC through July 1980 ,

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9 Table 2 PARTICULATE GASEOUS EFFLUENTS - 1980 Month Curies  % Monthly Limit

. -- .- January .00012 0.04

- February .00010 0.04 March ~~~~ ~ ~ .00008 0.03 April- .00010 0.0?

May .00005 0.02 June .00004 0.02 July .00005 0.02 August .00004 0.01 September .00005 0.02 1980 .00063 0.027 l .

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. Table 3 SURVEILLANCE TESTS 1 Soec. # Dibfect Comoleted This Quarter Comments 6.1 Raschig Ring Tanks Tanks are to be

. scheduled prior to next processing use 6.2 Sump Alarms and Eductors XC-2 7-7, 7-29, 8-19, 9-9, 9-30 Satisfactory XC-3 -

7-8, 7-29, 8-19, 9-9, 9-30 Satisfactory PPC 7-9, 7-29, 8-19, 9-9, 9-30 Satisfactory

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~ 6.3 Waste Storage Tank Pan Instrumentation 80-1, 8D-2 7-8, 7-30, 8-20, 9-8 Satisfactory 80-3, 8D-4 7-8, 7-30, 8-20, 9-8 Satisfactory 6.4 Emergency Utility Equipment 30T-1 7-1 Satisfactory 31K-1 7-1 Satisfactory 32G-4B 7-1 Satisfactory 31G-2, 2A 8-12 Satisfactory 31K-2, 2A- 8-12 Satisfactory 32G-2A, 28 8-12 Satisfactory Diesel Fuel 7-7, 7-14, 7-21, 7-28, 8-4, 8-11, 8-25, 9-1, 9-8, 9-15, 9-22, 9-29 Satisfactory Propane Fuel 7-8, 7-14, 7-21, 7-28, 8-4, 8-11, 8-18, 8-25, 9-2, 9-8,

.9-22, 9-29 Satisfactory 15K-10A 7-1 Satisfactory 15F-21 7-1 Satisfactory 6.5 Filters -

7-10, 7-17, 7-25, 7-29, 8-8,

. 8-15, 8-22, 8-?.7, 9-5, 9-11, 9-17, 9-25 . Satisfactory 6.6. Dilution Air Not required t_his period 6.7 Boric Acid .'NotLrequired this period 6.8 Locking Out -

Not required this period 6.9 Water Activity A1, arms 9-30 Satisfactory 6.10 Poisoned Dissolver Baskets Not required this period 6.11 Solvent Analysis Not required this period

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Table 4 FILTER REPLACEMEtiT The Waste Tank Farm filter 871A was changed on 8-31-80.

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PROCESSING SUFFARY During this period there was no orocessing of fuel.

The periodic pumpdown of Waste Tank 80-1 condensate continued until July 14,1980 with an additional 56,456 gallons being treated and sent to Lagoon 1. The total volume of condensate which was treated and sent to Lagoon 1 during the pumpout amounted to 78,795 galloris.

An additional 40,950 gallons of the 80-1 condensate were transferred directly to Waste Tank 80-2.

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l NUCLEAR FUEL

SUMMARY

The following .information is based upon nucleue material accountability records and indicates the disposition of nuclear material in fuel at the reprocessing plant.

A. INVENTORY .

The total on-site inventory on September 30, 1980 was 166,759 kilograms of uranium and 1,037,634 grams of plutonium. An inventory description by source and material type is presented in Table 5.

B. RECEIPTS AND SHIPMENTS During the quarter, there were no shipments or receipts of spent fuel assemblies at the West Valley site.

C. MEASURED WASTE AND ADJUSTMENTS There was no loss of uranium or plutonium during the reporting period as measured waste.

No adjustments for uranium and plutonium to NFS Lot 27A were

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l D. . LOSS ON DECAY l

l During the period 3/31/80 - 9/30/80 there was a reduction of l

- 1, ,7 grams of plutonium in stored fuel due to the radioactive decay

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'. . l Table 5 NUCLEAR FUEL STATUS AS OF SEPTEMBER 30, 1980 Kilograms -

Grams

. Total U- U-235 U-233 Total Pu

- I. INVENTORY *

(7/1/80) -

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3,271 8.01 -- 306 NFS _

20,429 144.03 0.30 116,887 Dresden-1 46,156 722.48 -- 285,787 RG&E ...

11,130 238.68 -- 64,118 Consumers. -

43,017 462.61 -- 338,394 WEPC0 Jersey Central 42,756 463.42 -- 234,335 TOTAL 166,759 2,039.23 0.30 1,039,827 II. RECEIPTS (7/1/80-9/30/80) No receipts during this period. -

III. REMOVALS (7/1/80-9/30/80) '

A. Measured Waste 0

Lot 27A 0 0 0 B'. Adjustments ~

0 0 0 0 .

Lot 27A 0 0 0 1,887 C. Loss on Decay 0 0 0 1,887 TOTAL 1V. INVENTORY (9/30/80)

NFS 3,271 / 8.01 -- 306 20,429 144.03 0.30 116,658 Oresden-1 285,272 RG&E 46,156 722.48 --

11,130 238.68 -- 64,039 Consumers 43,017 462.61 -- 337,652 WEPCO 234,013 Jersey Central -

42,756 463.42 --

166,759 2,039.23 0.30 1,037,940 TOTAL ,

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RADI0 ACTIVE WASTE ,

A. Solid Waste The radioactive plant waste buried during this quarter consisted of 1488.79 cu. ft. containing 161.176 curies. .This material was

. buried in the NRC-licensed burial area.

B. High Level Licuid Waste ,

As of September 30, 1980, the high level storage tank 80-2 contained 571,100 gallons of neutralized waste. with an actidty of 4,296 uCi Cs-137/ml and 65 pCi Cs-134/ml.

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, -l s FACILITY PERFORMANCE AND MODIFICATIONS This section describes:

1.0 Major modifications that were either initiated or completed at

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the processing plant during the recorting period.

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~ N device to detect small leaks by collecting and sampling water vapor condensate emanating from the waste tank 80-2 vault

  • vent was designed and fabricated, then installed on 9/19/80.

2.0 A description of malfunctions of any equipment listed in Acpendices 5.2, 9.51, 9.53 and 9.56 of the Fina! Safety Analysis Report which are important to safety. .

2.1 At approximately 4:00 A.M. on Sunday, September 14, 1980,

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lightning struck the power supp1f for the lake pumps,

! putting them out of service. ' Repairs were effected on Monday, September 15, and the unit again became operable.

2.2 The motor on the Con-Ed scrubber pump 8G-3 burned out. The

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unit was replaced and put back into service.

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17773

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