ML19338D534
| ML19338D534 | |
| Person / Time | |
|---|---|
| Site: | Arkansas Nuclear |
| Issue date: | 09/15/1980 |
| From: | Pendergraft R ARKANSAS POWER & LIGHT CO. |
| To: | |
| Shared Package | |
| ML19338D533 | List: |
| References | |
| NUDOCS 8009230410 | |
| Download: ML19338D534 (6) | |
Text
..
3 AVERAGE' DAILY UNIT POWER LEVEL.-
DOCKET NO.
~50-368
~
UNIT 2
DATE 9/ 15/ 80 COMPLETED BY' Rex Pendergraft -
TELEPHONE _(501) 968-2519 MONm
~ August; 1980 D AY-AVERAGE DAILY POWER LEVEL ~
DAY AVERAGE DAILY POWER LEVEL
.(MWe Net) ggwe.geg) 1 R65 g7 794 2
- 865 599 is 3
868 i9 195 4
- 866 20 838
-5
- 866 21 743 6
864 22 0
7
~ ~864 742 23 8
864
-24 867
~
'9 865 25 865 lo 865" 26 865
-11
- 80 8 865 27 12 _
827 33 868 13-
- 866 29 871 14 866 871 30 3
869
. 15.
531' 16 19 8 l
l INSTRUCTIONS.
On this format list the avenge daily unit power lesel in MWe-Net for cach day in the reporting month. Compute to the nearest whole megawatt.
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- OPERATING DATA REPORT DOCKETNO. 50-368 DATE 9/1b/80
. COMPLETED BY KeX Pendergraft TELEPHONE (bu11965-z519
' OPERATING STATUS '
1.' Unit Name: Arkans as i Ny. clear. One - - Uni t 2' Notes
- 2. Reporting Period: ' Augus t 1 - 31. lo Art "3. Licensed Thermal Power IMWtli:
2815:
- 4. Nameplate Rating (Gross MWeji
-959 L 5." Design Electrical Rating tNet MWe):
912
~
~
J6. Maximum Dependable Capacity (Gross MWe):
- 7. Maximum Dependable Capacity (Net MWe):
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report. Give Reasons:
NONE 1
-i
- 9. Power 1.evel To which Restricted. lf Anv (Net MWe):
NONE N/A
- 10. Reasons For Restrictions. lf Any.
2 u
- This Month Yr..to-Date Cumulative.
i
- 11. Hours in Reporting Period.
'744.0 3815.0 3815.0 i
J12. Number Of Hours Reactor Was Critical 700.1
'3148.2 3148.2
- 13. Reactor Reserve Shutdown Hours 42.4 124.8
-124.8
-14. Hours Generator On-Line
'691.7 3099.9 3099.9
- 15.. Unit Rewne Shutdown Hours -
0.0 75.0 75.0
- 16. Gross Thermal Energy Generated IMWH) 1845897.0 7773645.0 '
7773645.0 ~
- 17. Gross Electrical Erbrgy Generated (MWH) 593560.0 2523800.0 2523800.0
- 18. Net Electrical Energy Generated (MWHI ;
566350,0 2404879.0 2404879.0-
- 19. Unit' Service Factory 93.0
-81.3 81.3 4 20. Unit AsailabilitiFactor ;
93.0 83.2-
<83.2
~!
83.5 69.1~
69.1
- 21. Unit Capacity Factor (Using MDC Net) 83.5 64.-1 69.1-
- 22.. Unit Capacity Factor (Using DER Net).
- 23. Unit Forced Outage Rate' 7.0 18.7'
- 18.7
- 24. Shutdowns Scheduled 0 er Next 6 Months (Type. Date and Duration of Each):
3
' March :15 -.1981 to May '15,1981. Refue1ina
~
225. If Shut Down At'End Of Report Period. Estimated Date of Startup:.
- 26. Units in Ted StatA (Prior to Commercial Operation):
Forecast Achieved
~,1NITIA L CRITICALITYJ
- INITIAL ELECTRICITY -
- COMMERCIAL OPERATION -
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' UNIT SilU FDOWNS AND POWER REDUCTIONS.
DOCKET NO.
50-368J
^
UNIT NAME.. ~ ANO-Ifni e 2 -
-DATE W D M COMPLETED llY ne.- p - a- --.ct:
REPORT MONTil August
.TELEPilONE 501 968-25f9
?
er,
- 1 1
'.., 34 s X' Licensee
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'Actinn io
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Cause & Corrective.
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Date t'
ig 4-js&
Event ag e.
Report = '
LE O 5'
Prevent Recurrence ~
5 H
5 @ :{
U C
80-16 8-15-80l
-F 13.1 G
3 None WG ZZZZZZ Lost stator cooling.w'ater due"to human
~
- error while switching Control 4 Room-chillers and main chillers.
80-17
'8-16-80 F
5.0 A
3
'.ione CH.
PIPEXX Low S/G level trip from -17%-power due to faulty control oil line. fitting.
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Fitting was replaced.=
80-18
.8-18-80 F.
8.6 A
3 None Cll INSTRU Low S/G level tripifroml full power due to blown fuse in feedwater' control.
system cabinet..-Fuse was: replaced.
W 9
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F3 W
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h c) - l-3 3-l1 F: Forced Reason:
Method:
Exhibit G. Instructions LM-
. S: Scheduled.
A Equipment Failure (Explain) 1-Manual for Preparation of Data B-Maintenance of Test.
2 Manual Scram.
Entry Sheet 5 for I.icensee r1 C Refueling 3 Autonfatie Scram.
Event Report (Ll'R) File (NUREG '
b D. Regulatory Restriction Other (E xplain) 0161) li Operator Tiaining & License Examination F-Administrative 5
(, Op. gtion..I lis ro t Expliia)
Exhibit I-Same Source Py / /)
Il Other (Explain)
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. DOCKET NO. c 50--368 -..
.f. s. p UNIT SilUI'llOWNS AND POWER REDUCTIONS.
UNIT NAME, ANO-Unit'~ 2 -
4 DATEI 9[9/W
..-COMPLETED BY1. Rav Paviovovert:
- REPORT MONTil August TELEPIIONE ' snt or,n_9 d_o_
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Cause & Corrective-N5.
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80 :8-21-80' F-25.6 G
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.None IA INSTRU~
Human error:,DNBR/LPD_ trips occurred -
~ on' the CPC's 'due to improper'. switching ',. ',
of inverter'~ power.
(Station battery
'~,
to AC),
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. F; ? Forced -
Reason:
Method:
Exhibit G. tnstructions S. Scheduled A-Equipment Failure (Explain) 1 Manual
? for Preparation of Data -
B-Maintenance of Test - '
2 Manual Scram.
Entry Sheets for. Licensee C-Refueling.
3 Automatic Scram.
Event Reppet (ITR) File t N1IREG-D. Regulatory Restriction 4 Otheg (Explain)-
0161)
~
E-Operator Tsaining & Liu nse lixamination F Admin:strative 5
G-Operational *. mr (l' iplaial Exhibit I Same Source 19/ 4 )
Il-Other ( E @ lam) si
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. September,,1980 "
- DATE:
M REFUELING ~INFORMATION*
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r 71h Name of facility Arkansas Nuciear 0ne:-- Unit:2i i
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2
}2.
Scheduled-date!for nextirefusling shutdown.
3/15/811 i
s 3. - Scheduleid.date for restart'following. refueling..
5/ 15/ 81
/q n.
?4. -- =Will' refueling.or resumptionLof~ operation thereafter require-a>
technical specification change:or other license amendment? -
. If Lanswer is~ yes', yhat; in general,iwill these be?
'If ' answer -is no, has -the. reload fuel design and core configuration been: reviewed by your: Plant' Safety Review. committee-to determine.
- whether any unreviewed-safety! questions!are; associated with the
' core reload ((Ref.-10-CFRtSection-50.59)?-
-Yes. ' Description of effects of new core loadino.
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5.
- Schehuled-date(s) for submitting' proposed licensing action and
~
supporting:information.- 1/ 15/8 1-6.-
Important licensing considerations associated with' refueling, e.g.,
'.newfor'different fue15 design or supplier, Onreviewed design or performance analysis methods, significant. change's in fuel design, 7
- new operating procedures.
p As part of a'research and development effort.-two fuel assemblies-will? be loaded possessing design characteristics related to ' extended burnuD.
i-The number of-fuel assemblies (a) in' the core and (b) in the spent.:
7.'
fuel storage poo1~.~
a) 1177' b) S8"(New, normalTy stored in
?,_
- n new fuel.p1t) l.
. 8.'
The presentW11 censed' spent fuel l pool storage capacity and the size.
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f i
offany l increase in l' censedistorage capacity that has been requested
?or -is; planned,:;in number of' fuel ~ assemblies.
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- present-J486I
-increaseisize by 0
E
. 9'. [The~ projected 'date of,the last' refueling that can'be discharged
'S to the._ spent 1 fuel ^poolfassuming the present licensed capacity.
< :D' ATE:
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?NRC MONTHLY OPERATING REPORT s,
OPERATING
SUMMARY
.- AUGUST,,1980
_ UNIT II-p The Unit was operating 'at 100% power at the beginning;of this
~
reporting period. A brush fire under the 500 kv transmission
- line forced a' power reduction-to approximately 55% power on
' 8-11-80._ ;; A return _.to '100% power.was -accomplished early. in the morning on 8-12-80.
The Unit - tripped. from 100%. full power on the 15th of ' August;due' to loss.of stator cooling water (human error) to the' main generator. ~High generator amperage caused a generator runback. The reactor tripped on high RCS pressure.
While-returning to power on 8-16-80, the ~ reactor tripped from
_ j
~
approximately 17%'fuir power dueito low steam generator level.
~
Investigation revealed an oil leak. on the electrohydraulic
=
' control oil' system for.the' main feedwater. pumps causing the steam ~ generator level'. problem. - A faulty oil line fitting'was replaced'and.a return to 100% full. power operation was accom-
~
plished on. 8-17-80.
On 8-18-80 a blown fuse in:the main feed-
- l water control cabinet caused-a reactor trip'from.100% power duetto_ low steam generator level..The blown fuse was replaced and 100% power operation ~was reached on 8-19-80.
A brush fire under-a 500'kv transmission ~line caused a forced power reduction
- to_approximately 60% power on 8-21-80.
While returning to full
~
. power. operation,:a. reactor trip was experienced from 90% power.
DNBR/LPDl trips were received on the "B" & "D" core protection calculators causing the. trip logic to automatically trip the
~
reactor.
Cause.of the.DNBR/LPD trips were attributed to human
~
error. An. improper method.of transferring inverter power from R
station batteries to primary AC caused a voltage spike _which.
initiated.the DNBR/LPD trips. The Unit returned to 100% full power on 8-23-80;and has operated at full power for the' remain-der of the reportin'g period.
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