ML19344B544
| ML19344B544 | |
| Person / Time | |
|---|---|
| Site: | Millstone |
| Issue date: | 10/01/1980 |
| From: | Harran G NORTHEAST NUCLEAR ENERGY CO. |
| To: | |
| Shared Package | |
| ML19344B540 | List: |
| References | |
| NUDOCS 8010210430 | |
| Download: ML19344B544 (6) | |
Text
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- l AVERAGE DAILY UNIT POWER 11 VEL 1
l DocKLT No. __50-245 s
UNir -
Millstone - 1 DTTE S01001 l'
l 3
COMPl.ETED llY G d aICAn t
TELEPil0NE._223.-s4) 'U.2 Ext. 6bu
.10NTil September l
l l
DAY AVER AGE DAll.Y POWER I.EVEL DAY AVER AGE DAILY POWER LEVEL (MWe-Net)
(MWe Neo 491 i
I ~
___.5 38 37 l
2 638 Is 618 633 608 3
39 4
640-20 601 t
5 639 21 598 6
638 22 596 7
634 23 594 8
633 24
=c92 l
9 630 25 592 l
10 625 26 590 l
-11 624 c
27
_d8 621
.585 12.
,g l
13-619 29 582 1
- 14 616 30 53 15 615 3:
16 613
~
I
' INSTRUCTIONS r
' On this forrnat. fist the average daily unit power levelin MWe-Net for each day in the rep 6rting mdnth. Compute to the nearest whole megawait.
_ :MDC of 654 based on commitment to New England Power Exchange.
(9/77) t 18 o 1021e'/3R
P
~
OPERATING DATA REPORT DOCKET NO. 50-245 DATE 801001 I-
'CO.\\tPLETED 11Y G. Harran f'
TELEPl!ONE 203-447-1792 Ext. 655 Ol'ERATING STATUS Notes '
I.~ Unit N:nne:
11111stene Unit 1
- 2. Reporting Period:
SEDtember 1980
- 3. Licenced Thennal Power (SIWt):
2011 662-
- 4. Na ieplate Rating (Gross $1We):
- 5. Design Electrical Rating (Net 31We): _f 0 684
~ 6. Af aximum Dependable Capacity (Gross 5. 'e):
- 7. 51asimum Dependable Capacity (Net 31We):
654 S. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report. Gise Reasons:
Although the ratings have not changed, the unit is presently on an end-of-cycle coastdown with feedwater temperature reduced.
- 9. Po..er Level To which Restricted. If Any (Net 31We): NA NA
- 10. Reasons For Restrictions. lf Any:
This afonth Yr.-to.Date Cumularise 720 6,575.0 '
r.
86,255.0 II, Ifours In Reporting Period -
r
- 12. Number Of !!ours Reactor Was Critical 720 5,986.0 65,371.0
- 13. Reactor Resene Shutdown llours
- 0 592.3-1,527.3 14.!!our: Generator on.Line 720 5.954.0 64.049.9
- 15. Unit Reserve Shutdown llours 0
26.5 26.5
- 16. Gross Thermal Energy Generated (51WH) 1,369,333 10,359,790 114,407,735
- 17.' Gross Electrical Energy Generated (11WH) 459,500 3,519,447 38,750,843
- 18. Net Electrical Energy Generated (51Wil).
438,444 3,360,650 37,000,432
- 19. Unit Senice Factor 100.0
'90.6.
74.3
- 20. Unit Availability Factor 100.0 91.0 74.3
- 21. Unit Capacitv Factor (Using N1DC Net!
93.1 78.2 65.6 92.3 77.4 65.0
- 22. Unit Capacity Factor (Using DER Net)
- 23. Unit Forced Outage Rat,.
0.0 0.2
-15.4
- 24. Shutdowns Scheduled Oser Ne.st 6.\\fonths (Type.Date,and Duration of Each1:
Annual refuel and maintenance outage-scheduled to commence October 4,1980 for annmvi-a tely 11 wein NA
- 25. If Shut Down At End Of Report Period. Estimated Date of Startup:
- 26. Units In Test Status (Prior to Commercial Operationi:
Fore est Achieved I
INITIA L CRITICA LITY INITIA L ELECTRICITY NA CO.\\l%tERCl% L OPER ATION q[
y q
gh diru.=.
cif77)
Page 1 of 2 OPERATING HISTORY
_ September 1, '1980 Steady state 97% power.
September 3,1980 0015 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br /> -
Reactor power reduced to 90%
for Turbine Stop Valve Testing and Main Condenser Backwashing.
0135 hours0.00156 days <br />0.0375 hours <br />2.232143e-4 weeks <br />5.13675e-5 months <br /> Turbire Stop Valve Testing and Main Condenser Backwashing comple te.
Increasing reactor power to 98%.
0230 hours0.00266 days <br />0.0639 hours <br />3.80291e-4 weeks <br />8.7515e-5 months <br /> Reactor power at 97%.
September 5,1980 Reactor power at 99%.
(Unit begins it end-of-cycle coastdown with feedwater temperature reduced.)
September 10, 1980 0013 hours1.50463e-4 days <br />0.00361 hours <br />2.149471e-5 weeks <br />4.9465e-6 months <br />' Reducing reactor power for Turbine Stop Valve Testing.
0050 hours5.787037e-4 days <br />0.0139 hours <br />8.267196e-5 weeks <br />1.9025e-5 months <br /> Turbine Stop Valve Testing complete.
Reactor power at 97%.
l
_ Sep tembe r 17, 1980 1005 hours0.0116 days <br />0.279 hours <br />0.00166 weeks <br />3.824025e-4 months <br /> Reducing reactor power to maintain condenserd T limits.
1135 hours0.0131 days <br />0.315 hours <br />0.00188 weeks <br />4.318675e-4 months <br /> Reducing reactor power to_40%
to repair leaking main condenser l
tubes.
1300 hours0.015 days <br />0.361 hours <br />0.00215 weeks <br />4.9465e-4 months <br /> Reactor power at 40%.
Turbine Stop Valve Testing started and completed.
l 1720 hours0.0199 days <br />0.478 hours <br />0.00284 weeks <br />6.5446e-4 months <br /> Main condenser tube leaks repaired.
Increasing reactor power.
Sep tembe r -18, ' 1980
.0730 hour0.00845 days <br />0.203 hours <br />0.00121 weeks <br />2.77765e-4 months <br />s-Reactor power at 96%.
1010 hours0.0117 days <br />0.281 hours <br />0.00167 weeks <br />3.84305e-4 months <br /> Reducing reactor power to 90%-
f
. September 24 '1980 0
for Turbine Stop Valve Testing.
0035 hours4.050926e-4 days <br />0.00972 hours <br />5.787037e-5 weeks <br />1.33175e-5 months <br /> Turbine Stop Valve Testing complete.
Increasing reactor power.
Page 2 of 2 0055 hours6.365741e-4 days <br />0.0153 hours <br />9.093915e-5 weeks <br />2.09275e-5 months <br /> Reactor power at 93%.
September 30, 1980 Reactor power at 90%.
i i
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50-245 DOCKET NO.
UNIT S!!UTDOWNS AND POWER REDUCTIONS UNITNAME Mil 1 stone - l DATE 801001 REPORT MONTil September COMPLETED HY G. Ilarran TELEPIIONE 203/447-1792 Ext. 655 n.
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Cause & Corrective No.
Date E.
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?'5N Event g,7 p.3 Action to g.2 3
g g c::
3mj Report st to o O
Prevent Recurrence c=
m 6
09
- 801017, S
0 8
4
- f1A IfC IITEXCll Reduced power to repair main condenser tube leaks. Power was increased following maintenance ~.
O Cess x
- 9b) r i
M DM Cd$
GEED
@W 2
3 4
F: Forced Reason:
Method:
Exhibit G - Instructions S:. Scheduled.
A Equipment Failure (Exp!ain) l Manual for Prep.uation of Data :
IbMaintenance of Test 2-Manual Scrarn.
Entry Sheets for l.Lensee.
C Refueling 3 Automatic Scram.
Esent Report (1.ER) File (NUREG.
D Regu!atory Restriction 4-Other (Explain)
.-01611' E-Operator Training & License Examination F.Adntinistrative 5
G Operational Error (E splain)
Exhibit I - Same Source (9/77)
II.Other (Explain) 4 4
2
REFUELING INFORI%TI0t! REQUEST 1.
'tiame of facility:
Millstone 1 2.
Scheduled date for next refueling shutdown:
Oct. 4, 1980-3.
Scheduled date for restart foll,owing refueling:
Acorox. Dec. 11. 1980 4.
Will' refueling or resumption of operation ~ thereafter require a technical specification change or other license amendment?
Yes. Technical Specification changes regarding:
(1) 11aximun Average Planar Linear-Heat Generating Rate (2) liaximum Critical Power Ratio 5.
Scheduled date(s) for submitting proposed licensing action and supporting in formation :
Submitted 6.
Important licensing considerations associated with refueling, e.g., new or different' fuel design or supplier, unreviewed design or performance analysis methods, significant changes in fuel design, new operating procedures:
168 " Retrofit" 8 x 8 fuel assemblies are scheduled for insertion in cycle 8 (reload 7).
7.
The number of fuel assemblies (a) in the core and (b) in the spent fuel storage pool:
-(a) In Core:
580 (b) In SFp:
776
~
8.
The present licensed spent fuel pool storage capacity and the size of any in-crease in licensed storage capacity that has been requested or is planned, in number of fuel assemblies:
2184 assemblies 9.
The projected date of the last refueling that can be discharged to the spent fuel pool assuming the present licensed capacity:
1985. Spent Fuel-Pool, full core off load capability is reached.
1991, Core Full, Spent Fuel. Pool contains 2120 bundles.
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