05000313/LER-1981-006-03, /03L-0:on 810408,emergency Feedwater Feed Valve CV-2670 to Steam Generator a Control Power Fuse Blew on Valve Actuator.Caused by Fuse Opening on Transient Current. Fuse Replaced W/Slower Acting Fuse

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/03L-0:on 810408,emergency Feedwater Feed Valve CV-2670 to Steam Generator a Control Power Fuse Blew on Valve Actuator.Caused by Fuse Opening on Transient Current. Fuse Replaced W/Slower Acting Fuse
ML19347F088
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 05/05/1981
From: Shively C
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19347F087 List:
References
LER-81-006-03L, LER-81-6-3L, NUDOCS 8105150234
Download: ML19347F088 (1)


LER-1981-006, /03L-0:on 810408,emergency Feedwater Feed Valve CV-2670 to Steam Generator a Control Power Fuse Blew on Valve Actuator.Caused by Fuse Opening on Transient Current. Fuse Replaced W/Slower Acting Fuse
Event date:
Report date:
3131981006R03 - NRC Website

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