ML20003B600

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Forwards IE Bulletin 81-01, Surveillance of Mechanical Snubbers. No Written Response Required
ML20003B600
Person / Time
Site: Atlantic Nuclear Power Plant PSEG icon.png
Issue date: 01/27/1981
From: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To: Collier A
OFFSHORE POWER SYSTEMS (SUBS. OF WESTINGHOUSE ELECTRI
References
NUDOCS 8102120554
Download: ML20003B600 (1)


Text

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UNITED STATES NUCLEAR REGULATORY COMMISSION o

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101 MARIETTA ST., N.W., SUITE 3100 o

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ATLANTA, GEORGIA 30303 JAN 2 7 1981 m

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A. R. Collier, President

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P. O. Box 8000 Jacksonville, FL 32211 ru Gentlemen:

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The enclosed IE Bulletin No. 81-01 is forwarded to you for information. No written response is required. If you desire additional information regarding this matter, please contact this office.

Sincerely, 1

James P. O'Reill l

Director i

Enclosures:

1.

IE Bulletin No. 81-01 2.

List of Recently Issued IE Bulletins 4

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810212055'l g

SSINS No.:

6820 Accession No..

8005050075 IEB 81-01 UNITED STATES NUCLEAR REGULATORY COMMISSION OFFICE OF INSPECTION AND ENFORCEMENT WASHINGTON, D.C.

20555 January 27, 1981 IE Bulletin No. 81-01:

SURVEILLANCE OF MECHANICAL SNUBBERS Description of Circumstances:

Several instancer of failures of mechanical snubbers supplied by International Nuclear Safeguards Corporation (INC) have been identified that indicate possible deficiencies in these snubbers.

A summary of the failures that have occurred is provided below:

1.

On August 9, 1974, the Tennessee Valley Authority submitted event report BFAO-50-260/741W identifying 11 of 14 INC Model MSVA-1A snubbers that were found inoperable on Browns Ferry Nuclear Power Station Unit 2 and subsequently identified 5 of 14 inoperable units on Browns Ferry Nuclear Power Station Unit No 3.

All of these units were found to be frozen, and the cause was attributed to a failure to lubricate the parts during assembly.

The failed snubbers were replaced with new units produced by the same manufacturer.

2.

On April 12, 1976, the St. Lucie Plant Unit 1 facility of Florida Power and Light Corporation submitted event report No. 50-335-76-9 wherein five INC Model MSVA-1 snubbers were identified as inoperable because they were found to be frozen. The failures were caused by oxidation on the internals and by improper assembly. All INC mechanical snubbers were replaced with units produced by another manufacturer.

l 3.

On April 8, 1977, Iowa Electric Light and Power Company submitted event report No. 77-23 for the Duane Arnold Energy Center facility that identi-l fied 13 INC Model IMSVA-1 Type AS snubbers to be frozen; the cause of failure was attributed to large amounts of interior oxidation. The units l

were replaced with those produced by another manufacturer.

l 4.

On December 5,1979, personnel from the Nuclear Regulatory Commission visited Department of Energy (DOE) facilities at Richland, Washington, to obtain information on DOE experience with INC snubbers at the Fast Flux Test Facility (FFTF).

The DOE-owned FFTF was equipped with more than I

bbers) supplied by INC.

In 1978, mechanical snubbers by removing them t 43, or about 5% of those examined, DUPLICATE DOCUbuNT d to only normal construction Entire doctunent previously entered into system under:

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