05000313/LER-1980-027-03, Average Gross Gas Release Rate for 3rd Quarter Was Exceeded.Caused by Presence of 0.19% Failed Fuel & Two Shutdowns.Attempts Will Be Made to Repair or Replace Failed Fuel

From kanterella
(Redirected from ML19338G179)
Jump to navigation Jump to search
Average Gross Gas Release Rate for 3rd Quarter Was Exceeded.Caused by Presence of 0.19% Failed Fuel & Two Shutdowns.Attempts Will Be Made to Repair or Replace Failed Fuel
ML19338G179
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 10/16/1980
From: Bramlett L
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19338G175 List:
References
LER-80-027-03X, LER-80-27-3X, NUDOCS 8010280552
Download: ML19338G179 (1)


LER-1980-027, Average Gross Gas Release Rate for 3rd Quarter Was Exceeded.Caused by Presence of 0.19% Failed Fuel & Two Shutdowns.Attempts Will Be Made to Repair or Replace Failed Fuel
Event date:
Report date:
3131980027R03 - NRC Website

text

>

UPDATE REPORT - PREVIOUS REPORT DATE 4/16/80 i

NRC FOnu 354 U. s. NUCLI Aa aEGULATOnY COametsssow LICENSEE EVENT REPORT EXHIBIT A CoNinot eLoCx: l l l l l l l@

iettAss eniNT on vyet ALL atouinto iNronuatioNi

@ l AlR l Al Nl 0 l 1lgls010 l - 10 l 0 l 0l q 0 l-l 0 l0 lg l1 l 1 ]l l 1 lgl l lg I

e e tsCthltt Coog is i

UCamst NuMBtM

)$

3E La(k Nb( jv,4 JQ b) C.: bg p'T,

40 al DoCESThuusta to 03 EvtNT D.TE I4 P%

HF,OMID.Tt 90 CON "l,u' "C LL_J@l0 i s 10 10 i 0 is il 13 j@l o i 7:215le 10 i@il i 0111618101@

S EVENT DESCRiPflON AND PROBA8LE CONSEQUENCES [dD IDuring a plant shutdown for a G tube leak, on 7/25/80, the average i

t gross gas release rate for 3rd quarter was exceeded per E.T.S. 2.4.2.3a. I r==

Following a 9/23/80 OTSG tube leak, an E.T.S. change was requested and i

i o.

iapproved by the NRC retroactive to the beginning of the 3rd quarter.

o 3 iThe previous releases when applied to the revised E.T.S. resulted in i

o e ITrr) texceeding section 2.4.2.1 which was not specified previously.

The i o n,i irelease was 12 MRAD Beta where the limit is 10 MRAD.

LER 50-313/80-066 i

.was samii,ag, Kep,o,qt,aole,,gr t..

.d.

o.b.z.o.

==

CODE CCD(

Su8 CODE COMPONENT COut

%un e)ut nutetODI I Zl Z l@ [_X_J@ L,,Z__l@ lZ l Z lZ l Z lZ l Z l@ W@ [Zj @

o e

,o u

,o Ltarmo IVENTVI.R Rt T O E

v h

@,ajgt 18101 L--J 10 :217 1 a

10131 W

L--J ll_J 2%

27 23 24 26 2r 7s 29 Jo 3

3J l01070 J

l l Ig 33 34 JS 36 33 d0 el 42 43 44 er CAUSE DESCR6PTION AND CORREC flVE ACTIONS

, o iThe quarterly releases were significantly impacted by the occurrence of i

itwo shutdowns during the quarter for the repair of 0TSG tube leaks and i

ialso the presence of approximately.19% failed fuel. An attempt will be i Imade to identify, replace or repair the failed fuel at the next refueling i

, 3 ioutage.

i.

i

'd'.'Ws' ov e.1.vus @

",'dM n32 uo..

osCov, o

LGJ@ l 010101@l NA l LA_j@l Radiochemistry "Sur,3C,,,,,iTahte l

vel i s

".a,viiv Can~1 a

a l12 NO[6'het'U l

lRxBldg.Venf0i'Et"doTilhhe o IGj'[h'* ses i

l

',..so~~ t i,o.s ot.C...,,o @

ao

..u...

10l0l0l@lZ_J@l NA i i l

,o.so=~d'.~;u'4 s ea otsC...r o @

~u..

10 l 0l0 l@l NA i =

l is n

1 tNs ' o Yn,r$og "h

LI.J@l NA

' =

l i.

oE At# TION NRC USE ONLY glsygl@l E

NA 1 llg;;;;;;;;,l 2 a "d5/968-2519 1.. S. Bramlett 5

NAucorene,Anta 8 m eso5'51.