ML19340B212

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LER 80-050/03L-0:on 800915,during Piping Audit,Two Hydraulic Snubbers Installed on Class I Piping Were Not Routinely Tested.Caused by Snubbers Omitted from Testing Table Due to Oversight.Procedure Revised
ML19340B212
Person / Time
Site: Fort Saint Vrain Xcel Energy icon.png
Issue date: 10/14/1980
From: Gahm J
PUBLIC SERVICE CO. OF COLORADO
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19340B209 List:
References
LER-80-050-03L, LER-80-50-3L, NUDOCS 8010210656
Download: ML19340B212 (1)


Text

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MTE EVENT CESCRIPTION AND PROSABLE CONSEOUENCES h I

Io i2l l While the reactor was shutdown for scheduled maintenance and surveillance testin2.

t o 13 l l Engineering personnel performing an audit of 21/2" and larger piping identified two ,

I o I .a i l hydraulic snubbers (BFS-154E and BFS-166) which, although installed on Class I piping,[

}oIsIl had not been included in Table 4.3.10-1 of LCO 4.3.10 and were not routinely tested tog io is l l verify ooerability. Insbility to document snubber operability for past periods of re-f IC17I lactor operation is reportable oer AC 7.5.2(b)2 and AC 7.5.2(b) 3. No accompanying oc- l tata!Icurrence. No effect on gblj e health or safety. *

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44 47 CAUSE CESCRIPTION AND CCARECTIVE ACTIONS h l i t o l l Snubbers apparently omitted from Table 4.3.10-1 due to oversight during initial analy ;

l li1l sis. Snubbers inspected and tested per approved surveillance and maintenance pro- l 1,i?i icedures. Revision to SR 5.3.8a-X made to include the tuo snubbers. Revision to I

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