05000306/LER-1980-020-01, /01T-0:on 800715,during Severe Electrical Storm Several Breakers Operated.Main Generator Was Separated from Grid & Reactor & Reactor Coolant Pumps Tripped.Caused by Electrical Storm.Next Day Conditions Returned to Normal

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/01T-0:on 800715,during Severe Electrical Storm Several Breakers Operated.Main Generator Was Separated from Grid & Reactor & Reactor Coolant Pumps Tripped.Caused by Electrical Storm.Next Day Conditions Returned to Normal
ML19330B466
Person / Time
Site: Prairie Island Xcel Energy icon.png
Issue date: 07/29/1980
From: Hunstad A
NORTHERN STATES POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML19330B462 List:
References
LER-80-020-01T, LER-80-20-1T, NUDOCS 8008040054
Download: ML19330B466 (1)


LER-1980-020, /01T-0:on 800715,during Severe Electrical Storm Several Breakers Operated.Main Generator Was Separated from Grid & Reactor & Reactor Coolant Pumps Tripped.Caused by Electrical Storm.Next Day Conditions Returned to Normal
Event date:
Report date:
3061980020R01 - NRC Website

text

CRC FORM 306 U.1. NUCLEA*3 f.EIULATORY COMMISSION (7 771 LICENSEE EVENT REPORT CONTROL BLOCK: l l

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8 60 68 DOCKET NUMRER 88 89 EVENT DATE 74 75 REPOR T ?) ATE 80 EVENT DESCRIPTION AND PROBA8LE CONSEQUENCES h O 2 l With Unit 2 at 100% power and Unit 1 at cold shutdown. a severe electrical storm 1

0 a l caused operation of several breakers in the substation.

At about 2030 the main

_l 0 4 l Renerator was separated from the erfd and rho ronnent and rancenr enninne nnmna l

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Natural circulation unn egenblinhed fnr enre ennling.

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At about i

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(a degraded one), the diesel generators started and closed in on the safeguards buses.

l0l8l l No safety injection ves actuated. Not repetitive.

No effect on oublic health l

7 8 9 safety.

SYSTEM

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i i itransformer was restored. At 0137 the next day conditions at the substation I

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