ML19332G471

From kanterella
Jump to navigation Jump to search
Monthly Operating Rept for Nov 1989 for Jm Farley Nuclear Plant Unit 2.W/891214 Ltr
ML19332G471
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 11/30/1989
From: Hairston W, Dennis Morey
ALABAMA POWER CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NUDOCS 8912210288
Download: ML19332G471 (5)


Text

{{#Wiki_filter:'~ i

2q,. g. 7 4 ';
                              ' :,' ' Alabama Power Company
         '           ' * '-             4b inverness C* ntir Park 2ay

' Post Office Box 12951 Birmingham, Alabama 35201

  • Telepitone 205 068 5581.

W. G. Hairston, til *

                                       ~ Senior Vice President                                                                               .

Nuclear Operations Alabama Power the southern electrc systtyn December 14, 1989 , i Docket No. 50-364

                                      ~ U. S. Nuclear kegulatory Comission
                                      . ATIW: Document Control Desk washington, D..C.              20555 m                                                             Joseph M. Farley Nuclear Plant Unit 2 Monthly Operating Data Report Attached is the. November 1989 Monthly Operating Report for Joseph M. Farley Nuclear Plant Unit 2, required by section 6.9.1.10 of the Technical                                  .

Specifications. If you have any questions, please advise. Respectfully submitted, M

                                                                                                       . air on, I I JGS:sme/1.5 Attachment                                                                                            ,

cc: Mr. S. D. Ebneter Mr. E. A. Reeves i Mr. G..F. Maxwell i 1

                                .8912210288 891130
                                *PDR' ADOCK 05000364 iR                                PDC                                       dj 1

J S _ _ . .

59%T"% f  ;% ' 4 , c;0 - M-[ , $h#_mllal;f? A'R : g.- m y' ';;g, , p, ; ;,y g ,v . ' y! * ~ r $jg?

            !gfg L~'.

N. w.-].; p.7 y ;< < JOSIGH ! M.5 FARIEY -NUCLEAR PIANT <

                                                                                                                                                 ; UNIT 2.
         ,fM                                            ,

s NARRATIVE SUl+1AIN OF OPFRATIONS g J 0Cn- # ~ November,;1989-

i. 'j b. . A y- ,
                                                                                             -i--              .
                                                                                                                   ,;H      d.          . . . . ,
                       ,, ,                           2At 0433 on Novemler 18;1the reactor tripped following ' tJie loss of the .

4,,i Linverter which supplies: power toi.the Dinic system.'7 The unit-returned to Mi:/ m u.7, power operation at- 0455 on November 19. w. g w.-. ;Theffollowing major-safety-relatod'maintenarce was performd'in the inonth - ' is y~ Lof.Novemter:' uMs

       's              ti.                                                                                                              1
                                                                                                                                                            -(-

[- 4 R' @ - ' T. . ) Preventive maintenarceL.was tw rfonned on the 20 charging pump.-

           ;mmy g                              P                                        2. f A'celllwaa' replaced' in the auxiliary building B Inttery.
           =j; >
                                                                  '3.y Nitrogen Jcaks were repairal on the:2A' accumulator.
   ;               g.
 ;                   .q:                                          (4.; Radiation monitor R-2_5A'was replaced.
            ,y y                                                                  .'5.- Some high ehergy 'linell5reak sensors were recalibratal.-
m
                                                                 -1   6L-Miscellaneous correctiveLand preventive maintenance was performed on 4                                                        1
the ' diesel generators.

qq .

                                                              .-n   '

i

     ..,.a q
v $ V y 3
                       's         np     I
                                                                           -{..-

Wh . , i

                 -3 ;                                                  <
                                                                                                    .(
1 . , ,

M , t

f. s. ,

m., . . , m.- ,

.t  ; 5 .k y.tig. n '
                                  +

g i E j-[ , .

                                           ,~.'                                                                                                                                                       -
                ~
                                           ?

I' ,'-

           .'4'.._.

in ,

                                                                                                                                                                                                        ?

4 v+ ,. l k 1: ) (' u s t i

   ~
                                      .'r.                                                                                                                                                          .J,
                                                                                                                                                                                                  'l
                                                                                                                                                                                                    .1 70.0i                             ,
                                                                                                                                                                                                 .l
                                                                                                                                                                                                    -1
 ,-               ..p                  ,                                                               -
            %.jj j[                  :15~       -

i

 ,     .ap i . ..                                             >

I

i

             * .~

s, OPERATING DMR REPORT DOCKET NO. 50-364 DME _12/6/89 CCMPLETED BY D. N. Morey l

                                                                              'IELEPHONE (205)899-$135 i

OPERATING S'IR'IUS Notes I

1. Unit Name: Joseph M. Farley - Unit 2 -
       -2. Reporting Period:     November, 1989                             1) Cumulative data since     ,
3. Licensed Thermal Power ( M t): 2,652 7-30-81, date of
4. Nameplate Rating (Gross We): 860 comercial operation
5. Design Electrical Rating (Net MWe): 829
6. Maximum Dependable Capacity (Gross MWe): 870.3
7. Maximum Dependable Capacity (Net MWe): 829.7
8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons: N/A
9. Power Level To Which Restricted, If Any (Net MWe): N/A
10. Reasons For Restrictions, If Any: N/A
                                                           'Ihis Month      Yr-to-Date     Cu mlative   i
11. Hours In Reporting Period 720 8,016 73,105
       '12. Number Of Hours Reactor Was Critical               702.3            6,461.2       55,933.9
      ' 13. Reactor Reserve Shutdown Hours                        0.0               0.0           138.0
14. Hours Generator On-Line 695.6 6,295.4 62,328.0
15. Unit Reserve Shutdown Hours 0.0 0.0 0.0
16. Gross Thermal Energy Generated (MWH) 1,815,074 16,086,752 158,284,388  !
17. Gross Electrical Energy Generated (MWH) 600,696 5,273,398 52,008,884
18. Net Electrical Energy Generated (MWH) 571,776 4,990,412 49,315,698
19. Unit Service Factor 96.6 78.5 85.3
20. Unit Availability Factor 96.6 78.5 85.3
21. Unit Capacity Factor (Using MDC Net) 95.7 75.0 82.5
22. Unit Capacity Factor (Using DER Net) 95.8 75.1 81.4
23. Unit Forced Outage Rate 3.4 5.2 4.6
24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Eacl):

N/A

25. If Shut Down At End Of Report Period, Estimated Date of Startup: N/A
26. Units In Test Status (Prior to Commercial Operation): Forecast Achieved INITIAL CRITICALITY 05/06/81 05/08/81 INITIAL ELECTRICITY 05/24/81 05/25/81 COMMERCIAL OPERATION V8/01/81 07/30/81 l

l Form 2/30 l'

(v ,

    - *i:   .

p-( . L DOCKET NO. 50-364 UNIT 2 . DATE DECEMBER 6, 1989 COMPLETED BY D. N. Morey TELEPI)ONE (205)899-5156 - MONDI Noveaber si  ; DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) (MWe-Net) r 1 839 17 846 i i 2 840 18 135 3 844 19 229

                 '4              844                            20             828 5             841                            21             838                          ,

6 835 22 835 7 831 23 844 8 831 24 845 9 838 25 841 10 840 26 838 11 841 27 845 12 839 28 833 t 13 836 29 845 14 832 30 847 15 828 31 16 842 INSTRUCTIONS On this fornet, list the average daily unit power level in MNe-Net for each day in the reporting month. Compute to the nearest whole megawatt. l-Form 13/21 l

O e 7

                                                                                                                                                                           ~.          _.

UNIT SHUTDOWNS AND POWER 1*D(JCTIONS DocIET NGh 50-364 -"' a -[ UNIT 3AME J. M. FARMY -- UNIT 2 . /.' DATE' ~- DECEMBER 6, ' 198 9 , COMPLETED ST D. N. MMtET '*

                                                                                                                                                                                             ,]

REPORT MONTH KoVEMBER TELEPHO!T ( 205)8M-5156 1 I l' I I I METuoD or i 1.rcENSEE l l l. cAUSE & coRREcTzvE -1.

I- 1 I I DURArroN~ l i SnUTrzNo I EVENT I SYSTEM i coMroNENr i AcrrON TO . -P
                                                                               ; ,,,,,, , ; c,,,4     ; c,,,5 1

INo. I DATE I rrrE 1 (SOURS) l REASON 2 ; ,,,, ,,,c,,,3  ; ,,,,,,, ,,cy,,,,c, 7 I I I I I I I I I i 1. l 011 l 891118 l F l 24.4 l A l .3 l 89-015-00 l~ JJ l INvT l The reactor tripped due to a turbine trip l l 1 1 I l 1 l l l l following the loss of the inverter which l l l l l l l 'l l l l ' supplies power to the ~ digital electro-hydraulic l l l l l l l l ) l l control (DEET) system. The inverter was. ,! l 1 l l l 1 l l l l repaired, testing was performed, and the unit. Jl l l l 1 1 I I l l l returned to power operation. l l l l 1 l' I I I I I 'l l I I I I I I I I I 'l i I I I I I i 1 1 1 1 I I I I I I I i l 1 -l' I I I I I I I I i I i l i l l I l l l 1 I l' I I I I i i i I I i 1. I I I I i 1 I I I i .I I I I I I I I I I I i 4 I I I I I i l i i i l-1 i l i I I I I I i i i I I I I I I I I I I I I I I I i i i l i I I I I I I I I I I I I I I I I I i i i I I I I I I I I I I I I I I F: Forced Reason: Method:

  • Exhibit G-Instructions S: Scheduled A-Equipnent Failure (Explain) 1-Manual for Preparation of Data B-Maintenance or Test 2-Mantaal Scram. Entry Sheets for Licensee c-Refueling 3-Automatic Scram. Event Report lLER) File (NUREG-D-Regulatery Restriction 4-Other (Explain) 0161)

E-Operator Training & License Examination F-Administrative Exhibit I -Same Source G-Operational Error (Explain) (9/77) H-Other (Explain) M IDt]R N _ _ _ _ __ __ . , _ _}}