ML19331B855

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Monthly Operating Rept for Jul 1980
ML19331B855
Person / Time
Site: La Crosse File:Dairyland Power Cooperative icon.png
Issue date: 08/04/1980
From: Goodman L
DAIRYLAND POWER COOPERATIVE
To:
Shared Package
ML19331B852 List:
References
NUDOCS 8008130418
Download: ML19331B855 (10)


Text

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OPERATING DATA REPORT DOCKET NO. _50-409 DATE 08-04-80 COMPLETED BY L.S. GOODMAN 608-689-2331 TELEPHONE OPERATING STATUS b"I

1. Unit Name: La Crosse Bollina Water Reactor 0000. 80-01-07 to 2400. 80-31-07
2. Reporting Period:

165

3. Licensed Thermal Power ISIWti:

65.3

4. Nameplate Rating (Gross MWel:

50 S. Design Electrical Rating (Net MWel:

50

6. Maximum Dependable Capacity (Gross MWel:

48

7. Masimum Dependable Capacity (Net MWel:
8. If Changes Occur in Capacity Ratings titems Number 3 Through 71 Since Last Report. Give Reasons:
9. Power Lesel To hhich Restricted. lf Any (Net MWel:
10. Reasons For Restrictions. If Any:

This Month Yr..to.Date Cumulathe 744 5111 94226

11. Hours In Reporting Period 744 4365.9 62171.4
12. Number Of Hours Reactor Was Critical 0

0 478

13. Reactor Reserve Shutdown Hours 744.0 4237.0

_57.241.8

14. Hours Generator On_Line 0

0 79

15. Unit Reserse Shutdown Hours 95,274.0 564,799.7 7.849.580.2
16. Cross Thermal Energy Generated IMWHi
17. Gross Ettetrical Energy Generated (MWH 26,607____ _

164,176 2,363,308 24,714 153,301 2.186.036 lb. Net Electrical Energy Generahd (MWHI 100.0 82.9 60.8

19. Unit Service Factor 100.0 82.9 60.8
20. Unit Availability Factor 69 2 62.5 48.3
21. Unit Capacity Factor (Using MDC Neil 66.4 60.0 46.4
22. Unit Capacity Factor (Using DER Nett 0

6.0 6.4

23. Unit Forced Outage Rate
24. Shutdowns Scheduled Oser Nest 6 Months tType. Date,and Duration of Eachr ESTIMATED REFUELING OUTAGE. OCTOBER 17. 1980 (6 WEEKS)

NA

25. If Shut Down -\\t End Of Reivort Period, binnated Date of Startup.

l'orecast schiesed

26. Units in Test Status iPrior to ( ummercial Ogwration s INill \\L ( R111( At.IIY INill \\l. I l l t I Rl( Ili t o\\l\\ll Rt I \\1 Ol>l H \\ IION 4

I

.S0081304l$

AVERACE DAILY UNIT POWER LEVEL DOCKET NO. 50-409 UNIT LACBWR DATE 08-04-80 L.S.G00M COMPLETED BY 608-689-2331 TELEPHONE MONTil JULY 1980 DAY AVER AGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL IMWe-Net)

(MWe-Net) 16 I

17 37 2

20 18 37 3

22 19 36 4

24 20 21 5

26 21 32 6

29 22 37 31 23 37 8

11 24 37 9

35 25 37 10 37 26 38 11 17 27 38 12 37 38

s 13 37 29 37 14 16 30

'47 15 37 31 17 16 37 INSTR UCTIONS On thn f ormat. int the aserage dady unit power leselin MWe-Net for eat h day in the reporting sponth. Compute to the nearest whole nwpwatt.

(9/77i

d 50-409 DOCKET NO.

UNIT SHUlDOWNS AND POWER REDUCTIONS UNIT N AME LACBWR DATE 08-04-80 REPORT MONTil JULY 1980 COMPLETED BY L.S. GOODMAN TELEPHONE 608-689-2331 e.

5?

3 hY Licensec

,E-r, Cause & Corrective o

Date i

3?

4

.5 s E Evens 3,7 o-3 Action to y'

yE j ;jj Repori e in U Prevent Recurrence H

c5 80-06 07-19-80 F

0 A

4 NA CB PUMPXX IB FORCED CIRCULATION PUMP TRIPPED DUE TO LOW SEAL INJECTION LEAK-OFF FLOW WHICH OCCURRED WHEN RETURNING THE IB SEAL INJECTION PUMP TO STANDBY DUE TO THE SEAL INJECTION PUMPS' BY-PASS VALVES NOT COMPENSATING FAST ENOUGH TO MAINTAIN SUFFICIENT FLOW TO THE FCP's.

THE STANDBY SEAL INJECT-10N PUMP HAD STARTED DUE TO A SYSTEM SURGE WHEN PLACING A CLEANED SEAL IN-JECTION FILTER BACK IN STANDBY. THE 1A SEAL INJECTION PUMP WAS SUCCESS-FULLY PLACED IN STANDBY ON A SUBSE-QUENT TRY. THE IB FCP WAS PROMPTLY RESTARTED AFTER IT TRIPPED. THE SEAL INJECTION SYSTEM WILL BE THOROUGHLY EXAMlHED DURING THE NEXT COLD SHUT-DOWN.

I 2

3 4

I forced Reason.

Metimd:

Exhibit G. Instructions S S6 heduled A. Equipment Failure (Explain)

I-Manual for Pseparation of Data B. Maintenance of Test 2 Manual Serain.

Entry Sheets for Licensee C Refueling 3 Automatic Scram.

Event Report (1.1 R) File (NL'RI G-D Regulatory Restriction 4-Ot her ( Explain) 0161) l-Operator Training & License 1:xamination F Administratne 5

G Operational Error (Explain)

Eshibit I - Same Source 08/77)

Il-Ot her ( E xplain )

.c

NARRATIVE

SUMMARY

OF OPERATING EXPERIENCE JULY,1980 At the onset of the July 1980 reporting period, power escalation was continuing following the June 21 - 29 outage for the repair of a seal leak in Upper Control Rod Drive Mechanism No. 24.

On July lQth, 85% Reactor Rated Thermal Power (37 MWe-Net) was achieved.

This operating level has been scheduled to extend core life to stretch optimum production until refueling becomes necessary.

Power generation continued at this level until July 19th at 2214, when IB Forced Circulation Pump (FCP) tripped due to low seal injection leakoff flow, which occurred when returning the 1B Seal Injection Pump to standby.

The low leakoff flow condition occurred because the Seal Injection Pumps' bypass valves did not compensate fast enough to maintain sufficient flow to the FCP's.

The standby Seal Injection Pump had started due to a system surge

-when placing a cleaned seal injection filter back in standby'.

The 1B FCP was promptly restarted and the 1A Seal Injection Pump was successfully placed in standby on a subsequent try.

The Si;l Injection System will be thoroughly examined during the next cold shutdown.

Reactor power decreased to a minimum of 34% Reactor Rated Thermal Power (12 MWe-Net) prior to power re-escalation.

On July 21st, 85% Reactor Rated Thermal Power (37 MWe-Net) was again achieved.

Operation continued at this power level throughout the remainder of the July 1980 reporting period.

Significant maintenance itemn performed during the July 1980 reporting period are indicated on the attached Instrument and Electrical and Mechanical Maintenance listings.

3

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s I of 2 INSTRUMENT AND ELECTRICAL MAINTENANCE JULY, 1980 LER OR NATURE OF OUTAGE MALFUNCTION EQUIPMENT MAINTENANCE

. NUMBER CAUSE RESULT-CORRECTIVE ACTION NUCLEAR INSTRUMENTATION CORRECTIVE NA NORMAL USAGE CHART DRIVE INOP-ADJUSTED CHANNEL '5 MR 3212 ERATIVE RECORDER DRIVE NUCLEAR INSTRUMENTATION PREVENTIVE NA TEST DUE COMPLETED TESTS COMPLETE TECH. SPEC.

TESTS N-5 THROUGH N-9 SAFETY SYCTEM PREVENTIVE NA TEST DUE COMPLETED TESTS COMPLETE SAFETY SYSTEM TECH. SPEC. TESTS FOR.

CHANNELS 1, 2, AND H O 2

NO. 3 FIRE DETECTION PREVENTIVE NA TEST DilE COMPLETED TFSTS COMPLETED FIRE DETECTOR TESTING RADtAfl0N MONITORING PREVENTIVE NA TEST DUE COMPLETED TESTS COMPLETED FIXED RADIATION SYSTEM MONITORING TESTING TURBINE ROTOR ALARM CORRECTIVE NA NORMAL USAGE INOPERATIVE ALARM ADJUSTED AND LUBRICATED MR 3215 LIGHT CONTACT PlVOT DECAY HEAT VALVE SOLEN 0ID CORRECTIVE NA UNKNOWN SOLEN 0ID C0ll REPLACED SOLEN 0ID Colt VALVE MR 3229 BURNED OUT CONTROL AIR DRYER CORRECTIVE NA CONTAMINATION STICKING PURGE CLEANED AND LUBRICATED 1B VALVE MR 3222 VALVE IB VALVE -

OFF-GAS FLOW INDICATOR CORRECTIVE NA CONTAMINATION PLUGGED INDICATOR CLEANED FLOW METER MR 3231 REACTOR VENT FAN CORRECTIVE NA PLUGGED FILTERS MOTOR OVERHEATED REPLACED MOTOR AND MR 3233 FILTERS FUEL GRAPPLE TOOL CORRECTIVE NA LACK OF LUBRl-TOOL HANGUP RELUBRICATED MR 3223 CATION ENVIRONMENTAL AIR PUMP CORRECTIVE M

NORMAL USAGE DEFECTIVE FAN REPLACED FAN WITH METAL MR 3220 FAN TURBINE EXPANSION CORRECTIVE NA NORMAL USAGE DEFECTIVE Su-!TCH REPLACED ROTORY SWITCH RECORDER MR 3253 IN RECORDER m

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2 of 2 INSTRUMENT AND ELECTRICAL MAINTENANCE JULY 1980 LER OR NATURE OF OUTAGE MALFUNCTION EQUIPMENT MAINTENANCE NUMBER CAUSE RESULT CORRECTIVE ACTION

. TEST EQUIPMENT CAllBRA-PREVENTIVE NA TESTS DUE COMPLETED TESTING CAllBRATED ALL SHOP TION TEST EQUIPMENT SECURITY EQUIPMENT -

CORRECTIVE NA UNKNOWN 000R IN ALARM ADJUSTED BIAS MAGNET ZONE 10 MR 3214 FOR ZONE 10 SECURITY EQUIPXENT -

CORRECTIVE NA NORMAL USAGE SIDE CLIPS WORN REPLACED SIDE CLIPS IN 000R READER MR 3210 OUT READER SECURITY EQUIPMENT -

CORRECTIVE NA HIGH WIND TURNED CAMERA REALIGNED CCTV CAMERA ZONE 7 CAMERA SECURITY EQUIPMENT -

CORRECTIVE NA NEW INSTALLATION UNITS ALARMING ADJUSTED ALARM SWITCHES CRIO HOUSE HATCHES SECURITY EQUIPMENT -

CORRECTIVE NA NORMAL USAGE POOR PICTURE READJUSTED MECHANICAL SPARE CCTV MR 3236 FOCUS SECURITY EQUIPMENT -

CORRECTIVE NA MANUFACTURER POOR SENSITIVITY COMPLETED SYSTEM CRIB HOUSE E-F! ELD MR 3258 MODIFICATION MODIFICATION SECURITY EQUIPMENT -

CORRECTIVE NA UNKNOWN INOPERATIVE REPAIRED READER l

CRIB HOUSE READER MR 3247 SECURITY EQUIPMENT -

CORRECTIVE NA SPIDERS AND INOPERATIVE CLEANED READER STACK SHACK READER MR 3266 BUGS SECURITY EQUIPMENT -

CORRECTIVE NA NEW INSTALLATION INOPERATIVE ADJUSTED FOR PROPER i

MAIN AIRLOCK READER MR 3263 OPERATION SECURITY EQUIPMENT -

CORRECTIVE NA UNKNOWN NO ALARM RESET ADJUSTED FOR PROPER 4

FRONT 000R ALARM MR 3267 OPERATION SECURITY SYSTEM ZONE 19.5 CORRECTIVE NA UNKNOWN NO ALARM RESET ADJUSTED SECURITY ALARM MR 3277 I

ENVIRONMENTAL AIR MONITOR CORRECTIVE NA NORMAL USAGE TIME METER WORN REPLACED TIME METER MR 3282 OUT i

FUEL SIPPING FIXTURE FACILITY CHANGE NA THERM 0 COUPLES NOT NOT REQUIRED REMOVE THERMOCOUPLES FROM i

FC-77-05 REQUIRED SIPPING FlXTURE AND PLUGGED OPENINGS 1

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MECHAMTCAT, MAINTENANCE JULY 1980 IER OR

!!ATURE Of DUTAGE

.SAtfufCTIO!i EQUIPMEtlT f'Alf4TEllAf;CE f.UTEE R CAUSE RESULT CORRECTIVE ACTION

^

RESIN DEWATERING PUMP CORRECTIVE NA WORN IMPELLER.

WOULD NOT. PUMP REPLACED. IMPELLER MR 3219

-0FF-GAS VALVE CORRECTIVE NA SPRING TENSION STEAM LEAK REPLACED STEM, DISC NO. 55-22-001 MR 3227 NOT SET.

STEAM SEAT AND NEW GASKETS CUT SEAT AND DISC.

OFFCGAS RECOM81NER CORRECTIVE NA CATALYST WAS NOT RECOMBIN-REPLACED NEW CATALYST MR 3227 DEPLETED ING PROPERLY SEAL WELDED CARTRIDGE l.D.

TORQUED BOLTS TO 975 Ft/Lbs.

SEAL WATER FILTERS PREVENTIVE NA NA NA CHANGED FILTERS WELL WATER FILTERS PREVENTIVE NA NA NA CHANGED FILTERS OFF-GAS DRYER 1B CORRECTIVE NA LEAK IN LINE WAS NOT COOLING FIXED LEAK AND RECHARGED HR 3251 DOWN WITH FREON WASTE WATER TOTAll2ER CORRECTIVE NA WAS DIRTY WAS NOT READING CLEANED SCREENS MR 3226 FLOW

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