05000306/LER-1980-027-03, /03L-0:on 800919,steam Flow Transmitter 2FT-474 Found Reading Low.Caused by Zero Adjustment Shift in Barton Model 384 Differential Pressure Transmitter. Transmitter Recalibr.Transmitters Scheduled to Be Replaced

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/03L-0:on 800919,steam Flow Transmitter 2FT-474 Found Reading Low.Caused by Zero Adjustment Shift in Barton Model 384 Differential Pressure Transmitter. Transmitter Recalibr.Transmitters Scheduled to Be Replaced
ML19340B255
Person / Time
Site: Prairie Island Xcel Energy icon.png
Issue date: 10/17/1980
From: Hunstad A
NORTHERN STATES POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML19340B242 List:
References
LER-80-027-03L-01, LER-80-27-3L-1, NUDOCS 8010210705
Download: ML19340B255 (1)


LER-1980-027, /03L-0:on 800919,steam Flow Transmitter 2FT-474 Found Reading Low.Caused by Zero Adjustment Shift in Barton Model 384 Differential Pressure Transmitter. Transmitter Recalibr.Transmitters Scheduled to Be Replaced
Event date:
Report date:
3061980027R03 - NRC Website

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60 61 DOCKET NUMBE R 68 69 EVENT DATE 74 75 REPORT DATE 80-EVENT DESCRIPTION AND PROBABLE CSNSEQUENCES h 1012 l l During normal operation, steam flow transmitter 2FT-474 was observed to be l

lTT'n I reading low. At recalibration it was determined that the MSIV closure signal l

lO64l l and reactor trip signal from this channel would have occurred as much as 1.15%

l l0 isi l above the Tech Spec limits. Tech Spec Table 3.5-1 and -2 apply. Recent similar l

l0 is l l event was R0-80-08.

Appropriate bistables were placed in trip. No effect on l

['isTF1 I public health and safety.

Redundant devices were operable.

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