ML20002E419

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IE Insp Rept 50-155/78-01 on 780116-20.Noncompliance Noted: Alarm Settings on Radwaste Monitors for 17 Releases Made During 1977 Exceeded Required Level for Radioactive Discharge
ML20002E419
Person / Time
Site: Big Rock Point File:Consumers Energy icon.png
Issue date: 02/15/1978
From: Fisher W, Schumacher M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20002E418 List:
References
50-155-78-01, 50-155-78-1, NUDOCS 8101270923
Download: ML20002E419 (6)


See also: IR 05000155/1978001

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U.S. NUCLEAR REGULATORY COMMISSION

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OFFICE OF INSPECTION AND ENFORCEMENT

REGION III

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Report No. 50-155/78-01

Docket No. 50-155

License No. DPR-6

Licensee: Consumers Power Company

212 West Michigan Avenue

Jackson, MI 49201

Facility name: Big Rock Point Nuclear Plant

Inspection at: Big Rock. Point Site, Charlevoix, MI

Inspection conducted: Janua ry 16-20, 1978

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Inspector:

M. C. S humacher

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Approved by:

W. L. Fisher, Chief

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Fuel Facility Projects and

Radiation Support Section

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Inspection Summary

Inspection on January 16-20, 1978 (Report No. 50-155/78-01)

Areas Inspected: Routine, unannounced inspection of radioactive waste

systems, includingt effluent rr. eases; records and reports of effluents;

effluent. control instrumentation; procedures for controlling releases;

containment air-cleaning systems; reactor coolant water quality; solid

radioactive waste; and review of licensee event reports. The inspection

involved 50 inspector-hours onsite by one NRC inspector.

Results: No items of noncompliance were identified in 5 of the 8

areas inspected. One item of noncompliance was identified in each of

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the areas of liquid effluent releases, solid radioactive waste, and

effluent control instrumentation.

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DETAILS

1.

Persons Contacted

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  • C. J. Hartman Plant Superintendent
  • C.

E. Axtell, Health Physicist

  • T. !!. Brun, Chemical and Radiation Protection Supervisor
  • D. DeMoor, Technical Engineer
  • G. Gilbody, QA Engineer

The inspector also talked with other licensee employees, includ-

ing operators and health physics and instrument control technicians.

  • denotes those present at exit inte rview.

2.

General

This inspection, which began at 8:00 a.m. on January 16, 1978,

was conducted to examine licensee activities with regard to

radioactive waste management. The plant was in cold shutdown

for repair work on control rod drives. An initial tour was

made of selected areas of the plant, including access control,

radwaste, various process monitor locations, and the control

room. A more extensive tour of the plant was made later in the

insnect ion.

Radiological conditions within the plant appeared

sc'.isfactory; good 1>usekeeping was evident. A small office near

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access control has seen given over to health physics use.

Licensee employees indicated that it is also used for the one-oe

onerespiratortrainingformey}ygiveninaccesscontrolasnot '

during a previous inspection.--

No items of noncompliance were observed.

3.

Licensee Action on Previous Inspection Findings

(Closed) Exit Interview Commitment (155/77-09):

review and

revise air sampling analysis procedures as necessary. Appropriate

changes to Procedure RP-29, " Radiological Surveys," were made by

the licensee.

4.

Airborne Effluents

Plant records of airborne release samples for 1977 were examined.

These data are used by the licensee's corporate office staff to

1/ RlII Inspection Rpt No. 50-155/77-09.

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generate, by computer, the data presented in the semiannual

effluent report. No significant inconsistencies were noted

between the two data sets. -Noble gas releases are based on

daily samples of off-gas.

Isotopic characteristics are

specified based on weekly spectral analysis of an off-gas

sample. Release rates measures during 1977 were relatively

stable in the range of 400 to 1100 microcuries per second,

less than one percent of the technical specification limits.

Iodine and particulate releases are determined from continu-

ously collected particulate and charcoal filters that are

changed and analyzed weekly. Technetium-99m (half-life

approximately six hours), reported previously only in January

1976, became the dominant particulate released, beginning in

April 1977. Licensee representatives were unable to explain

this matter but agreed to look into it.

All iodine and particu-

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late releases during the period were less than one percent of

the technical specification limits.

No items of noncompliance were identified.

5.

Liquid Effluents

The records of 37 liquid waste batches released during 1977

were reviewed.

In accordance with Licensir.g Procedure RCP-7,

" Analysis of Liquid Radwaste Batch," each batch was sampled,

ccunted for gross alpha and beta activity, and analyzed to

determine isotopic composition. The permissibic release rate,

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a function of the batch isotopic characteristics, is calculated

for the available dilution flow. All releases made in 1977

appeared to meet technical specification requirements with

regard to release concentrations.

During releases, the radwaste monitor is set to alarm at a

count rate that corresponds to a concentration of IE-5

microcuries per milliliter, p'.us background. This setting

is derived using the monitor calibration curve, the expected

dilution flow, and the authorized discharge flov.

T.t assumes

an applicable MPC 'value of IE-6 microcuries per milliliter,

which is further augmented by the factor 10 to allow for

monitor vagaries. This practice appears to be contrary to

Technical Spec 1fication 6.4.1.d, which requires that the

monitor alarm be set to detect 10 CFR 20, Appendix B Table 2,

Column 2 levels. The licensee's set points have averaged

about a factor of three higher than those corresponding to

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the 30 CFR 20 limits determined from the licensee's isotopic

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analyses. The maximum variation ha's been about a factor of

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10.

It was also noted that during the last quarter of 1977

the monitor background increased by a factor of about five

to greater tha;. iC? 000 counts per minute. The need for improved

monitor decontamination was discussed at the exit interview.

6.

Solid Radioactive Waste

The records of 14 solid waste shipments made during 1977 were

reviewed. Twelve shipments of greater than Type A quantities

of dewatered spent resins were made during the period Iby 24-

June 121, 1977. In atparent noncompliance with 10 CFR 71.3,

the shipments were made in packages unapprosed as required

by 10 CFR 71.12.

Before this inspection, tie licensee deter-

mined that the packages were not approved.

Following this

determination, arriangements were made with the consignee and

package owner (Nuclear Engineering Company, Morehead, Kentucky)

to provide an approved Type B Cask for such shipments until

approvals for the formerly used packages are obtained.

Accordingly, the licensee had on hand copies of the licenses

and reference documents for NUS Cask Model SN-1 (Certificate

Number 6771). The inspector pointed out the 10 CFR 71.12

notification requirement before first use of this cask. The

corrective action taken by the licensee in this matter appears

to be satisfactory.

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7.

Records and Reports of Effluents

The licensee's semiannual report for the period January to

June 1977 was reviewed for internal consistency. No problems

were identified. Licensee effluent records examined at the

plant were satisfactory.

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8.

Effluent Control Instrumentation

Process monitor calibration records for 1977 were reviewed.

The records indicated noncompliance with the calibration

check requirements of Technical Specification 6.4.3.d when

the monthly check of the radwaste. monitor was missed during

1977. The missed surveillance was an isolated occurrence; the

licensce's surveillance procedures appear adequate to prevent

recurrence.

9.

Reactor Coolant Water Quality

Records of daily radioactivity measurements in reactor coolant

water during 1977 were reviewed.

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No items of noncompliance were identified.

10. - Procedures

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Thefollowingradwasteprocedures,adgydoramendedsincethe

radwaste inspection of December 1976,- were revie.wed.

RCP2, " Analysis of Of fgas," Revision 2. December 1,1977:

No problems were identified.

RCP5, " Changing Stack Gas Sampling Filters," Revision 3,

November 15, 1977: The possible effects of leaking

valves on the sampling system integrity test in this

procedure was discussed; the absence of a valve line-up

checklist in the procedure was noted. Licensee employees

indicated the procedure would be reviewed.

RCP6, " Analysis of Stack Gas Filters, " Revision 5,

December 2, 1977: No problems were identified.

RCP7, Analysis of Liquid Radioactive Batch, " Revision 2,

December 2, 1977: No problems were identified.

CIP3, " Operation of the TASC-2 Radioisotope Analyzer,"

Revision 1 December 9, 1977: No p.oblems were identified.

The inspector also reviewed the following procedures

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related to radiation protection.

RP4, " Radiation Protection Procedures for Radiation

Workers," Revision 2, September 26, 1977: No problems

were identified.

RP10 "Use of High Radiation Area Worksheet," Revision 1,

October 31, 1977: No problems were identified.

RP29, " Radiological Surveys," Revision 3. August 12,

1977, Revision 4, November 7, 1977, Revision 5, November 29,

1977: This procedure was cha

duringapreviousinspection.ggedtoaddressproblemsnoted

No problems were identified

in this review.

RIP 10. " Sphere and Turbine Room, Calibration of Continuous

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Air Monitors (CAMS)," Revision 1, December 11, 1977: The

inspector noted the absence of the requirement for running

a plateau on the Geiger Mueller detector.

It was also noted

that the method of setting the monitor alarm was dependent

upon an unvarying detector counting efficiency. Alternate

2/ RIII InFpection Rpt No. 50-155/76-22.

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3/ RIII Inspection Rpt No. 50-155/77-09.

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schemes for determining alarm set points were discussed

with licensee representatives, who indicated the proce-

dure would be reviewed.

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RIP 11, " Calibration of Continuous Air Monitor-Sphere

Exhaust CAM," Revision 0. December 8, 1977: The

inspector noted that there was no requirement to run a

plataeu for the Geiger Mueller detector.

An arithmetic error was noted in the particulate channel

calibration in Section 6.5.

11.

Review of Licensee Event Report

The licensee's corrective actions on the following licensee

event reports were reviewed.

155/77-25

Water and clean up resin drain to floor of

clean up denineralizer room, September 24,

1977.

155/77-44

Plant heating boiler contaminated by reactor

closed cooling water, October 31, 1977.

No items of noncompliance were identified in this review.

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12.

Containment Air Cleaning Sys'. ens

The offgas is treated for removal of particulates by passing

through a high ef ficiency (HEPA) filter near the base of the

stack. Other air exhausted through the stack is unfiltered.

The filter is changed at refueling outages.

i.o provisien was

made for introducing a test aerosol for in-place efficiency

testing.

13.

Exit Interview

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The inspection results were discussed with Mr. liartman and

others of the station staff at the c' lose of the inspection.

The inspector st,

ed that corrective actions regarding the

missed radwaste c.

' tor calibration check and unepproved

solid radwaste pat ages appeared adequate.

The need for lower radwaste monitor background was discussed.

The licensee stated that steps would be taken to inprove

monitor background.

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