ML19345G085
| ML19345G085 | |
| Person / Time | |
|---|---|
| Site: | Humboldt Bay |
| Issue date: | 09/08/1977 |
| From: | Redeker S PACIFIC GAS & ELECTRIC CO. |
| To: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V) |
| References | |
| RO-77-03, RO-77-3, NUDOCS 8103020137 | |
| Download: ML19345G085 (2) | |
Text
LICENSEE EVENT REPORT
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tCENSE NUMBER YE Y
E lc lA In l:e lsl11 D lo l-1010101010 l-10 10l 14 l1 l il il il 10131 7 89 14 15 25 26 30 31.32 CATEGOAY Y
0 DOCKET NUVDER EVENT DATE REPO'RT DATE O 1 CONT l P l Ol (j W l 0 l 5 } 0l-l 0l Il 3l 3l l 0 l 8l 1l Sl 7l 7l l0 l 9 l 0 l 8l 7l 7l, 7 8 57 68 59 60 61 68 69 74 75 60 EVENT DESCRIPTION
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gg lDuring celd shutdown operations, the secondary containment (refueling building) auto-l 7 89 CO gg lmatic isolation feature monthly test, required by the Technical Specifications Section_l 7 89 EO gg lV11.E.5, was not performed as scheduled.
It was performed four days af ter the l
7 83 GO f l scheduled date but plant procedures allow only a two-day extension of the test date forj 7
89 E:0 g l monthly tests. This is a repetitive event (not all surveillance tests have always l
(cont) 80 7 89 psus cNE coof COMPONENT CODE R
MANUF UrER VOLATON ME l5lDl B l Il Nl Sl Ti R; Uj lAl lZ l9 l9 l9 l lY l 7 89 10 11 12 17 43 44 47 48 CAUSE DESCRIPTION gg l Administrative error in interpretation of Technical Specification requirecents and l
7 89 C3 l excessively restrictive plant procedures. Procedures will be changed, training will l
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g lhe conducted.
sTAIUS
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OTHER STATUS D COvt AY DISCOVERY DESCAiPTON W
l0lGl0] l N/A l W l Review of test data l
1 7 8 9
10 12 13 44 45 46 80 tt s O
E ACUNJ OF ACTMTY LOCATON OF RELEASE gg
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]ASE l N7A l
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7 8 9
10 11 44 45 80 PERSONNEL EXPOSURES NUMDE A.
TYPE DE ScAFTON H 10101 0l tz j l
N/A l
7 89 11 12 13 80 PERSONNEi INJUR!ES NUMPER DE 5cnirTcN I
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80 V
7 89 11 12 OFFSITE CONSEQUENCES l
gg l None 7 89 80 LOSS OR OAMAGE TO FACILITY
- Pt otstnoTON D] [_Zj lN/A l
7 89
' 10 80 PUBLICITY M lN/A l
7-89 80
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ONAL FACTOAS
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7 89 80 707-443-2787 Navr Steve l Redeker PHONE:
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LICENSEE EVENT PEPORT A
EVENT DESCRIPTION (continued) been perfomed en schedule)e Corrective action planned includes
- revising plant procedurcs'.to increase scheduling flexibility and e
conducting training-regarding test scheduling and perforrance.. (LER-77-03).
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