ML19339B471

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Monthly Operating Rept for Oct 1976
ML19339B471
Person / Time
Site: Yankee Rowe
Issue date: 11/05/1976
From: Tarnuzzer E
YANKEE ATOMIC ELECTRIC CO.
To:
Shared Package
ML19339B470 List:
References
NUDOCS 8011070028
Download: ML19339B471 (4)


Text

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DOCKET NO.

50-29

-j p y,,;; s;ur L i UNIT Yankee Rowc DATE 761105 COMPLETED BY.

E. C. Tarnu:zer

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TELEPl!ONE (617) 366-9011 X276 AVERAGE DAILY UNIT POWER LEVEL MONTt!

October 1976 DAY AVERAGE DAILY MWe-nct DAY AVERAGE DAILY.Wc-nc.

I 156-16 157 2

156 17 156 E:..

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3 155 18 157

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4 155 19.

159 p;

5 154 20 160 I~

6 154 21 160 I

7 154 22 157 8

154 23 157 157 9

154 24 156 25 157 to 156 26 157

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156 27 157 12 i'

156 28 158 L

13 155 156 29 14 157 30 2

15 102 31 I

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. COMPI(F.TED BY E. C. TAki.vZZER

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TELEPHONE (617) 366-9011 X276 2PERAllNG SIAIUS 1.

REPORTING PERIOD:

October 1976 GROSS !!OURS IN REPORTING PERIOD 745 2.

CURRENTLY AUTi!0RIZED POWER LEVEL MXt 600

-MAX DEPEND. CAP. (FMe-NET) 175

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DESIGN ELECTRICAL RATING (MNc-hET) 175 3.

PONER LEVEL TO WillCll RESTRICTED (IF ANY):

920 (553 MNt)

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REASONS FOR RESTRICTIONS (IF ANY):

Peak linear heat generation rate associated with ECCS cvaluation.

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MONTil YR-TO-DATE TO DATE

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HOURS REACTOR WAS CRITICAL 739 6538 115938

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REACTOR RESERVE SliUTDOWN HOURS 0

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HOURS GENERATOR ON-LINE 715 6432 110795 r=i 8.

UNIT RESERVE SHUTDONN HOURS 0

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GROSS THERMAL POWER GENERATED (MWH) 386,003 3,457,932 59,107,020 10.

GROSS ELECTRICAL POWER GENERATED (MNH) 119,18S 1,081,364 18,146,916 11.

NET ELECTRICAL POWER GENERATED (FNi) 111,973 1,014,092 16,984,255 12.

REACTOR SERVICE FACTOR 99.2 89.3 81.7

13. ' REACTOR AVAILABILITY FACTOR 99.2 8 9. t, 81.1 14.

L* NIT SERVICE FACTOR 96.0 87.9 79.2 15.

UNIT AVAILABILITY FACTOR 9C.0 94.0 S5.9 79.2 72.2 16.

UNIT CAPACITY FACTOR (USING MDC)

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85.9 79.2 72.2 17.

UNIT CAPACITY FACTOR (USING DESIGN MWe) 0.0 7.7 1.5 18.

UNIT FORCED OLTTAGE RATE 19.

S!!UTDONNS SCllEDULED TO BEGIN IN NEXT 6 MONTl!S (STATE TYPE, DATE AND DURATION

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20.

IF S!!U rDOWN AT l'.ND OF Rr. PORT l'I:l:10li. 1:STIMATI:D DATr. OF STARTUP:

N.A.

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]D 030 Y $

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DOCKET NO.

50-29 UNIT NAME Yankee Rowe DATE 761104 COSIPLETED BY E. C. TARN'UZZER APPENDIX D TELEPliONE (617) 366-901I X276 UNIT SIIUTDOWNS AND POWER REDUCTIONS REPORT MONTil October 1976 TYPE METil0D OF F-FORCED DURATION S!!UTTING DOWN NO.

DATE S-SCllEDULED (IIOURS)

REASON (1)

Tile REACTOR, (2)

CORRECTIVE ACTIONS /CO5NENTS

/6-5 761030 S

30 A

2 Repair Icak in #1 feedwater heater.

SUM'.fARY :

Shutdown on October 30 ended a continuous power run of over 162 days.

Plant returned to service upon repair of leak in #1 feedwater heater.

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NHC oonu 105 u.s. hucLE An atoutATonE ul' acN occxe7 NuurE n o.m 6:.

59-29 s

n RC Dl'STRIBUTION ron PART 50 COCKET MATERIAL "h'ohQ'y" REPORT TO:

FROM:

DATE oF DOCUMENT Yankee Atomic Clectric Com,any 11/5/76 N. R. C.

fles tborough, 'fass.

DATE RECEiVECs

.J. L. French 11/19/76 XLE TrE n OnoTonizEo enor iravTronu NuueEn oF COPIES RECEIVED O onlGIN AL jfuNC LASSIFlit o One signed copy K ory DESCRIPT60N ENCLoSu sar LETTER TRANS T!!E FOLLO'4ING:

MONTHLY REPORT FOR October. 1976 PLANT & COMPONENT OPERABILITY &

AVAILABILITY. T1 3 REPORT TO BE USED IN FREPARING GRAY BOOK BY PLANS & OPERATIONS.

D63.d.MWe_

PLANT NAME:

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Yanken. Rowe JLH FOR ACTION / INFORM ATION Li'VlMV 11/19/76 RJL fEJEC I I b'/4 C_yS FOR ACTLON

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