05000267/LER-1980-050-03, /03L-0:on 800915,during Piping Audit,Two Hydraulic Snubbers Installed on Class I Piping Were Not Routinely Tested.Caused by Snubbers Omitted from Testing Table Due to Oversight.Procedure Revised

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/03L-0:on 800915,during Piping Audit,Two Hydraulic Snubbers Installed on Class I Piping Were Not Routinely Tested.Caused by Snubbers Omitted from Testing Table Due to Oversight.Procedure Revised
ML19340B212
Person / Time
Site: Fort Saint Vrain 
Issue date: 10/14/1980
From: Gahm J
PUBLIC SERVICE CO. OF COLORADO
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19340B209 List:
References
LER-80-050-03L, LER-80-50-3L, NUDOCS 8010210656
Download: ML19340B212 (1)


LER-1980-050, /03L-0:on 800915,during Piping Audit,Two Hydraulic Snubbers Installed on Class I Piping Were Not Routinely Tested.Caused by Snubbers Omitted from Testing Table Due to Oversight.Procedure Revised
Event date:
Report date:
2671980050R03 - NRC Website

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