05000313/LER-1980-032-04, /04L-0:on 800905,during Cooldown Following Steam Generator Tube Leak,Excessive Release of Radioactive Matls in Gaseous Wastes Occurred.Caused by Premature Lifting of Letdown Relief Valve PSV-1236.Valve Was Readjusted

From kanterella
(Redirected from ML19338F126)
Jump to navigation Jump to search
/04L-0:on 800905,during Cooldown Following Steam Generator Tube Leak,Excessive Release of Radioactive Matls in Gaseous Wastes Occurred.Caused by Premature Lifting of Letdown Relief Valve PSV-1236.Valve Was Readjusted
ML19338F126
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 10/01/1980
From: Shively C
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19338F117 List:
References
LER-80-032-04L, LER-80-32-4L, NUDOCS 8010070549
Download: ML19338F126 (1)


LER-1980-032, /04L-0:on 800905,during Cooldown Following Steam Generator Tube Leak,Excessive Release of Radioactive Matls in Gaseous Wastes Occurred.Caused by Premature Lifting of Letdown Relief Valve PSV-1236.Valve Was Readjusted
Event date:
Report date:
3131980032R04 - NRC Website

text

..

m.f I

NRC PORM 366 U.S. NUCLE AR REGULATORY COMMtsSION LICENSEE EVENT REPORT EXHIBIT A CONTROL BLOCst: l l l l l l lh (PLEASE PRINT 04 TYPE ALL REQU1 RED INFORMATION) i 6

l AlR l A l Nj 0 l 1lg[S0l0 l-l0 l0[ 0l q 0l- [0l0 l g l1 l1l1 l1lgl l lg o i 9

tICiNsis CoDg to 1

teceNssNuuBiH 2$

26 LiciNhi ITFE JO b 7 c AI t.l 9

8 CON *7

"'Tc! [L_J@l0 l 510 1010 l3 l 1131@l 019 I 01518 I Ol@l 11010 '1 I R l Ol@

p8,

60 68 DOcat ei NUMS.R 68 M

iveNT DAT.

34 iS HE,OMTDAY.

80

,,u EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES o, i During cooldown following a st m generator tube leak, the rate of release i of radioactive materials in gaseous wastes was such that 1 MPC at the site ran Iboundary was exceeded, assumina worst case meteorology conditions (2.2 1

o 4 IMPC at site boundary).

Actual meteoroloav conditions proiected 0.25 MPC l e s oa lat site boundary.

RCS letdown was immediately secured on hiah stack mon-1 Iitor indication.

No similar occurrences.

Reportable per ETS 5.6.2.b dueI o >

i c i= I I to violation of 2.4.2.3.a.

su',E s"Midia

' CSS"

ci!

s'. cili co,o~i=rconi g

IC l B l@ [E_J@ @J@ lV l All l VIE l X I@ W@ @j @

[

i'3"ot'N'

"'F N'" h i

- vi~,

@,a'=,..,o18101 L-J 101312 l M

1014l LLJ

[--J O

n

,,, 3 9 23 33 34 26 2B 18 29 30 31 32 s'u ACTIO L

T u7 wouns 22 59

.T

,Om vee ti uaN Actunen Amen LE_J@[_zJ@ Lzj g tzj@

l 01010:o i LNj@

[_NJ@

LA_J@ lC15l6l7l@

33 34 JS 36 3

40 el 42 43 as er CAUSE DESCRIPTION AND CORRECflVE ACTIONS gi The letdown relief valve, PS 1236, lifted prematurely.

This sent RCS FTTr1 ifluid to the Auxiliary Bldo. Eauipment drain tank, which allows cas to i

tvent through the plant exhaust plenum.

The relief valve was adjusted to i GID I the proper setpoint.

I I

[E) I 1

~

'd'.'WA" orHea si tus @

T>,cMN Operator Observation @

v oona o scovinv oisc,..,no,,

l E LoJ@ 101010181 NA l

[A_J@l l

l

  • !nony co,iviur a

l P1 ant Exhaust M u"6"*" b

"'@'[QI

'" 176' &Y'*""

l i s

',. so=~'it i.,o,ssis oisc..1,

,,u....

10101 Ol@0@l NA l

i i

=

easo=,..'t' ou'n',is oisca.,no=@

uu.. a 101010l@l NA l

i u

' 'os,s,o, oa,o" ac,i[o,.ciurv g (1,J@l NA l

i o

""k7c,,,,o.,@

NRc use oNLY

. $. 61 2 o NA 1 llllll[illlll Chris N. Shively MMMM NAME OP PREPARER

, goy,;

8010070 %