ML19345G085

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RO 77-03:on 770815,secondary Containment (Refueling Bldg) Automatic Isolation Feature Monthly Test Not Performed as Scheduled.Caused by Administrative Error in Interpretation of Tech Specs.Plant Procedures to Be Revised
ML19345G085
Person / Time
Site: Humboldt Bay
Issue date: 09/08/1977
From: Redeker S
PACIFIC GAS & ELECTRIC CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
References
RO-77-03, RO-77-3, NUDOCS 8103020137
Download: ML19345G085 (2)


Text

LICENSEE EVENT REPORT

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tCENSE NUMBER YE Y

E lc lA In l:e lsl11 D lo l-1010101010 l-10 10l 14 l1 l il il il 10131 7 89 14 15 25 26 30 31.32 CATEGOAY Y

0 DOCKET NUVDER EVENT DATE REPO'RT DATE O 1 CONT l P l Ol (j W l 0 l 5 } 0l-l 0l Il 3l 3l l 0 l 8l 1l Sl 7l 7l l0 l 9 l 0 l 8l 7l 7l, 7 8 57 68 59 60 61 68 69 74 75 60 EVENT DESCRIPTION

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gg lDuring celd shutdown operations, the secondary containment (refueling building) auto-l 7 89 CO gg lmatic isolation feature monthly test, required by the Technical Specifications Section_l 7 89 EO gg lV11.E.5, was not performed as scheduled.

It was performed four days af ter the l

7 83 GO f l scheduled date but plant procedures allow only a two-day extension of the test date forj 7

89 E:0 g l monthly tests. This is a repetitive event (not all surveillance tests have always l

(cont) 80 7 89 psus cNE coof COMPONENT CODE R

MANUF UrER VOLATON ME l5lDl B l Il Nl Sl Ti R; Uj lAl lZ l9 l9 l9 l lY l 7 89 10 11 12 17 43 44 47 48 CAUSE DESCRIPTION gg l Administrative error in interpretation of Technical Specification requirecents and l

7 89 C3 l excessively restrictive plant procedures. Procedures will be changed, training will l

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OTHER STATUS D COvt AY DISCOVERY DESCAiPTON W

l0lGl0] l N/A l W l Review of test data l

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10 12 13 44 45 46 80 tt s O

E ACUNJ OF ACTMTY LOCATON OF RELEASE gg

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10 11 44 45 80 PERSONNEL EXPOSURES NUMDE A.

TYPE DE ScAFTON H 10101 0l tz j l

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7 89 11 12 13 80 PERSONNEi INJUR!ES NUMPER DE 5cnirTcN I

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7 89 11 12 OFFSITE CONSEQUENCES l

gg l None 7 89 80 LOSS OR OAMAGE TO FACILITY

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' 10 80 PUBLICITY M lN/A l

7-89 80

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ONAL FACTOAS

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7 89 80 707-443-2787 Navr Steve l Redeker PHONE:

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LICENSEE EVENT PEPORT A

EVENT DESCRIPTION (continued) been perfomed en schedule)e Corrective action planned includes

- revising plant procedurcs'.to increase scheduling flexibility and e

conducting training-regarding test scheduling and perforrance.. (LER-77-03).

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